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Well ID: 34-059-24235 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Oxford Township | |
Operator Name: ASCENT RESOURCES UTICA LLC | |
Well Pad ID: US-OH-000490 | |
Farm/Lease Name: ATMOS W OXF GR | |
License Status: Producing | |
License Date: 2013-01-07 | |
Spud Date: 2013-02-01 | |
Spud Drilling Contractor: H&P DRILLING | |
Final Drill Date: 2013-06-22 | |
Well Total Depth: 12738 ft | |
Configuration: Horizontal | |
Latitude: 40.057845113 | |
Longitude: -81.26701568 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2012-09-11 | Proposed Formations:POINT PLEASANT, Issued Date:9/11/2012, Expired Date:9/11/2014 12:00:00 PM, Drilling unit acres:151.742, Proposed Well Type:OG, Proposed Well Class:EDPW |
APP | 2013-01-07 | Proposed Formations:POINT PLEASANT, Issued Date:1/7/2013, Expired Date:1/7/2015 12:00:00 PM, Drilling unit acres:151.742, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2013-06-22 | |
Correction to Well | 2013-09-27 | CHANGE IN TARGET & TAKE-POINT INFORMATION (FOOTAGE & X,Y COORDINATES) FROM AS DRILLED SURVEY PLAT. UNIT SIZE CHANGED TO 129.965 ACRES. |
Completion Report Received | 2014-05-08 | |
Construction Permit Expires | 2015-01-07 | |
Change of Owner | 2018-10-15 | Operator changed from 8870, HESS OHIO DEVELOPMENTS LLC to 9520, ASCENT RESOURCES UTICA LLC |
Record Last Modified | 2018-10-25 | |
Correction to Well | 2018-10-26 | CHANGE TO WELL NAME AND NUMBER. PREVIOUS--CNXGUE 10N7W #3H-8. |
For data sources see[2]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 09/09/2013 | 09/14/2013 | 7983 | 5,006,110.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Scaletrol 720 | Baker Hughes | Scale Inhibitor | Ethylene Glycol | 107-21-1 | 30 | 0.0073931 | 3661.21 |
Calcium Chloride | 10043-52-4 | 5 | 0.0012322 | 610.202 | ||||
BF-9L, 300 gal tote | Baker Hughes | Buffer | Potassium Hydroxide | 1310-58-3 | 30 | 0.0005643 | 279.45 | |
Potassium Carbonate | 584-08-7 | 60 | 0.0011286 | 558.9 | ||||
CI-14 | Baker Hughes | Corrosion Inhibitor | Polyoxyalkylenes | Trade Secret | 30 | 0.0004348 | 215.325 | |
Propargyl Alcohol | 107-19-7 | 5 | 0.00007250 | 35.8875 | ||||
Olefin | Trade Secret | 5 | 0.00007250 | 35.8875 | ||||
Fatty Acids | Trade Secret | 10 | 0.0001449 | 71.775 | ||||
Methanol | 67-56-1 | 100 | 0.0014494 | 717.75 | ||||
Ferrotrol 300L | Baker Hughes | Iron Control | Citric Acid | 77-92-9 | 60 | 0.0037682 | 1866.08 | |
XLW-32, 260 gal tote | Baker Hughes | Crosslinker | Boric Acid | 10043-35-3 | 30 | 0.0003613 | 178.935 | |
Methyl Borate | 121-43-7 | 30 | 0.0003613 | 178.935 | ||||
Methanol | 67-56-1 | 60 | 0.0007226 | 357.87 | ||||
GW-3LDF | Baker Hughes | Gelling Agent | Isotridecanol, ethoxylated | 9043-30-5 | 5 | 0.0005739 | 284.229 | |
Guar Gum | 9000-30-0 | 60 | 0.0068873 | 3410.75 | ||||
Paraffinic Petroleum Distillate | 64742-55-8 | 30 | 0.0034437 | 1705.37 | ||||
Petroleum Distillates | 64742-47-8 | 30 | 0.0034437 | 1705.37 | ||||
Crystalline Silica: Quartz | 14808-60-7 | 5 | 0.0005739 | 284.229 | ||||
1-butoxy-2-propanol | 5131-66-8 | 5 | 0.0005739 | 284.229 | ||||
GasFlo G, 330 gal tote | Baker Hughes | Surfactant | Polyoxyalkylene | Trade Secret | 10 | 0.00008050 | 39.886 | |
Methanol | 67-56-1 | 30 | 0.0002416 | 119.658 | ||||
Oxyalkylated Amine | Trade Secret | 3 | 0.00002420 | 11.9658 | ||||
Oxyalkylated Alkylphenol (1) | Trade Secret | 10 | 0.00008050 | 39.886 | ||||
Oxyalkylated Alkylphenol (2) | Trade Secret | 10 | 0.00008050 | 39.886 | ||||
Sand, White, 30/50 | Baker Hughes | Proppant | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 11.932 | 5,908,980.0 | |
GBW-5 | Baker Hughes | Breaker | Ammonium persulphate | 7727-54-0 | 100 | 0.0023606 | 1169 | |
NE-900, tote | Baker Hughes | Non-emulsifier | Nonyl phenyl polyethylene glycol ether | 9016-45-9 | 10 | 0.00008030 | 39.7775 | |
Methanol | 67-56-1 | 30 | 0.000241 | 119.333 | ||||
