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Well ID: 34-157-25452 | Loading map...
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Country: United States | |
State: Ohio | |
County: Tuscarawas | |
Municipality: Oxford Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: BAKER-ROAHRIG UNIT | |
License Status: Final Restoration | |
License Date: 2016-05-05 | |
Spud Date: 2010-08-27 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 2010-09-13 | |
Well Total Depth: 7440 ft | |
Configuration: Vertical | |
Latitude: 40.248466607 | |
Longitude: -81.58044696 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2009-12-30 | Proposed Formations:OHIO SHALE THRU KNOX, Issued Date:12/30/2009, Expired Date:12/30/2010 6:00:00 AM, Drilling unit acres:98, Proposed Well Type:OG, Proposed Well Class:POOL |
Correction to Well | 2010-02-05 | DECREASE UNIT SIZE TO 94.13 ACRES. |
Reached Total Depth | 2010-09-13 | |
Completion Report Received | 2010-11-26 | |
APP | 2015-05-15 | Proposed Formations:BEEKMANTOWN, Issued Date:5/15/2015, Expired Date:5/14/2017 12:00:00 PM, Drilling unit acres:94.13, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-09-16 | |
Construction Permit Expires | 2017-05-14 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-01-25 | 7260 | 7320 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2010-09-21 | ACID | 15 | 14300 Gal | 0 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | ARTEX OIL COMPANY | 19126 | 58 | 365 |
2012 | ARTEX OIL COMPANY | 5322 | 94 | 366 |
2013 | ARTEX OIL COMPANY | 3767 | 0 | 365 |
2014 | ARTEX OIL COMPANY | 2185 | 0 | 365 |
2015 | ARTEX OIL COMPANY | 1873 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | ARTEX OIL COMPANY | Brine | 2166 | 365 |
2012 | ARTEX OIL COMPANY | Brine | 1602 | 366 |
2013 | ARTEX OIL COMPANY | Brine | 523 | 365 |
2014 | ARTEX OIL COMPANY | Brine | 1567 | 365 |
2015 | ARTEX OIL COMPANY | Brine | 1312 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0809666166 | 2013-08-07 | Preliminary Restoration | No Violations | Everything passed according to 1509.072A. |
1442335465 | 2015-09-15 | Plug / Plug Back | No Violations | Bishop Well Service ran 2-3/8 inch diameter tubing in to 7320 ft. and set the bottom plug from 7320 to 6970 ft. on 9/14/2015- Formation Cement Service set the bottom plug with 30 sacks of class A at 15.6 lb. and a yield of 1.18 then the well was shut in. Bishop Wall tagged the top of the plug at 6900 ft. but could not rip the 4-1/2 inch diameter casing. They called and I advised that the 4-1/2 inch diameter casing be perforated and a plug squeezed to cover the Clinton formation. I arrived today and Timco Wireline shot the casing at 4916 ft. Bishop Well ran 2-3/8 inch diameter tubing to 4936 ft. and Formation Cementing established circulation and set a 200 ft. plug with 54 sacks of class A cement at 15.6 lb. and a yield of 1.18 - Bishop Well pulled 35 joints of tubing out and Formation reverse circulated any cement out of the tubing, then the well was packed off. Formation squeezed 7 bbl. Of cement into the perfs at 4916 ft. The tubing was pulled and the well shut in for the night. |
1442417889 | 2015-09-16 | Plug / Plug Back | No Violations | Bishop Well Service ran in this morning and tagged the top of the cement plug which was set at 4916 ft.on 9/15/2015 and found the cement top at 4700 ft. The plug after being set was squeezed back into the perfs and 7 barrels of good cement made it to the annular side of the perforated 4-1/2 inch diameter casing. That would be approximately 30 sacks of cement in the annulus. After tagging the plug Bishops Well Service was able to rip the 4-1/2 casing at 4350 ft. and pulled the casing up to 3513 ft. and set a 300 ft. combined plug to 3213 ft. cemented with 75 sacks of class A cement at 14.7 and a yield of 1.36 Next pull casing up to 1516 ft. and set a 200 ft. to 1316 ft. Last plug set at 200 ft. to 0 ft. and circulated cement to surface. All the plugs set today were set using the 4-1/2 inch casing. |
1462452668 | 2016-05-05 | Final Restoration | No Violations | On the day of my inspection I found that the final restoration has been completed. The site passed final restoration according to ORC 1509.072 (B) |
For data sources see[9]