X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-007-24408

Well Details

Well ID: 34-007-24408
Loading map...
Country: United States
State: Ohio
County: Ashtabula
Municipality: Geneva
Operator Name: ANDRUS DONALD
Well Pad ID:
Farm/Lease Name: ANDRUS
License Status: Producing
License Date: 2008-09-30
Spud Date: 2006-06-16
Spud Drilling Contractor: APPALACHIAN DRILLING
Final Drill Date: 2006-06-24
Well Total Depth: 2854 ft
Configuration: Vertical
Latitude: 41.850266956
Longitude: -80.91786536

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2006-03-20 Proposed Formations:CLINTON, Issued Date:3/20/2006, Expired Date:3/20/2007 6:00:00 AM, Drilling unit acres:69.5, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 2006-06-16
Reached Total Depth 2006-06-24
Construction Permit Expires 2007-03-20
Completion Report Received 2008-09-30
Change of Owner 2011-12-12 Operator changed from 4415, PLATEAU ENERGY CORP to 8898, ANDRUS DONALD
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2008-11-17 2723 2744 13

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 600 Bbl 15000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 PLATEAU ENERGY CORP 428 0 300
2015 ANDRUS DONALD 674 0 365
2016 ANDRUS DONALD 895 0 365
2017 ANDRUS DONALD 643 5 360

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 PLATEAU ENERGY CORP Brine 0 300
2015 ANDRUS DONALD Brine 75 365
2016 ANDRUS DONALD Brine 0 365
2017 ANDRUS DONALD Brine 12 360

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0157559799 2006-08-03 Production Wells No Violations On site to collect soil samples in brine dumping area .
0351553476 2006-08-23 Preliminary Restoration No Violations Pit solidification approved .
0402359752 2007-01-18 Preliminary Restoration No Violations Remedial work has not been completed .
0465062785 2006-06-19 Drill / Deepen / Reopen No Violations On site to test B.O.P. on coductor casing . Test B.O.P. at 250 p.s.I. With no loss after 15 minutes .
0724360543 2006-08-09 Production Wells No Violations Inspection showed no remedial has been done to remove contaminated soil .
0989822243 2006-07-31 Production Wells No Violations Inspection showed fluid in working pit had been lowered , blow pit was full to top . There has been no action to remove contaminated soil at this time .
1021939416 2006-08-02 Production Wells No Violations Inspection showed company pumping fluid from blow pit into frac tanks .
1138963771 2006-06-21 Drill / Deepen / Reopen No Violations On site to test B.O.P. on surfsce casing . Test B.O.P. at 400 p.s.I. With no loss after 15 minutes .
1151398993 2006-08-22 Preliminary Restoration No Violations On site for solidification of drilling pits .
1154365724 2006-07-26 Drill / Deepen / Reopen Violations Noted Arrived on site to find a 2 water pump set at n-w corner of blow pit . There was a 2 rubber hose from pump 40 then hooked to 2 plastic flowline . The 2 plastic line then run west on top of surface 600 when it turned north for another 300 . The line had a hammer union connection at this point , which was not connected . I then smelled a very strong odor of oilfield brine . There were sevaral large puddles of fluid running n-e of 2 plastic pipe . 1176 quantab readings of fluid showed chloride levels off the scale of the quantab { 6000+ ppm } . I then observerd a area of dead vegetation and trees in a 150 diameter along route brine traveled , the kill area the narrowed to 10-20 and traveled another 250+ n-e where the kill area ended . I then collected water samples at beginning of spill . I took several photos { water pump location , 2 plastic pipe & kill area } . Water samples were transported to lab for analsis . I contacted Bob Anderson and advised of immediate clean-up needed { remove all free standing brine from kill area } . The case # given to this investigation is # 06-013 in complaint log .
1812257994 2006-06-15 Drill / Deepen / Reopen No Violations Appalachian Drilling rigging up drilling rig . On site for lake plain pit constuction .
1904530516 2006-06-20 Drill / Deepen / Reopen No Violations Driiling rig trying to kill gas to run surface casing .
1993919860 2006-09-29 Production Wells No Violations There has been no soil removed per notice requirements .
2021875038 2006-06-22 Drill / Deepen / Reopen No Violations On site to wittness flaring of gas . The first pocket of gas was encountered at 469 . Drilling at 1500 when I left site .

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1154365724 US-OH-104031 2006-07-31 Drilling operation causing pollution and contamination

For data sources see[9]

References