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Well ID: 34-157-25290 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Washington Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: TROYER WILLIAM | |
License Status: Final Restoration | |
License Date: 2016-09-28 | |
Spud Date: 2006-11-09 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 2006-11-21 | |
Well Total Depth: 7634 ft | |
Configuration: Vertical | |
Latitude: 40.276083445 | |
Longitude: -81.46153502 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-09-18 | Proposed Formations:KNOX, Issued Date:9/18/2006, Expired Date:9/18/2007 6:00:00 AM, Drilling unit acres:58.5, Proposed Well Type:OG, Proposed Well Class:POOL |
Completed | 2006-11-21 | |
Reached Total Depth | 2006-11-21 | |
Completion Report Received | 2007-02-15 | |
Construction Permit Expires | 2007-09-18 | |
Plugged/Abandoned | 2016-08-02 | |
Record Last Modified | 2016-12-06 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2007-05-17 | 7090 | 7496 | 32 |
2007-05-17 | 7500 | 7508 | 23 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 19800 Gal | 0 | TREATED PERF INTERVALS IN BLACK RIVER AND BEEKMANTOWN |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2007 | ARTEX OIL COMPANY | 7780 | 39 | 365 |
2008 | ARTEX OIL COMPANY | 3792 | 0 | 365 |
2009 | ARTEX OIL COMPANY | 3232 | 0 | 365 |
2010 | ARTEX OIL COMPANY | 858 | 0 | 365 |
2011 | ARTEX OIL COMPANY | 403 | 11 | 365 |
2012 | ARTEX OIL COMPANY | 157 | 0 | 366 |
2013 | ARTEX OIL COMPANY | 47 | 0 | 365 |
2014 | ARTEX OIL COMPANY | 74 | 0 | 365 |
2015 | ARTEX OIL COMPANY | 43 | 0 | 365 |
2016 | ARTEX OIL COMPANY | 52 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | ARTEX OIL COMPANY | Brine | 4902 | 365 |
2007 | ARTEX OIL COMPANY | Brine | 7702 | 365 |
2008 | ARTEX OIL COMPANY | Brine | 260 | 365 |
2009 | ARTEX OIL COMPANY | Brine | 113 | 365 |
2010 | ARTEX OIL COMPANY | Brine | 689 | 365 |
2011 | ARTEX OIL COMPANY | Brine | 371 | 365 |
2012 | ARTEX OIL COMPANY | Brine | 0 | 366 |
2013 | ARTEX OIL COMPANY | Brine | 43 | 365 |
2014 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2015 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2016 | ARTEX OIL COMPANY | Brine | 185 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0022096435 | 2016-07-26 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig crew preparing to plug the well. The rig is all rigged up and they are blowing the tubing and the back side down and will load the hole with brine water. They will attempt to unseat the packer, and pull the tubing. The tubing will then be run back into the wellbore and the bottom plug will be set through the 2 3/8 inch tubing. |
0998785980 | 2016-09-28 | Final Restoration | No Violations | On the day of my inspection, I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B). |
1469720361 | 2016-07-28 | Plug / Plug Back | No Violations | |
1469802399 | 2016-07-29 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig crew ready to set the bottom plug at 7451 feet with 40 sacks of class A cement. The well did circulate in the process of setting the plug. The 2 3/8 inch tubing was pulled to a depth of 5000 feet, and a 200 foot plug was set with class A cement. The well did circulate. The rest of the tubing is being pulled out of the wellbore and the will be shut in for the weekend. |
1470071463 | 2016-08-01 | Plug / Plug Back | No Violations | |
1470158179 | 2016-08-02 | Plug / Plug Back | No Violations | Upon arrival on location I found the rig ready to set the rip plug at a depth of 3961 feet. A 100 foot plug with class A cement will be set. We pulled the 2 3/8 inch tubing up to the depth of 3479 feet andset a 200 foot top of the lime plug with class A cement. The tubing was pulled to a depth of 1272 feet and set a 200 foot plug, 100 feet outside the bottom of the 8 5/8 inch casing and 100 feet inside the casing. The 2 3/8 inch tubing was then pulled to a depth of 200 feet and it was cemented to the ground level. |
1767402410 | 2013-11-19 | Preliminary Restoration | No Violations |
For data sources see[9]