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Well ID: 34-153-23028 | Loading map...
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Country: United States | |
State: Ohio | |
County: Summit | |
Municipality: Twinsburg | |
Operator Name: SUMMIT PETROLEUM INC | |
Well Pad ID: | |
Farm/Lease Name: VILLAGE OF REMINDERVILLE | |
License Status: Producing | |
License Date: 2008-01-02 | |
Spud Date: 2008-01-17 | |
Spud Drilling Contractor: POULSON DRILLING | |
Final Drill Date: 2008-01-21 | |
Well Total Depth: 3902 ft | |
Configuration: Vertical | |
Latitude: 41.342027969 | |
Longitude: -81.40217460 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-11-26 | Proposed Formations:CLINTON, Issued Date:11/26/2007, Expired Date:11/25/2008 6:00:00 AM, Drilling unit acres:35.8, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2008-01-02 | Proposed Formations:CLINTON, Issued Date:1/2/2008, Expired Date:1/1/2009 6:00:00 AM, Drilling unit acres:35.8, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2008-01-21 | |
Completion Report Received | 2008-02-19 | |
Construction Permit Expires | 2009-01-01 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2008-05-23 | 3711 | 3773 | 20 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 78500 Gal | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | SUMMIT PETROLEUM INC | 10382 | 236 | 306 |
2009 | SUMMIT PETROLEUM INC | 5401 | 148 | 365 |
2010 | SUMMIT PETROLEUM INC | 2571 | 82 | 365 |
2011 | SUMMIT PETROLEUM INC | 3675 | 129 | 365 |
2012 | SUMMIT PETROLEUM INC | 2181 | 60 | 366 |
2013 | SUMMIT PETROLEUM INC | 1804 | 64 | 365 |
2014 | SUMMIT PETROLEUM INC | 1699 | 59 | 365 |
2015 | SUMMIT PETROLEUM INC | 1374 | 0 | 365 |
2016 | SUMMIT PETROLEUM INC | 1095 | 69 | 365 |
2017 | SUMMIT PETROLEUM INC | 1022 | 0 | 365 |
2018 | SUMMIT PETROLEUM INC | 810 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | SUMMIT PETROLEUM INC | Brine | 835 | 306 |
2009 | SUMMIT PETROLEUM INC | Brine | 139 | 365 |
2010 | SUMMIT PETROLEUM INC | Brine | 300 | 365 |
2011 | SUMMIT PETROLEUM INC | Brine | 230 | 365 |
2012 | SUMMIT PETROLEUM INC | Brine | 74 | 366 |
2013 | SUMMIT PETROLEUM INC | Brine | 138 | 365 |
2014 | SUMMIT PETROLEUM INC | Brine | 142 | 365 |
2015 | SUMMIT PETROLEUM INC | Brine | 83 | 365 |
2016 | SUMMIT PETROLEUM INC | Brine | 61 | 365 |
2017 | SUMMIT PETROLEUM INC | Brine | 0 | 365 |
2018 | SUMMIT PETROLEUM INC | Brine | 74 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0179890330 | 2008-04-02 | Production Wells | No Violations | The well has been turned on. Additional work still needs to be completed for preliminary restoration approval. |
0323314744 | 2008-01-04 | Drill / Deepen / Reopen | No Violations | The drilling location has been cleared and graded. A decision as to pit requirements will be made after the pits are dug. |
0325807941 | 2008-01-22 | Drill / Deepen / Reopen | No Violations | Poulson Drilling has moved off. The pits are fenced, lined and in good condition with sufficient freeboard to contain any precipitation. |
0415103270 | 2008-02-04 | Drill / Deepen / Reopen | No Violations | Recent heavy rains have washed the majority of the lime off of the nearby trees. Only the trees closest to the pits still have residual coverage. |
0729542406 | 2008-01-23 | Drill / Deepen / Reopen | No Violations | The surface hole annulus between the 8-5/8 surface casing and the ground has been topped of with 4 cubic yards of 9 sack grout. |
0829171259 | 2008-03-14 | Production Wells | No Violations | The well has been turned on before the fences were installed around the wellhead and the tank battery. I called Bill Kinney and told him to shut the well in immediately and to keep it shut in until the fences have been installed. |
0928614344 | 2008-02-01 | Drill / Deepen / Reopen | No Violations | On site to solidify pits with quick lime obtained from a plant in Huron Ohio. The material was very hot and easily became airborn during off loading and mixing. The material was blown into the shale pit only after the entire pit was covered with another pit liner. The lime was hot enough to melt portions of the cover liner. Plumes of steam and dust extented some 30 feet into the air while mixing the pit. The location is fairly remote and the only area affected by the plumes were nearby trees. This material is not suitable for use in developed areas unless an alternate method of applying and mixing is used. |
1318802646 | 2008-09-30 | Preliminary Restoration | No Violations | Preliminary restoration is approved. |
1928099990 | 2008-02-13 | Drill / Deepen / Reopen | No Violations | Moore Well Service rig is on site to correct a casing leak that has resulted in natural gas on the backside of the 4-1/2 casing. Summit has plumbed the 8-5/8 casing head to a frac tank in order to leave the valve open and prevent pressurization of the annulus. The company intends to run a Halliburton R-4 packer on tubing and to set the packer above the perforations in order to isolate the gas leak. The work is scheduled for 2/14. |
For data sources see[9]