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34-085-21094

Well Details

Well ID: 34-085-21094
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Country: United States
State: Ohio
County: Lake
Municipality: Leroy Township
Operator Name: ROCKEFELLER OIL COMPANY LLC
Well Pad ID:
Farm/Lease Name: VROOMAN(SWIW #6)
License Status: Active Injection
License Date: 2006-05-25
Spud Date: 2004-01-03
Spud Drilling Contractor: CAPSTAR DRILLING
Final Drill Date: 2004-01-24
Well Total Depth: 6355 ft
Configuration: Vertical
Latitude: 41.709986811
Longitude: -81.17770413

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2003-12-04 Proposed Formations:TRENTON-BLACK RIVER, Issued Date:12/4/2003, Expired Date:12/3/2004 6:00:00 AM, Drilling unit acres:49.59, Proposed Well Type:OG, Proposed Well Class:EDPW
Original Spud 2004-01-03 RBDMS Rec
Completed 2004-01-24 RBDMS Rec
Reached Total Depth 2004-01-24 RBDMS Rec
Completion Report Received 2004-09-02 RBDMS Rec
APP 2006-05-25 Proposed Formations:MT. SIMON SANDSTONE, Issued Date:5/25/2006, Expired Date:5/25/2007 6:00:00 AM, Drilling unit acres:49.59, Proposed Well Type:SWD, Proposed Well Class:SWIW
Construction Permit Expires 2007-05-25 RBDMS Rec
Annulus Pressure Monitoring Approved 2008-05-06 RBDMS Rec
Last Compliance Report 2008-05-06 RBDMS Rec
Change of Owner 2016-12-05 Operator changed from 7447, GREAT PLAINS EXPLORATION LLC to 9828, ROCKEFELLER OIL COMPANY LLC
Record Last Modified 2016-12-05 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1899-12-30 3156 3166 13
2008-05-06 5595 6318 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
FOAM 15 17670 Gal 90000 515M SCF NITROGEN & 500 GALLONS ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 GREAT PLAINS EXPLORATION LLC 7533 80 365
2008 GREAT PLAINS EXPLORATION LLC 29 0 31

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 GREAT PLAINS EXPLORATION LLC Brine 560 365
2008 GREAT PLAINS EXPLORATION LLC Brine 0 31

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0030804960 2013-12-30 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0071786909 2016-03-30 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The gate was closed and no one was onsite. There were no violations found at the time.
0090924292 2017-02-28 Salt Water Injection Well No Violations Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarters of 2016. Please submit the appropriate reports by March 14, 2017. Reports/Fees Received 3/10/2017
0099114980 2008-01-18 Surface Facility Construction No Violations Tubing fished out and ran back in to drill cement
0133367454 2009-09-02 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0154768653 2017-09-22 Salt Water Injection Well No Violations I inspected this well location as part of routine inspection activity. No injection activities were occurring at the time of my visit. The wellhead connections were secure with 100 nominal PSI showing at the casing and tubing. I walked the areas surrounding the tank battery and wellhead and found no signs of problems or issues warranting further investigation.
0248261256 2018-06-25 Salt Water Injection Well No Violations I found the injection well not in operation. An identification sign is posted. I observed no leaks or spills. There are no violations at this time.
0346716483 2015-12-30 Salt Water Injection Well No Violations My inspection found the well in good repair. The well was not being operated at the time of inspection. The tubing had 0 PSI on it and the 4.5 casing was at 35 PSI. The tank battery was in good repair and consisted of nine 400 BBL brine tanks. The tank battery is surrounded by the proper containment. The loading pad was clean. Tank battery floor was free of water and debris. Lease road was stable condition. No violations found.
0363931599 2008-06-10 Surface Facility Construction No Violations Off-loading pad sealed
0372388098 2008-07-29 Salt Water Injection Well No Violations in compliance
0412562975 2011-08-25 Salt Water Injection Well No Violations There were no violations found at the time of my inspection.
0414054455 2014-03-06 Salt Water Injection Well No Violations My inspection found the well in good repair. The well was not being operated at the time of inspection. The tubing had 300 PSI on it and the 4.5 casing was at 10 PSI. The tank battery was in good repair and consisted of nine 400 BBL brine tanks. The tank battery is surrounded by the proper containment. The loading pad was clean. Tank battery floor was free of water and debris. Lease road was stable condition. No violations found.
0445250087 2016-03-16 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on February 15th for 2015, despite a letter that was sent March 1, 2016 with a deadline of March 15, 2016 to submit the reports requested. REPORTS RECEIVED
0480344269 2012-02-09 Salt Water Injection Well No Violations The operator was actively injecting at the time of inspection and was cleaning loading pad into sump. The injection pressure was 900 PSI and the injection rate was 48 barrels/hour. This well automatically shuts down if the pressure exceeds 900 PSI.
0495713717 2016-08-23 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The well was not in use. There were no violations found at the time.
0550794220 2016-12-20 UrbanProduction Wells No Violations I inspected this well as part of routine inspection activity. The well has been utilized for brine injection disposal and is located at Great Plains Explorations facility at Vrooman Rd. at I-90. At the time of this inspection, the well was idle and not in use for injection. I observed no casing pressure at the injection fitting connection and no pressure at the 8.625-inch surface casing. The associated storage tank battery is comprised of six 210-barrel steel tanks in a field-constructed, containment structure with 48-inch concrete containment walls. The interior of the containment was free from signs of tank leakage or impacts from oil or brine. The tanks were secure and showed no evidence of problems. I walked the area around the exterior and did not note and signs of impact or erosional deficits.
0563420050 2008-03-04 Salt Water Injection Well No Violations on site checking progress packer leaking .
0568025360 2007-10-23 Salt Water Injection Well No Violations Well still hooked up for prodution in clinton

