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Well ID: 34-157-21960 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Warren Township | |
Operator Name: DOVER ATWOOD CORP. | |
Well Pad ID: | |
Farm/Lease Name: NEMETZ | |
License Status: Producing | |
License Date: 1973-06-01 | |
Spud Date: 1973-11-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-04-08 | |
Well Total Depth: 5396 ft | |
Configuration: Vertical | |
Latitude: 40.555774094 | |
Longitude: -81.27727370 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1973-06-01 | 133 QUAKER STATE OIL REF CORP GeoDate 6/1/73 |
Unknown | 1973-06-01 | Issued Date 6/1/73 Expired Date Acres 0000000 Tool Type RTAF Proposed Formation Proposed Depth Proposed Drill Depth |
Original Spud | 1973-11-15 | |
Completed | 1974-04-08 | |
Reached Total Depth | 1974-04-08 | |
Construction Permit Expires | 1974-06-01 | |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 6/1/73 |
Change of Owner | 1999-04-23 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 6351, T & C OIL & GAS COMPANY |
Change of Owner | 1999-05-24 | Operator changed from 6351, T & C OIL & GAS COMPANY to 5935, DOVER ATWOOD CORP. |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5227 | 5289 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 4400 Bbl | 70000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0305293968 | 2018-05-04 | Production Wells | No Violations | Upon arrival on location, I witnessed the well was equipped 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing, and a pumping unit ran with an electric motor. The valves were open on tubing and one of two valves were open on the casing. Production equipment included a steel 100 barrel tank, a vertical separator, and an Roots Meter within an earthen dike. The production report was up to date and proper identification was in place. |
1187272446 | 2007-08-15 | Production Wells | Violations Noted | Arrived on location and found dike full of fluid, also found a buried steel 100 bbl tank. |
1191194459 | 2007-08-29 | Production Wells | No Violations | Check this site for Inspector Grimm and found that it is being cleaned up after an oil spill.Met with the crew and went over clean up and what all is needed and relay info to Inpsector Grimm.Tanks have been pulled and the area under the tanks is being excavaded and removed.Also there are tanks which will need to be repaired or replaced. |
1708554292 | 2007-08-29 | Production Wells | No Violations | Follow up for Inspector Grimm who was on another job.Met clean up crew on site and pumped all free fluid off. Next pull in ground tank.Tank did not have any holes in tank and valve appears to have been damaged when tank was pulled out .Advise Inspector Gr |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1187272446 | US-OH-104976 | 2007-08-16 | Failure to keep dike or pit free of brine or other wastes |
For data sources see[9]