If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-151-22155 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.800296594,"lon":-81.56087413,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Tuscarawas Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: VETTE R& J | |
License Status: Producing | |
License Date: 1970-09-01 | |
Spud Date: 1970-09-01 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-09-16 | |
Well Total Depth: 4271 ft | |
Configuration: Vertical | |
Latitude: 40.800296594 | |
Longitude: -81.56087413 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1970-09-01 | 182 BELDEN & BLAKE CO GeoDate 9/1/70 |
Original Spud | 1970-09-01 | EB-1021.49, KB-1028.5, LOG TYPE=HI |
Completed | 1970-09-16 | EB-1021.49, KB-1028.5, LOG TYPE=HI |
Reached Total Depth | 1970-09-16 | EB-1021.49, KB-1028.5, LOG TYPE=HI |
Change of Owner | 2002-08-12 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2015-01-22 | Operator changed from 1966, PETROX, INC to 7578, ENERVEST OPERATING L |
Record Last Modified | 2019-06-04 | EB-1021.49, KB-1028.5, LOG TYPE=HI |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4072 | 4200 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 23350 Gal | 8000 |
For data sources see[4]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BELDEN & BLAKE CORPORATION | Brine | 0 | 0 |
1985 | BELDEN & BLAKE CORPORATION | Brine | 2 | 0 |
1986 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
1987 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
1988 | BELDEN & BLAKE CORPORATION | Brine | 0 | 366 |
1990 | BELDEN & BLAKE CORPORATION | Brine | 0 | 356 |
1991 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
1992 | BELDEN & BLAKE CORPORATION | Brine | 0 | 359 |
1993 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
1994 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
1996 | BELDEN & BLAKE CORPORATION | Brine | 0 | 366 |
1997 | BELDEN & BLAKE CORPORATION | Brine | 0 | 358 |
1998 | BELDEN & BLAKE CORPORATION | Brine | 0 | 358 |
1999 | BELDEN & BLAKE CORPORATION | Brine | 0 | 365 |
2000 | BELDEN & BLAKE CORPORATION | Brine | 0 | 359 |
2001 | BELDEN & BLAKE CORPORATION | Brine | 0 | 318 |
2002 | PETROX, INC | Brine | 0 | 28 |
2003 | PETROX, INC | Brine | 0 | 365 |
2004 | PETROX, INC | Brine | 0 | 365 |
2005 | PETROX, INC | Brine | 0 | 365 |
2006 | PETROX, INC | Brine | 0 | 365 |
2007 | PETROX, INC | Brine | 365 | |
2008 | PETROX, INC | Brine | 0 | 365 |
2009 | PETROX, INC | Brine | 0 | 324 |
2010 | PETROX, INC | Brine | 0 | 365 |
2011 | PETROX, INC | Brine | 0 | 365 |
2012 | PETROX, INC | Brine | 0 | 366 |
2013 | PETROX, INC | Brine | 0 | 365 |
2014 | PETROX, INC | Brine | 0 | 365 |
2015 | PETROX, INC | Brine | 0 | 60 |
2016 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
2017 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2018 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0256342955 | 2009-09-24 | Production Wells | No Violations | The excavation around the wellhead is filled in. There is a swab rig on the well. The complaint is RESOLVED. |
0692163391 | 2009-04-28 | Production Wells | No Violations | I received a call on 4-27-2009 from Steve Collins (Massillon Fire Department, 330-833-1053) regarding an odor complaint at a well located at 106 Rolling Park Dr., Massillon, OH. On 4-28-2009, I met with John Casper (Rolling Hills Trailer Park) at the well site. A gas leak was reported on Sunday 4-26-2009 and the Massillon Fire Department responded. Petrox was notified and addressed the leak. During my inspection on 4-28-2009, I called Bill Magrell (330-565-5873) with Petrox to get the details of the incident. Gas had been leaking from under the production string casing hanger out of the surface casing. The surface casing was loaded with water to kill the gas. A hole was drilled in the surface casing to monitor for gas. During my inspection there was no gas present. Petrox will evaluate the leak and then repair the casing or plug the well. I informed the Massillon Fire Department of my findings. I talked to Cindy (Rolling Hills Trailer Park) later that day and informed her of the situation. |
0710964767 | 2009-05-05 | Production Wells | No Violations | The excavation at the wellhead is still open. There was no visible venting or odor coming from the port in the casing. I met with Justin (Cindys son), who is in charge of maintenance. |
0738779186 | 2014-03-27 | Production Wells | No Violations | I was on location to obtain updated GPS coordinates for this well. During my inspection I found a plunger lift well with a 100bbl production tank and separator all enclosed in a fence. The well is located in a manufactured home park. The wellhead is in good conditioned has proper I.D. signage with 55psi of pressure on the tubing. There are no violations at this time. |
For data sources see[9]