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Well ID: 34-155-20157 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Newton Township | |
Operator Name: ERIC PETROLEUM CORP | |
Well Pad ID: | |
Farm/Lease Name: BEER CLANENCE & CHARLENE | |
License Status: Producing | |
License Date: 2006-09-12 | |
Spud Date: 1974-01-22 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-02-10 | |
Well Total Depth: 4667 ft | |
Configuration: Vertical | |
Latitude: 41.181516543 | |
Longitude: -80.91526423 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 1100 GM/DELPHI PACKARD ELEC. |
Original Spud | 1974-01-22 | |
Completed | 1974-02-10 | |
Reached Total Depth | 1974-02-10 | |
CO | 1996-07-11 | 4884 EASTERN STATES OIL & GAS GeoDate |
Change of Owner | 2005-06-07 | Operator changed from 4884, EASTERN STATES OIL & GAS INC to 7849, NCL NATURAL RESOURCES LLC |
Change of Owner | 2017-02-21 | Operator changed from 7849, NCL NATURAL RESOURCES LLC to 5054, ERIC PETROLEUM CORP |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4453 | 4510 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | ||||
H2O | 0 | 79000 Gal | 70000 | INITIAL SHUT-IN WELLHEAD PRESS = OSIG/72 HRS. |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1553766249 | 2007-11-01 | Production Wells | No Violations | no violations . |
1620212597 | 2013-08-22 | Production Wells | No Violations | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery contained a 100 barrel production tank. There were plugs on the load lines. The dike had a 4 PVC drain with a cap and mets containment requirements. The heat, treated separator had the correct spacing and contained a 7 day production chart. An identification sign was posted on the production tank. The lease road was in good, working condition. |
For data sources see[9]