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Well ID: 34-115-24673 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Deerfield Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: DAYSPRING UNIT | |
License Status: Producing | |
License Date: 2013-04-03 | |
Spud Date: 2013-04-03 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2013-04-18 | |
Well Total Depth: 6437 ft | |
Configuration: Vertical | |
Latitude: 39.709689401 | |
Longitude: -81.95731466 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2013-03-08 | Proposed Formations:QUEENSTON THRU KNOX, Issued Date:3/8/2013, Expired Date:3/8/2015 12:00:00 PM, Drilling unit acres:50, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2013-04-18 | |
Completion Report Received | 2014-03-31 | |
Construction Permit Expires | 2015-03-08 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2014-04-01 | 6275 | 6341 | 53 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2013-04-24 | ACID | 0 | 0 | 0 | Producers Service Corporation | 53 SHOTS |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | ARTEX OIL COMPANY | 279929 | 908 | 365 |
2015 | ARTEX OIL COMPANY | 185282 | 521 | 365 |
2016 | ARTEX OIL COMPANY | 113951 | 438 | 365 |
2017 | ARTEX OIL COMPANY | 90552 | 297 | 365 |
2018 | ARTEX OIL COMPANY | 66714 | 92 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | ARTEX OIL COMPANY | Brine | 139 | 365 |
2015 | ARTEX OIL COMPANY | Brine | 108 | 365 |
2016 | ARTEX OIL COMPANY | Brine | 63 | 365 |
2017 | ARTEX OIL COMPANY | Brine | 46 | 365 |
2018 | ARTEX OIL COMPANY | Brine | 24 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0798706389 | 2013-09-26 | Preliminary Restoration | No Violations | Preliminary restoration is passed in accordance to 1509.072. |
0966949572 | 2018-12-18 | Production Wells | No Violations | I was on location today to do a field inspection on this well. The well is producing through the 2 inch diameter tubing that is ran inside the 4.5 inch diameter casing. There are 2 -100 barrel storage tanks located at the end of the lease road. The identification for the well is located on the production tank. There are no violations at this time. |
1314406500 | 2013-06-03 | Drill / Deepen / Reopen | No Violations | I accompanied Joe Schneider and Frank Riggle in the field to review the restoration work at all of Artexs most recently drilled wells. The pit was filled and there were dozers on location smoothing out the road and well location. The wellhead is shut in until they install production lines. |
1365036757 | 2013-04-03 | Drill / Deepen / Reopen | No Violations | I was on location to witness the cementing of the conductor casing by Formation Cement Company. There was good returns on the cement job. |
1365175220 | 2013-04-05 | Drill / Deepen / Reopen | No Violations | I was on location to witness the cementing of the 9 5/8 surface casing. The Killbarger IDECO Rig #17 drilled a 12 1/4 hole to a TD of 719. The casing shoe depth was 687. Centralizers were not run on the surface casing and the baffle insert was at a depth of 644. The operator encountered hard sandstone with fresh water at 601-632 which slowed drilling earlier. Formation cement on location. The plug was down at 10:55am with good cement returns, and casing pressure was held at 600 psi for 5 minutes. |
1375900083 | 2013-08-07 | Drill / Deepen / Reopen | No Violations | The well is currently shut in however the lines have been buried and tied into a new separator and tank up at top of acces road. There is a good dike around the tank. Operator still needs to seed and mulch location. |
For data sources see[9]