tank pad set .Tank Pad for UIC storage has been built.

0575888653 2013-01-17 Salt Water Injection Well No Violations My inspection of the well and injection facility found no violations.
0597605295 2008-10-07 Salt Water Injection Well No Violations PSI 500
0609732284 2010-06-29 Salt Water Injection Well No Violations No violations were found at the time of inspection.
0697410591 2012-04-24 Salt Water Injection Well No Violations My inspection today found the salt water injection well operating. The injection pressure was 780 PSI. The annulus pressure was 50 PSI. The well tender was on location at the time of my inspection. The site was in good repair. The lease road was stable. Loading pad was clean and the sump was free of water and debris. The tank battery was free of fluid. The well identification sign was posted. The operator asked about spreading brine on the drive and parking area to prevent dust. I advised the operator to review the law and the procedure for obtaining approval to spread brine. Spreading of brine at this time is prohibited.
0744226997 2018-05-03 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the 2017 Salt Water Injection Well Annual Report (Form 204) that was due to the Division by April 15, 2018. Please submit the requested report by June 4, 2018.
0784025421 2012-07-11 Salt Water Injection Well No Violations My inspection of the well site and injection facility was accompanied by another inspector, Tom Hill.

There were no violations at the time of inspection.

0787361671 2015-09-24 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
0791257029 2008-03-07 Salt Water Injection Well No Violations On site for MIT . Tubing and packer was set at 6117.4 . Tested annulus from 1500-1600+ PSI several times with a loss of 100+ PSI within a few minutes . MIT failed .
0819323449 2009-09-02 Preliminary Restoration No Violations Preliminary restoration meets requirements.
0849452606 2012-07-11 Salt Water Injection Well No Violations My inspection today found the following: the wellhead and tank battery were in good repair. The injection well was operating within its allowable limits. Well tender was on location.
0991972801 2018-07-26 Salt Water Injection Well No Violations I found the well not in operation on the day of my inspection. I observed no spills or leaks. There is an identification sign posted at the tank battery; however, Great Plains is listed at the well owner. I spoke with Rockefeller Oil Company and instructed them update the well owner name on the sign. A follow-up inspection will be completed by August 3, 2018.
1060942611 2018-02-14 Storage Well No Violations I was on location to inspect the UIC well and facility. I found the well not in operation on the day of my inspection. I observed no leaks or spills. There was a Great Plains brine truck on location with the proper UIC number displayed (#25-336). There are no violations at this time.
1070456449 2012-09-21 Salt Water Injection Well No Violations My inspection of the well and injection facility found no violations.
1074091095 2004-01-12 Drill / Deepen / Reopen No Violations On site to check drilling of 143/4 hole for 113/4 shorten from 200 to 150 because of possible shale gas around 200 conductor cemented went fine.

