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34-055-20018

Well Details

Well ID: 34-055-20018
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Country: United States
State: Ohio
County: Geauga
Municipality: Munson Township
Operator Name: BEST SAND CORPORATION
Well Pad ID:
Farm/Lease Name: FAIRMOUNT MINERALS
License Status: Final Restoration
License Date: 2008-07-24
Spud Date: 1962-07-09
Spud Drilling Contractor:
Final Drill Date: 1962-07-16
Well Total Depth: 3355 ft
Configuration: Vertical
Latitude: 41.547668819
Longitude: -81.20042085

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1962-07-09 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG
Completed 1962-07-16 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG
Reached Total Depth 1962-07-16 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG
Plugging Plan Approved 1998-02-03 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG
Change of Owner 2005-05-26 Operator changed from 4616, BEST SAND CORP to 7848, BEST SAND CORPORATION
APP 2008-07-24 Proposed Formations:NEWBURG, Issued Date:7/24/2008, Expired Date:7/24/2009 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2008-10-31 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG
Construction Permit Expires 2009-07-24 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG
Record Last Modified 2017-02-15 GPS PROVIDED BY BEST SAND ON 5/10/2005. JG

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 BEST SAND CORPORATION 0 0 22
2008 BEST SAND CORPORATION 0 0 8

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 BEST SAND CORPORATION Brine 1115 22
2008 BEST SAND CORPORATION Brine 452 8

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1225372693 2008-10-30 Plug / Plug Back No Violations On site for plug job. Operator ran tubing down hole, there is an obstruction at 1630. Operator ran an impression block down hole, impression block showed a 1.5cm wide by 7cm long crescent shaped impression. Doug Gonzales thought that it may be 7 inch pipe curled in. Options are to mill, see if Newburg will take fluid pump a plug down to isolate the Newburg, or perf at 1630 and squeeze bottom plug at that location. Fluid level was down 300 in the 7 inch pipe, filled
1242932432 2009-05-21 Final Restoration No Violations Site has been ruff graded. Site needs final grading completed, area seeded and mulched and vegetation established before Final Restoration can be passed.
1305260261 2009-07-07 Final Restoration No Violations Site has been graded and seeded. Vegetation is established.

For data sources see[7]

References