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Well ID: 34-059-23537 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Cambridge | |
Operator Name: GEORGETOWN OIL CO LLC | |
Well Pad ID: | |
Farm/Lease Name: TIPPLE T & W | |
License Status: Producing | |
License Date: 1995-10-31 | |
Spud Date: 1983-12-15 | |
Spud Drilling Contractor: J E B DRLG | |
Final Drill Date: 1983-12-22 | |
Well Total Depth: 5050 ft | |
Configuration: Vertical | |
Latitude: 40.081982544 | |
Longitude: -81.62126292 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-11-16 | Issued Date 11/16/83 Expired Date 5/14/84 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05050 Proposed Drill Depth 05050 |
Original Spud | 1983-12-06 | I.P. S/OIL |
Completed | 1983-12-22 | I.P. S/OIL |
Reached Total Depth | 1983-12-22 | I.P. S/OIL |
CO | 1984-01-02 | 28 CGAS EXPLORATION,INC GeoDate 11/16/83 |
Completion Report Received | 1984-01-17 | I.P. S/OIL |
CO | 1995-10-31 | 28 CGAS EXPLORATION,INC GeoDate 10/31/95 |
Unknown | 1995-10-31 | Issued Date 10/31/95 Expired Date 10/30/96 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date |
Construction Permit Expires | 1996-10-30 | I.P. S/OIL |
CO | 1996-11-13 | 264 CONSOLIDATED RES OF AMER GeoDate 10/31/95 |
Change of Owner | 2003-03-20 | Operator changed from 4884, EASTERN STATES OIL & GAS INC to 5352, ARTEX OIL COMPANY |
Change of Owner | 2017-05-17 | Operator changed from 5352, ARTEX OIL COMPANY to 9239, GEORGETOWN OIL CO LLC |
Record Last Modified | 2017-05-17 | I.P. S/OIL |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4920 | 4942 | 14 |
1997-06-29 | 4890 | 4990 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 164 Mscf | 0 | |||
H2O | 0 | 58000 Gal | 50000 | FRAC;H2O,SAND,N2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | YEI INC | 4195 | 184 | 0 |
1985 | YEI INC | 5199 | 267 | 365 |
1986 | YEI INC | 3849 | 99 | 365 |
1987 | YEI INC | 3046 | 82 | 365 |
1988 | YEI INC | 2380 | 0 | 365 |
1989 | CGAS EXPLORATION | 1406 | 85 | 365 |
1990 | CGAS EXPLORATION | 1396 | 0 | 365 |
1991 | CGAS EXPLORATION | 1088 | 0 | 365 |
1992 | CGAS EXPLORATION | 778 | 0 | 366 |
1993 | CGAS EXPLORATION | 496 | 0 | 366 |
1994 | CGAS EXPLORATION | 0 | 0 | 365 |
1995 | CGAS EXPLORATION | 0 | 0 | 365 |
1996 | CGAS EXPLORATION | 0 | 0 | 365 |
1997 | EASTERN STATES OIL & GAS INC | 0 | 0 | 365 |
1998 | EASTERN STATES OIL & GAS INC | 0 | 0 | 365 |
1999 | EASTERN STATES OIL & GAS INC | 0 | 0 | 0 |
2000 | EASTERN STATES OIL & GAS INC | 0 | 0 | 0 |
2001 | EASTERN STATES OIL & GAS INC | 0 | 0 | 365 |
2002 | EASTERN STATES OIL & GAS INC | 0 | 0 | 0 |
2003 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2004 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2005 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2006 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2007 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2008 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2009 | ARTEX OIL COMPANY | 0 | 0 | 365 |
2010 | ARTEX OIL COMPANY | 456 | 132 | 365 |
2011 | ARTEX OIL COMPANY | 2056 | 183 | 365 |
2012 | ARTEX OIL COMPANY | 2251 | 0 | 366 |
2013 | ARTEX OIL COMPANY | 2097 | 0 | 365 |
2014 | ARTEX OIL COMPANY | 2024 | 75 | 365 |
2015 | ARTEX OIL COMPANY | 1892 | 0 | 365 |
2016 | ARTEX OIL COMPANY | 1541 | 0 | 365 |
2017 | ARTEX OIL COMPANY | 856 | 0 | 365 |
2018 | GEORGETOWN OIL CO LLC | 677 | 22 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | YEI INC | Brine | 0 | 0 |
1985 | YEI INC | Brine | 150 | 365 |
1986 | YEI INC | Brine | 40 | 365 |
1987 | YEI INC | Brine | 85 | 365 |
1988 | YEI INC | Brine | 0 | 365 |
1989 | CGAS EXPLORATION | Brine | 35 | 365 |
1990 | CGAS EXPLORATION | Brine | 0 | 365 |
1991 | CGAS EXPLORATION | Brine | 0 | 365 |
1992 | CGAS EXPLORATION | Brine | 0 | 366 |
1993 | CGAS EXPLORATION | Brine | 0 | 366 |
1994 | CGAS EXPLORATION | Brine | 0 | 365 |
