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Well ID: 34-121-20084 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Beaver Township | |
Operator Name: MFC DRILLING INC | |
Well Pad ID: | |
Farm/Lease Name: HOUSE WILLIAM (BETTS) | |
License Status: Final Restoration | |
License Date: 2014-02-03 | |
Spud Date: 1938-10-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1938-11-25 | |
Well Total Depth: 1586 ft | |
Configuration: Vertical | |
Latitude: 39.926749437 | |
Longitude: -81.27209009 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1938-10-20 | FDT=GRIT SAND; PF=GRIT SAND |
Completed | 1938-11-25 | FDT=GRIT SAND; PF=GRIT SAND |
Reached Total Depth | 1938-11-25 | FDT=GRIT SAND; PF=GRIT SAND |
Change of Owner | 2013-11-25 | Operator changed from 98, NGO DEVELOPMENT CORP. to 3059, MFC DRILLING INC |
APP | 2014-02-03 | Proposed Formations:, Issued Date:2/3/2014, Expired Date:2/3/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-03-26 | FDT=GRIT SAND; PF=GRIT SAND |
Construction Permit Expires | 2016-02-03 | FDT=GRIT SAND; PF=GRIT SAND |
Record Last Modified | 2019-06-14 | FDT=GRIT SAND; PF=GRIT SAND |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | NATIONAL PRODUCTION CORP | 627 | 0 | 0 |
1985 | NATIONAL PRODUCTION CORP | 591 | 0 | 365 |
1986 | NATIONAL PRODUCTION CORP | 0 | 0 | 0 |
1987 | NATIONAL PRODUCTION CORP | 0 | 0 | 366 |
1989 | NATIONAL PRODUCTION CORP | 0 | 0 | 0 |
1990 | NATIONAL PRODUCTION CORP | 0 | 0 | 0 |
1991 | NATIONAL PRODUCTION CORP | 0 | 0 | 365 |
2012 | NGO DEVELOPMENT CORP. | 0 | 0 | 366 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | NATIONAL PRODUCTION CORP | Brine | 0 | 0 |
1985 | NATIONAL PRODUCTION CORP | Brine | 0 | 365 |
1986 | NATIONAL PRODUCTION CORP | Brine | 0 | 0 |
1987 | NATIONAL PRODUCTION CORP | Brine | 0 | 366 |
1989 | NATIONAL PRODUCTION CORP | Brine | 0 | 0 |
1990 | NATIONAL PRODUCTION CORP | Brine | 0 | 0 |
1991 | NATIONAL PRODUCTION CORP | Brine | 0 | 365 |
2012 | NGO DEVELOPMENT CORP. | Brine | 0 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0970598163 | 2006-02-17 | Production Wells | No Violations | Betts#3lease name well is owned by NGO Develoment well is hooked up and 1 gas line going towards batesville not able to determine if well is being used for domestic or commerical use valves at wellhead are open slightly. |
0985986058 | 2014-06-05 | Final Restoration | No Violations | I am accompanied by supervisor Brent Bear. My inspection today finds the site meets the preliminary restoration requirements. Vegetation has been established and the pits have been filled. |
1143247326 | 2006-03-21 | Production Wells | No Violations | Site GPS readings taken NGO Development CORP is well owner. |
1498994096 | 2014-03-18 | Production Wells | No Violations | I received a call from MFC Drilling stating that they were preparing to move in and plug the well. They wanted to provide 24 hour notice. |
2093458184 | 2014-03-26 | Plug / Plug Back | No Violations | Appalachian shot ten holes from 1115 to 1100 after a bond log revealed a void behind the 2 pipe. The service rig ran 1500 of 1 pipe. Omega pumped enough cement to fill the 2 tubing then hooked up to the tubing and pumped an additional 9 bbl of cement under slight pressure to fill the backside void. |
For data sources see[7]