Water | Operator | Carrier | Water | 7732-18-5 | 100 | 84.2854 | 41,739,900.0 | |
MaxPerm-20A, 265 gallon tote | Baker Hughes | Friction Reducer | Oxyalkylated Alcohol | Trade Secret | 5 | 0.0116841 | 5786.19 | |
Petroleum Distillates | 64742-47-8 | 30 | 0.0701043 | 34717.2 | ||||
Sodium Chloride | 7647-14-5 | 3 | 0.0070104 | 3471.72 | ||||
Polyacrylate | Trade Secret | 60 | 0.140209 | 69434.3 | ||||
HCl, 5.1 - 7.5% | Baker Hughes | Acidizing | Hydrochloric Acid | 7647-01-0 | 7.5 | 0.0720342 | 35672.9 | |
Water | 7732-18-5 | 92.5 | 0.888422 | 439966 | ||||
Other Chemicals | Water | 7732-18-5 | 0 | 0.122793 | 60809.9 | |||
Sodium Chloride | 7647-14-5 | 0 | 0.00000740 | 3.6612 | ||||
Modified Thiorea Polymer | 68527-49-1 | 0 | 0.0001015 | 50.2425 | ||||
Copolymer | Trade Secret | 0 | 0.0003213 | 159.11 | ||||
Formaldehyde | 50-00-0 | 0 | 0.00001450 | 7.1775 | ||||
2-butoxy-1-propanol | 15821-83-7 | 0 | 0.00001150 | 5.6846 | ||||
Hydrochloric Acid | 7647-01-0 | 0 | 0.00001450 | 7.1775 | ||||
Oleate Ester | 1338-43-8 | 0 | 0.0070104 | 3471.72 | ||||
Potassium Chloride | 7447-40-7 | 0 | 0.00001230 | 6.102 | ||||
Polysorbate | 9005-65-6 | 0 | 0.0070104 | 3471.72 | ||||
Polyacrylate | Trade Secret | 0 | 0.0049287 | 2440.81 | ||||
Sand, White, 100 mesh | Baker Hughes | Proppant | Crystalline Silica (Quartz) | 14808-60-7 | 100 | 2.41454 | 1,195,730.0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2013-09-12 | H2O | 8 | 7843 Bbl | 481020 | BAKER-HUGHES | STAGE 8
36 SHOTS |
2013-09-13 | H2O | 8 | 7943 Bbl | 520240 | BAKER-HUGHES | STAGE 12
36 SHOTS |
2013-09-09 | H2O | 8 | 6696 Bbl | 277360 | BAKER-HUGHES | STAGE 1
36 SHOTS |
2013-09-11 | H2O | 8 | 7842 Bbl | 480440 | BAKER-HUGHES | STAGE 5
36 SHOTS |
2013-09-10 | H2O | 8 | 7756 Bbl | 481560 | BAKER-HUGHES | STAGE 2
36 SHOTS |
2013-09-12 | H2O | 8 | 8602 Bbl | 492320 | BAKER-HUGHES | STAGE 9
36 SHOTS |
2013-09-14 | H2O | 8 | 7761 Bbl | 518300 | BAKER-HUGHES | STAGE 14
36 SHOTS |
2013-10-10 | H2O | 8 | 7869 Bbl | 487500 | BAKER-HUGHES | STAGE 3
36 SHOTS |
2013-09-03 | H2O | 8 | 7679 Bbl | 488840 | BAKER-HUGHES | STAGE 10
36 SHOTS |
2013-09-11 | H2O | 8 | 7617 Bbl | 469740 | BAKER-HUGHES | STAGE 6
36 SHOTS |
2013-09-14 | H2O | 8 | 7669 Bbl | 475680 | BAKER-HUGHES | STAGE 15
36 SHOTS |
2013-09-13 | H2O | 8 | 7747 Bbl | 485840 | BAKER-HUGHES | STAGE 11
36 SHOTS |
2013-09-14 | H2O | 8 | 8206 Bbl | 485480 | BAKER-HUGHES | STAGE 13
36 SHOTS |
2013-09-10 | H2O | 8 | 7885 Bbl | 486760 | BAKER-HUGHES | STAGE 4
36 SHOTS |
2013-09-11 | H2O | 8 | 7557 Bbl | 472800 | BAKER-HUGHES | STAGE 7
36 SHOTS |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2013 | HESS OHIO DEVELOPMENTS LLC | 0 | 829 | 4 |
2014 | HESS OHIO DEVELOPMENTS LLC | 367713 | 36239 | 293 |
2015 | HESS OHIO DEVELOPMENTS LLC | 294523 | 14253 | 342 |
2016 | HESS OHIO DEVELOPMENTS LLC | 163376 | 4824 | 322 |
2017 | HESS OHIO DEVELOPMENTS LLC | 158207 | 5801 | 362 |
2018 | ASCENT RESOURCES UTICA LLC | 117318 | 3554 | 335 |
2019 | ASCENT RESOURCES UTICA LLC | 23414 | 696 | 89 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2013 | HESS OHIO DEVELOPMENTS LLC | Brine | 696 | 4 |
2014 | HESS OHIO DEVELOPMENTS LLC | Brine | 8687 | 293 |
2015 | HESS OHIO DEVELOPMENTS LLC | Brine | 6068 | 342 |
2016 | HESS OHIO DEVELOPMENTS LLC | Brine | 2514 | 322 |
2017 | HESS OHIO DEVELOPMENTS LLC | Brine | 4326 | 362 |
2018 | ASCENT RESOURCES UTICA LLC | Brine | 2214 | 335 |
2019 | ASCENT RESOURCES UTICA LLC | Brine | 396 | 89 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0045703146 | 2014-01-23 | Preliminary Restoration | No Violations | Site passed preliminary restoration according to 1509.072A. |
0236341579 | 2016-06-08 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a line heater, a bulk separator, a flash gas compressor, a fuel gas skid, a vapor recovery system, 3-400bbl condensate tanks and a 400bbl produced water tank within containment and a flare stack. The well was equipped with a plunger lift system with valves in the open position. Gauges present read 635psi on the casing and 400psi on the tubing. Identification was present and current production records. |