1995 | CGAS EXPLORATION | Brine | 0 | 365 |
1996 | CGAS EXPLORATION | Brine | 0 | 365 |
1997 | EASTERN STATES OIL & GAS INC | Brine | 365 | |
1998 | EASTERN STATES OIL & GAS INC | Brine | 365 | |
1999 | EASTERN STATES OIL & GAS INC | Brine | 0 | |
2000 | EASTERN STATES OIL & GAS INC | Brine | 0 | |
2001 | EASTERN STATES OIL & GAS INC | Brine | 0 | 365 |
2002 | EASTERN STATES OIL & GAS INC | Brine | 0 | 0 |
2003 | EASTERN STATES OIL & GAS INC | Brine | ||
2004 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2005 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2006 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2007 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2008 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2009 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2010 | ARTEX OIL COMPANY | Brine | 430 | 365 |
2011 | ARTEX OIL COMPANY | Brine | 75 | 365 |
2012 | ARTEX OIL COMPANY | Brine | 75 | 366 |
2013 | ARTEX OIL COMPANY | Brine | 50 | 365 |
2014 | ARTEX OIL COMPANY | Brine | 52 | 365 |
2015 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2016 | ARTEX OIL COMPANY | Brine | 93 | 365 |
2017 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2018 | GEORGETOWN OIL CO LLC | Brine | 20 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0082990077 | 2018-02-13 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a 210 barrel tank, a disconnected concrete vault, a horizontal separator, a drip, a 2 inch meter run with a .25 orifice and a chart recorder all within an earthen dike. The well was equipped with 8.625 diameter casing, 4.5 inch diameter, 2.875 inch diameter tubing, 1.5 inch diameter tubing, rods, a pumping unit powered by natural gas and domestic gas service with valves in the open position on the 2.875 inch diameter tubing and 1.5 inch diameter tubing. Identification was present and production records were current. |
0410228997 | 2004-12-17 | Production Wells | No Violations | STATUS CHECK, TANK REMOVED. |
0448756617 | 2005-02-04 | Production Wells | No Violations | STATUS CHECK. WELL SHUT IN. |
0708837231 | 2010-01-19 | Production Wells | Violations Noted | Complaint received from landowner Vonda Tipple of idle well on property,inspected site and found well shut in no production reported on well since 1993,well is equipped with 8 surface casing and 4.5 production casing and 1.5 tubing and 1-210 bbl tank and meter run located in dike area,no charts in meter box and all valves at wellhead were shut on the day of my inspection. |
0893806335 | 2005-07-14 | Production Wells | No Violations | STATUS CHECK. |
1264634301 | 2010-01-26 | Production Wells | No Violations | Inspection revealed that owner has moved service rig on site to repair well, operator pulled 1.5 tubing and began to swab 4.5 production in process they went to production tank and discovered that flow line had lost integrity and leaked approximately 4 bbl oil in low lying area and clean up efforts began immediately, area was flushed and water&oil was hauled to storage tank, will monitor area for more clean up if needed. Operator applied oil absorbent to area and applied oil absorbent pads to effected area. |
1264705045 | 2010-01-27 | Production Wells | No Violations | Stopped by service rig for update on getting well back into production, operator stated that they were going to run a string of 2.875 tubing in well along with a packer, they suspect casing leak at unknown depth and also run a string of 1.5 tubing and rods and install pumping unit to get well back into production. |
1265325790 | 2010-02-04 | Production Wells | No Violations | Well has been repaired and is in production resolving previous Notice of Violation. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0708837231 | US-OH-127996 | 2010-01-19 | Failure to legibly identify well | |
0708837231 | US-OH-127997 | 2010-01-19 | Well shall be plugged |
For data sources see[9]