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34-153-22661

Well Details

Well ID: 34-153-22661
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Country: United States
State: Ohio
County: Summit
Municipality: Bath Township
Operator Name: ST CROIX LTD
Well Pad ID:
Farm/Lease Name: BILLMAN
License Status: Producing
License Date: 2019-03-25
Spud Date: 1990-08-28
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]]
Final Drill Date: 1990-09-03
Well Total Depth: 3631 ft
Configuration: Vertical
Latitude: 41.154465502
Longitude: -81.62864119

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1990-05-16 2364 ST CROIX LTD GeoDate 5/16/90
Oil and Gas 1990-05-16 Issued Date 5/16/90 Expired Date 5/16/91 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03631 Proposed Drill Depth 03631
Original Spud 1990-08-28
Completed 1990-09-03
Reached Total Depth 1990-09-03
Completion Report Received 1990-10-21
Construction Permit Expires 1991-05-16
Record Last Modified 2019-04-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3405 3470 0
2006-09-11 3439 3469 35

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 105175 Gal 56000 FRAC:WATER/SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1990 ST CROIX LTD 2280 993 122
1991 ST CROIX LTD 3923 1708 365
1992 ST CROIX LTD 2516 957 365
1993 ST CROIX LTD 3160 400 365
1994 ST CROIX LTD 1399 260 365
1995 ST CROIX LTD 723 116 365
1996 ST CROIX LTD 3179 304 365
1997 ST CROIX LTD 3035 410 365
1998 ST CROIX LTD 664 231 365
1999 ST CROIX LTD 501 110 365
2000 ST CROIX LTD 515 160 365
2001 ST CROIX LTD 708 149 365
2002 ST CROIX LTD 756 86 365
2003 ST CROIX LTD 468 112 365
2004 ST CROIX LTD 468 90 365
2005 ST CROIX LTD 492 109 365
2006 ST CROIX LTD 455 68 365
2007 ST CROIX LTD 424 114 365
2008 ST CROIX LTD 407 99 365
2009 ST CROIX LTD 344 56 365
2010 ST CROIX LTD 323 0 365
2011 ST CROIX LTD 336 21 365
2012 ST CROIX LTD 353 17 366
2013 ST CROIX LTD 342 16 365
2014 ST CROIX LTD 247 10 365
2015 ST CROIX LTD 238 22 365
2016 ST CROIX LTD 0 0 0
2017 ST CROIX LTD 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1990 ST CROIX LTD Brine 2136 122
1991 ST CROIX LTD Brine 1227 365
1992 ST CROIX LTD Brine 297 365
1993 ST CROIX LTD Brine 284 365
1994 ST CROIX LTD Brine 218 365
1995 ST CROIX LTD Brine 157 365
1996 ST CROIX LTD Brine 282 365
1997 ST CROIX LTD Brine 254 365
1998 ST CROIX LTD Brine 306 365
1999 ST CROIX LTD Brine 422 365
2000 ST CROIX LTD Brine 346 365
2001 ST CROIX LTD Brine 330 365
2002 ST CROIX LTD Brine 327 365
2003 ST CROIX LTD Brine 462 365
2004 ST CROIX LTD Brine 253 365
2005 ST CROIX LTD Brine 158 365
2006 ST CROIX LTD Brine 188 365
2007 ST CROIX LTD Brine 276 365
2008 ST CROIX LTD Brine 130 365
2009 ST CROIX LTD Brine 85 365
2010 ST CROIX LTD Brine 0 365
2011 ST CROIX LTD Brine 45 365
2012 ST CROIX LTD Brine 162 366
2013 ST CROIX LTD Brine 92 365
2014 ST CROIX LTD Brine 101 365
2015 ST CROIX LTD Brine 87 365
2016 ST CROIX LTD Brine 0 0
2017 ST CROIX LTD Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL4139 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1345387631 2012-03-30 Orphan No Violations The recent failure of an earthen dam located west of the Billman wellhead has exposed the flowline to the tank battery. I advised them to shut the well in to prevent the possibility of a release from the flowline. St. Croix instead has stated that they intend to reenforce the flowline with added support and are monitoring the facility. The inspection of the tank battery found that the Billman stock tank has rusted through and is no longer being used and must be removed. Instead liquid production from the Billman is being directed to one of the other stock tanks in the tank battery. The other tanks in the tank battery have recently been patched and may need to be replaced. Minor amounts of staining were present below the patches. The gates to the tank battery were not locked as required. Failure to address these concerns by May 15 will result in a written violation.

For data sources see[9]

References