01-13-03 Drilling 11 hole for 85/8caseing Hit big pocket of gas at 187 and flare keep buring during t

1074874621 2004-01-23 Drill / Deepen / Reopen No Violations Drilling 5995 slow on fluid.
1144081712 2018-10-10 Salt Water Injection Well No Violations I found the injection well not in operation at the time of my inspection. The well is in good repair. I observed no leaks or spills. An identification sign is posted. There was a brine truck on location with Great Plains Exploration LLC sticker on the passenger door and with a UIC number of 25-336 displayed on the tank. I called the phone number on the sticker from the brine truck, which was disconnected. According to ODNR UIC active brine haulers list dated 10-2-2018, UIC 25-336 is not an active number. Rockefeller Oil Co. does have an active UIC number (#25-674). I spoke with John Magnusus from Rockefeller Oil Co. concerning the brine truck. Mr. Magnusus stated Rockefeller owns the brine truck and has not updated the sticker or UIC number.

I told Mr. Magnusus: To immediately update the UIC number and company name displayed on the brine truck. Not to haul brine in the truck under the expired UIC number.

Follow-up inspections will be conducted. Photos of the truck have been taken and are available upon request.

1147969086 2006-05-18 Production Wells No Violations per site for UIC,No homes within 1/4 mile, on then edge of wooded area, no streams visible
1191840163 2012-06-26 Salt Water Injection Well No Violations My inspection today found the well operating and no one on location. Murphy switches are in place to control well pressure. A UIC brine truck (registered UIC-336) was under repair on the lease road. There were two brine stains on the lease road, before the off loading pad. These spills had been stabilized with peat-sorb. Lease road is stable and in good repair. Well is in good repair.
1197299752 2007-05-22 Surface Facility Construction No Violations Dug And Poured Footer for tank pad which is north of well
1205157159 2008-01-25 Surface Facility Construction No Violations Mixed and pumped the knox plug shut in (SHOULD BE FOR CLINTON PERF PLUG per test)
1205445664 2008-03-13 Salt Water Injection Well No Violations 8:45am Arrived on site, operator was attaching packer to the tubing. Operator began running tubing. As the operator was running tubing they were also tallying the tubing. Talley had been lost before the job. 6116.97+6 of tubing ran with packer on the end. 4.5 inch casing was loaded with fluid before they ran tubing. Tubing was loaded with fluid while it was ran. Operator set packer and attempted pressure tested. Pressure test failed, on all attempts up till 6:10pm. Operator attempted to bleed any air out of 4.5 inch pipe. Operator decide to unset packer and circulate hole. Then they are going to run the rust inhibiter. Rust inhibitor 5.25 gal to 70 BBL of fluid.
1205930525 2008-02-01 Surface Facility Construction No Violations on site for pressure test of casing all perferation cemented off and this test is check casing only
1210775964 2008-01-10 Salt Water Injection Well No Violations on site company drilling rig unable to pull tubing tried pulling several times. Ran Bond Log found tubing cemented at 1374 crew shut down to round up tools needed.
1210780131 2008-03-18 Surface Facility Construction No Violations Presure Failed on 03-13-08 packer set at 6122.97+6

Packer released and reset at (18jts) 5551.7top of packer (type A-3LOK-set retrievable Casing Packer repessrued up to 1600 PSI held for 15min with no loss.

1210855266 2008-02-22 Salt Water Injection Well No Violations On site for MIT . Tubing and packer was set at 6119.4 . Tested annulus from 1500-1600+ PSI several times with a loss of 100+ PSI within a few minutes . MIT failed .
1210946663 2008-01-17 Salt Water Injection Well No Violations drilled through cement and pulled tubing rigged up to fish rest of tubing out
1233069069 2009-01-06 Salt Water Injection Well No Violations NO Violation
1297174182 2010-10-21 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1299270046 2004-02-04 Drill / Deepen / Reopen No Violations Rig moved off closeing pits.
1301677395 2011-03-30 Salt Water Injection Well No Violations There were no violations at the time inspection.
1320784977 2011-11-08 Salt Water Injection Well No Violations Injection pressure 720 PSI and the annulus pressure is 0 PSI. Well location and battery are in good repair. Loading pad was clean. Tank battery floor was free of water and debris. Lease road was stable and constructed out of durable material. Well was in operation.
1325274708 2007-08-08 Surface Facility Construction No Violations Setting tanks in side poured walled dikes
1368755286 2008-01-25 Salt Water Injection Well No Violations Pulled tubing and bit and ran tubing to knox ROSE RUN talley 5647 Perfs at 5595- 5601

rigged up to cement formation in mixed and pumped 50 sks Class A.

