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Well ID: 34-019-22722 | Loading map...
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Country: United States | |
State: Ohio | |
County: Carroll | |
Municipality: Brown Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: STARK BRICK UNIT | |
License Status: Lost Hole | |
License Date: 2016-05-09 | |
Spud Date: 2017-10-24 | |
Spud Drilling Contractor: EXPRESS ENERGY SERVICES | |
Final Drill Date: 2017-10-25 | |
Well Total Depth: 50 ft | |
Configuration: Vertical | |
Latitude: 40.702252447 | |
Longitude: -81.16842111 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2016-05-09 | Proposed Formations:OHIO SHALE THRU CLINTON, Issued Date:5/9/2016, Expired Date:5/9/2018 12:00:00 PM, Drilling unit acres:53.27, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2017-10-25 | LOST HOLE WHILE AUGERING CONDUCTOR HOLE. PLUG TO SKID AND DRILL 13A- |
Reached Total Depth | 2017-10-25 | LOST HOLE WHILE AUGERING CONDUCTOR HOLE. PLUG TO SKID AND DRILL 13A- |
Record Last Modified | 2017-11-28 | LOST HOLE WHILE AUGERING CONDUCTOR HOLE. PLUG TO SKID AND DRILL 13A- |
Construction Permit Expires | 2018-05-09 | LOST HOLE WHILE AUGERING CONDUCTOR HOLE. PLUG TO SKID AND DRILL 13A- |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0126435949 | 2017-10-17 | Drill / Deepen / Reopen | No Violations | I was on site with District Supervisor Stephen Ochs to check the status of pad construction. Tree removal was complete at the time of inspection, and excavation was in progress. Silt fences were installed to the north and east of the pad, and the pits were not yet constructed. No violations were observed at the time of inspection. |
0311415018 | 2017-11-05 | Casing String Witnessed | No Violations | I was on the Stark Brick # 13 to witness a remedial squeeze operation on the 20 conductor casing. Employing a concentric drilling method the 20 conductor casing was previously set at 115 G.L. I received notification that while drilling underneath the 20 conductor at approximately 420 the drilling fluid began to circulate to the cellar outside of the 20 casing. I arrived on location at 3:30 am to discuss remedial cementing procedures with James Stephens ( Enervest ) . The plan was to perform a balanced squeeze job on the casing seat which would have the cement slurry displace the drilling fluid and re-establish the casing seat. Schlumberger mixed a cement slurry ( 200 sacks of Class A blended with 3% CaCl2) and pumped it through drill pipe from approximately 50 to 150. The cement was placed at 8:00 am and a 12 hour wait on cement time was given due to low bottom hole temperature. Fluid was observed filling the cellar as the cement slurry displaced the fluid in the microannulus. No violations identified during this inspection. |
0410707450 | 2017-12-18 | Drill / Deepen / Reopen | No Violations | Reliance Well Services was on location staging their equipment in preparation for the stimulation operation. Allied Horizontal Wireline was rigging down after completing a Cement Bond Log analysis of the horizontal lateral. A walk around inspection did not indication any violations during this inspection. |
0552690902 | 2017-10-25 | Drill / Deepen / Reopen | No Violations
-sack grout. The cellar was then filled with cement after the tin horn was removed. The pits were constructed on 10/24/2017, and inspector Bob Roush witnessed operations. The pits were lined and the liner apron was secured around the berm. Enervest will then move to a new location to drill the well. The new Stark Brick #13H permit number is 34-019-22746-00-00 | |
1867031652 | 2017-10-11 | Drill / Deepen / Reopen | No Violations | I conducted a non-urban pre- |
For data sources see[3]