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Well ID: 34-005-22012 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Mifflin Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: ANDRESS-WINKLER | |
License Status: Storage Well | |
License Date: 2012-10-22 | |
Spud Date: 1961-12-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1962-03-27 | |
Well Total Depth: 2577 ft | |
Configuration: Vertical | |
Latitude: 40.783561083 | |
Longitude: -82.37007108 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1961-12-13 | |
Completed | 1962-03-27 | |
Reached Total Depth | 1962-03-27 | |
Record Last Modified | 2013-05-23 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0406281397 | 2017-04-11 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is shut in. There is no separator at the well. |
1349358391 | 2012-09-18 | Storage Well | No Violations | Contacted by operator to witness a liner set and cement across formation to rehabilitate well. Set and cement 3 inch liner over formation. Pump cement though 2467 ft of used 2.375 inch tubing stung into liner hanger. Use latch down wiper plug that was seated. Pull tubing out of liner hanger then wash out hole. |
1511122291 | 2015-07-08 | Storage Well | No Violations | The surface owner, Dave Baker, contacted the inspector regarding a large area of dead vegetation around the well and fluid leaking from the well. The landowner was on site during the inspection. Dead vegetation starts on the hill just above the pipeline tie in and proceeds down hill and down the ditch along the access road from that point. There was a small puddle of standing water near the pipeline that had an orange color and a sheen on top. The water tested 0.8 on a high range Quantab which corresponds to less than 291 ppm Chloride. The sheen broke up into platy structures when disturbed indicating organic material and not oil. Another puddle at the access road below the well tested 0 for chlorides on a high range Quantab strip. A third puddle was tested in the access road ditch below the well location and indicated no detectable Chloride. Columbia Gas was contacted and advised to check the well for problems. The valve on the surface casing annulus was closed and a bull plug was in the valve. No leaks were observed from the well or pipeline. The source of the fluid that killed the vegetation around the well is not clear at this time. The hill around the well is wet indicating a seep, however the water tested at the location is not salty. Dave Baker can be reached at 419-368-7756. Terry VanSickle of Columbia checked the well and did not find an issue there. He stated that a vegetation management contractor was working on the pipeline right of way and that they applied herbicide that caused the dead vegetation. |
1512500380 | 2012-10-05 | Storage Well | No Violations | Inspect well location and gather GPS data. Well has been completed after re-habilitation. Rig moved off site. Pits open and tanks on location. |
1598102832 | 2018-04-19 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is shut in. |
1716757905 | 2013-11-20 | Storage Well | No Violations | ID posted, location maintained. |
1729813163 | 2016-08-10 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is shut in. The well is not equipped with a separator. The well location is dry and vegetated. Vegetation has recovered from last year. |
1740038987 | 2014-10-01 | Storage Well | No Violations | ID posted, location maintained. |
2137858901 | 2019-03-08 | Storage Well | No Violations | Performed annual inspection for Columbia Gas Storage Well #10356 on 03/08/2019. The well is equipped with a flanged wellhead with 1-master valve and 1-wing valve. Well identification is clearly displayed. The well is located ~260 from its RBDMS location. A map showing the location discrepancy, as well as a request for the location to be updated in RBDMS was sent to Aaron Lantz (DOGRM Columbus). No other problems were noted at the time of the inspection. |
For data sources see[3]