1373555751 2013-04-17 Salt Water Injection Well No Violations There were no violations at the time of my inspection.
1378739866 2013-09-06 Salt Water Injection Well No Violations There was a slight amount of pressure on the annulus. My inspection of the well and injection facility found no violations.
1383200211 2010-04-07 Salt Water Injection Well No Violations Pressure within compliance
1401093605 2015-03-30 Salt Water Injection Well No Violations My inspection found the well in good repair. The well was not being operated at the time of inspection. The tubing had 0 PSI on it and the 4.5 casing was at 10 PSI. The tank battery was in good repair and consisted of nine 400 BBL brine tanks. The tank battery is surrounded by the proper containment. The loading pad was clean. Tank battery floor was free of water and debris. Lease road was stable condition. No violations found.
1425888096 2008-03-04 Surface Facility Construction No Violations
1426043667 2008-01-22 Salt Water Injection Well No Violations drilling cement 18 jts in
1428002728 2014-12-26 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1432588535 2007-06-07 Surface Facility Construction No Violations working on retaining wall forms will be poured on Friday
1446856586 2011-06-28 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1460831218 2016-12-30 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations at the time.
1461676257 2016-04-25 Salt Water Injection Well No Violations My inspection found the well in good repair. The well was not being operated at the time of inspection. The tubing was on vacuum with 0 PSI on it and the 4.5 casing was at 35 PSI. The tank battery was in good repair and consisted of nine 400 BBL brine tanks. The tank battery is surrounded by the proper containment. The loading pad was clean. Tank battery floor was free of water and debris. Lease road was stable condition. No violations found.
1498743169 2017-06-27 Salt Water Injection Well No Violations The injection well and surface facility were inspected. No violations were observed at the time.
1506537543 2017-09-27 Salt Water Injection Well No Violations Well was operating at the time of inspection. There was approximately 5 gallons of free oil in the tank battery by the sump. Spoke to well tender on location Ron and requested that the dike be kept clean. Identification sign needs updated to the new owner.
1540182296 2008-02-19 Salt Water Injection Well No Violations Ran tubing to 6119.40 Packer (R-4) 6116.90 tubing +2.50 packer=6119.40
1572966967 2016-03-02 Salt Water Injection Well No Violations Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 2nd, 3rd & 4th quarter of 2015 despite a letter that was sent with a deadline of February 29, 2016. Please submit the appropriate reports by March 16th, 2016. reports received 3/10/2017
1620856641 2010-08-13 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1621642440 2008-01-08 Salt Water Injection Well No Violations on site to witness clinton perf plug set at 3126-1901 100 sks of class A cement. Land plug in perfs

and perssured up to 2000# shut in

1663722343 2017-03-31 Salt Water Injection Well No Violations The injection well and surface facility were inspected. The well owner was instructed to pressure up the annulus. There were no violations found at the time.
1784613260 2011-12-27 Salt Water Injection Well No Violations The well location and tank battery are in good repair. The lease road was stable. Oil streaks were noted on the standing water on location. I reminded the operator to make sure that the brine haulers pull their trucks completely onto the unloading pad to prevent any potential leakage from their trucks from landing off of the pad.
1822923270 2014-05-16 Salt Water Injection Well No Violations An inspection of the well and injection facility found no violations.
1838346901 2014-09-23 Salt Water Injection Well No Violations An inspection of the well and injection facility found no violations.
1916645421 2016-06-09 Salt Water Injection Well No Violations My inspection found the well in good repair. The well was not being operated at the time of inspection. The tubing had 0 PSI on it and the 4.5 casing was at 35 PSI. The tank battery was in good repair and consisted of nine 400 BBL brine tanks. The tank battery is surrounded by the proper containment. The loading pad was clean. Tank battery floor was free of water and debris. Lease road was stable condition. No violations found.
1953529046 2017-11-06 Salt Water Injection Well No Violations
2071293784 2009-08-03 Salt Water Injection Well No Violations no violation at time of inspection.
2084788180 2018-02-16 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st quarter of 2017 . Please submit the appropriate reports by March 17, 2018.
2089889575 2008-01-09 Salt Water Injection Well No Violations On site company was ran tubing in tagged plug at 3168 (3156=100jts) . Cement company on site mixed another 100 sks of class A cement Shut in.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0445250087 US-OH-124807 2016-04-04 Failure to file salt water injection annual report
0744226997 US-OH-128469 2018-08-03 Failure to file salt water injection annual report
2084788180 US-OH-121279 2018-02-23 Failure to report disposal fees

For data sources see[9]

References