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Well ID: 34-067-20637 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Washington Township | |
Operator Name: TIPKA ENERGY DEVLOPMENT COMPAN | |
Well Pad ID: | |
Farm/Lease Name: CROSSAN UNIT | |
License Status: Producing | |
License Date: 1998-12-17 | |
Spud Date: 1983-10-16 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1983-10-21 | |
Well Total Depth: 5939 ft | |
Configuration: Vertical | |
Latitude: 40.232342537 | |
Longitude: -81.33558885 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1983-09-14 | 2559 WNT OPERATING INC GeoDate 9/14/83 |
Oil and Gas | 1983-09-14 | Issued Date 9/14/83 Expired Date 3/12/84 Acres 0104000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05939 Proposed Drill Depth 05939 |
Original Spud | 1983-10-16 | |
Completed | 1983-10-21 | |
Reached Total Depth | 1983-10-21 | |
Completion Report Received | 1983-11-07 | |
Construction Permit Expires | 1984-03-12 | |
Change of Owner | 2001-09-05 | Operator changed from 2559, WNT OPERATING INC to 2543, TIPKA ENERGY DEVLOP CO |
Last Compliance Report | 2016-09-30 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5700 | 5812 | 0 |
2006-09-11 | 5733 | 5806 | 19 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 72000 Gal | 50000 | FRAC; FLUID & SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1561170215 | 2016-06-15 | Production Wells | No Violations | On the day of my inspection, I witnessed this is a plunger- lift system well, using 2 inch diameter production tubing placed inside 4.5 inch diameter production casing. The plunger is being operated by a motor valve. Two domestic gas hook ups are present at the well head and one domestic gas hook up is present at the separator. Production equipment for this well includes a 100 bbl. production tank, a horizontal separator and a 2 inch diameter meter run; all placed inside an earth dike that measures approximately 40*30 feet at an average height of 4 foot. Proper identification was in place on the tank battery at the time of my inspection. RBDM records indicate the well is in producing order. |
1964271281 | 2016-09-20 | Temporary Abandoned Annular Disposal | No Violations | On the day of my inspection, I witnessed this is a plunger- lift system well, using 2 inch diameter production tubing placed inside 4.5 inch diameter production casing. The plunger is being operated by a motor valve. Two domestic gas hook ups are present at the well head and one domestic gas hook up is present at the separator. Production equipment for this well includes a 100 bbl. production tank, a horizontal separator and a 2 inch diameter meter run; all placed inside an earth dike that measures approximately 40*30 feet at an average height of 4 foot. Proper identification was in place on the tank battery at the time of my inspection. My inspection revealed no indication the well is being used for annular disposal use. |
For data sources see[9]