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34-067-20952

Well Details

Well ID: 34-067-20952
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Country: United States
State: Ohio
County: Harrison
Municipality: Cadiz Township
Operator Name: COAL GAS TRANSPORTATION LLC
Well Pad ID:
Farm/Lease Name: HARRISON CO COMMISSIONERS
License Status: Final Restoration
License Date: 2014-07-22
Spud Date: 2000-03-02
Spud Drilling Contractor: CENTURY WELL SERVICES,INC
Final Drill Date: 2000-03-03
Well Total Depth: 623 ft
Configuration: Vertical
Latitude: 40.251622764
Longitude: -81.01554950

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 1999-08-26 Proposed Formations:LOWER FREEPORT, Issued Date:8/26/99, Expired Date:8/25/00 6:00:00 AM, Drilling unit acres:1, Proposed Well Type:CM, Proposed Well Class:ESPW
Original Spud 2000-03-02 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT
Completed 2000-03-03 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT
Reached Total Depth 2000-03-03 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT
Completion Report Received 2000-09-18 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT
Change of Owner 2008-12-29 Operator changed from 5319, LAHD ENERGY INC to 8454, COAL GAS TRANSPORTATION LLC
APP 2014-07-22 Proposed Formations:LOWER FREEPORT 6A COAL SEAM, Issued Date:7/22/2014, Expired Date:7/21/2016 12:00:00 PM, Drilling unit acres:1, Proposed Well Type:CM, Proposed Well Class:
Plugged/Abandoned 2016-04-08 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT
Construction Permit Expires 2016-07-21 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT
Record Last Modified 2019-06-05 RBDMS Rec GMM STAUS WAS CHANGED TO PA PER PLUG REPORT

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2000 LAHD ENERGY INC 1386 0 175
2001 LAHD ENERGY INC 2697 0 183
2002 LAHD ENERGY INC 1825 0 365
2003 LAHD ENERGY INC 1200 0 365
2004 LAHD ENERGY INC 1825 0 365
2005 LAHD ENERGY INC 189 0 365
2007 LAHD ENERGY INC 1825 0 365
2008 LAHD ENERGY INC 6966 0 334
2009 COAL GAS TRANSPORTATION LLC 0 0 0
2010 COAL GAS TRANSPORTATION LLC 0 0 0
2011 COAL GAS TRANSPORTATION LLC 266 0 334
2012 COAL GAS TRANSPORTATION LLC 112 0 59
2013 COAL GAS TRANSPORTATION LLC 0 0 0
2014 COAL GAS TRANSPORTATION LLC 0 0 0
2015 COAL GAS TRANSPORTATION LLC 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2000 LAHD ENERGY INC Brine 0 175
2001 LAHD ENERGY INC Brine 0 183
2002 LAHD ENERGY INC Brine 0 365
2003 LAHD ENERGY INC Brine 0 365
2004 LAHD ENERGY INC Brine 0 365
2005 LAHD ENERGY INC Brine 0 365
2007 LAHD ENERGY INC Brine 0 365
2008 LAHD ENERGY INC Brine 0 334
2009 COAL GAS TRANSPORTATION LLC Brine 0 0
2010 COAL GAS TRANSPORTATION LLC Brine 0 0
2011 COAL GAS TRANSPORTATION LLC Brine 0 334
2012 COAL GAS TRANSPORTATION LLC Brine 0 59
2013 COAL GAS TRANSPORTATION LLC Brine 0 0
2014 COAL GAS TRANSPORTATION LLC Brine 0 0
2015 COAL GAS TRANSPORTATION LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0040614994 2016-03-09 Production Wells No Violations I am on site accompanied by inspector Mark Moreland to review the plans on what will need to be done to plug the well bore. The owner informed us that he plans to plug the well within the next week.
0135426534 2016-03-10 Plug / Plug Back No Violations Appalachian Well Service is on site to run a CCL log inside the 4.5 inch diameter casing to indicate if there is a packer set on the backside of the casing, in order to discover what will need to be done to plug this well bore. After Appalachian ran the CCL log there was no indication that a packer was set on the 4 inch diameter casing. After the log I placed a call to Mark Moreland who informed me that a service rig will have to pull the casing in order to plug the well or a bon-log will need to be run to indicate if there is cement on the backside of the casing. I was accompanied by inspector Pat Shreve on the day of my inspection.
0406916912 2016-04-07 Plug / Plug Back No Violations I am on site where I witnessed Davis Well Service used a service rig to unset the packer and pull out 615 feet of 4.5 inch diameter surface casing. Appalachian Well Service is on site to set a wire line bridge plug inside the 7 inch diameter surface casing in preparation for plugging this well. Appalachian hit an obstruction in the hole at 315 feet. The last collar for the 7 inch diameter pipe was found at 300 feet. The bridge plug was then set at 285 feet. The well will be filled with cement on a later date.
0498863317 2016-03-10 Plug / Plug Back No Violations Ran in to check depth. Appalachian tried to run bond log and Collar Locate. The well would not hold fluid. I accompanied Joe Zellers. Mark Clark was the company man.
0589961536 2016-04-19 Plug / Plug Back No Violations On the day of my inspection I witnessed the well location has been restored, but vegetation has yet to be established. I will return at a later date to indicate if the site can pass final restoration.
0916885342 2016-04-08 Plug / Plug Back No Violations The well would not load indicating a leak either in the casing or the bridge plug. Decided to run tubing and displace hole volume of cement and see where the leak was. Cemenco pumped the cement with no returns and when we pulled the tubing there was cement on the tubing starting at 80 down. Pulled the tubing and shut down for the weekend. Will tag the cement top on Monday morning.
1100779340 2016-07-13 Final Restoration No Violations On the day of my inspection, I found that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B).
1737467987 2016-04-12 Plug / Plug Back No Violations
1956277427 2016-05-26 Plug / Plug Back No Violations On the day of my inspection I witnessed the well location has been graded and the lease road was in adequate condition. However, the site could not pass final restoration due to lack of vegetation.
iDIAN00456 2000-06-21 Preliminary Restoration No Violations

For data sources see[8]

References