0491590839 | 2017-07-05 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a line heater and a bulk separator. Also present a flash gas compressor, a fuel gas skid, a vapor recovery system, 4-400 barrel tanks within containment and a flare stack and shared with the 4H-8, 2H-8 and 1H-8. The well was equipped with a plunger lift system with the valves in the open position. Gauges present read 440 pounds per square inch on the casing and 430 pounds per square inch on the tubing with annular pressure monitoring in place. Identification was present and current production records. |
1316878148 | 2018-04-25 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with production valves in the open position. Annular pressure monitoring was present. The production equipment consisted of four 400 barrel tanks, four line heaters, and four horizontal separators. A gas compression skid, horizontal vent scrubber, and a flare stack to capture tank vapors were located on the west side of the pad. A flame was present coming from the flare stack that was roughly 4 feet high at global positioning coordinates 40.05750 -81.26691. Identification was present and production records were current. |
1363555185 | 2013-03-16 | Drill / Deepen / Reopen | No Violations | On site to witness running and cementing of 20 surface casing,H&P Drilling rig 387 ran 420 of casing and used 1-shoe and 1-basket and 5 centralizes and once casing was on bottom they ran 5 drill pipe inside of casing and attempted too sting into shoe so they could cement casing in place ,unable to sting into shoe and drill pipe was partially hung in hole once free they pulled pipe and then attempted to pull 20 casing and they were unable to do so, then decision was made to run impression tools inside of casing to verify that casing is possibly collapsed.
Verified that casing is collapsed on first joint in hole and it is collapsed 8.5 in, company is trying to make decision on how to remedy problem. |
1560026824 | 2016-10-13 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a line heater and a bulk separator. Also present a flash gas compressor, a fuel gas skid, a vapor recovery system, 3-400 barrel condensate tanks and a 400 barrel produced water tank within containment and a flare stack and shared with the 4H-8, 2H-8 and 1H-8. The well was equipped with a plunger lift system with the valves in the open position. Gauges present read 400 pounds per square inch on the casing and 370 pounds per square inch on the tubing with annular pressure monitoring in place. Identification was present and current production records. |
1769281732 | 2015-12-10 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a line heater, a bulk separator, a flash gas compressor, a fuel gas skid, a vapor recovery system, 3-400bbl condensate tanks and a 400bbl produced water tank within containment and a flare stack. The well was equipped with Crown wellheads and a combination of Neeco and Cameron valves making up the production tree. Gauges present read 200psi on the casing with proper identification and current production records. |
1857962391 | 2019-03-05 | Production Wells | No Violations | The purpose of my inspection was a status check. During my inspection the well was equipped with a plunger lift system with production valves in the open position. Annular pressure monitoring was present with gauges reading 0 pounds per square inch on the 13.375-inch surface casing and 100 pounds per square inch on the 9.625-inch diameter intermediate casing. The production equipment consisted of four horizontal indirect line heaters, four horizontal separators, one gas compression skid, four 400-barrel tanks, and a flare stack. Identification was present and production records were current. |
For data sources see[9]