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Well ID: 37-063-37473 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Banks Township | |
Operator Name: SUSQUEHANNA EXPL & PROD LLC | |
Well Pad ID: | |
Farm/Lease Name: H E CLARK ESTATE 1 | |
License Status: Active | |
Spud Date: 2013-03-04 | |
Permit Date: 2012-12-05 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.826583 | |
Longitude: -78.850225 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2013 | SUSQUEHANNA EXPL & PROD LLC | 16,611.00 | 254 | 0.00 | 0 | 0.00 | 0 |
2014 | SUSQUEHANNA EXPL & PROD LLC | 20,978.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SUSQUEHANNA EXPL & PROD LLC | 14,073.00 | 333 | 0.00 | 0 | 0.00 | 0 |
2016 | SUSQUEHANNA EXPL & PROD LLC | 12,822.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | SUSQUEHANNA EXPL & PROD LLC | 10,528.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | SUSQUEHANNA EXPL & PROD LLC | 10,722.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2013-A00 | Drilling Fluid Waste (in Barrels) | 260.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
2013-A00 | Fracing Fluid Waste (in Barrels) | 620.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
2013-A00 | Produced Fluid (in Barrels) | 185.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2014-A00 | Produced Fluid (in Barrels) | 34.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2018-A00 | Produced Fluid (in Barrels) RWC 802 | 70.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095443 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2146573 | Primary Facility | 2013-03-06 | Drilling/Alteration | Violation(s) Noted | |
2149784 | Primary Facility | 2013-03-14 | Routine/Complete Inspection | Violation(s) & Outstanding Violations | Well spudded on 3/4/2013. Site ID sign, permit, and E&S plan all on-site. Accompanied by OGI Rick Hoover.At time of inspection, drilling completed, but well not yet equipped for production.Lined below-grade drill pit on-site.Less than two feet freeboard remaining.Dept recommends Opr restore freeboard as per current regulations.Liner punctured with stakes.As per current regulation, puncturing the liner is prohibited when encapsulating the drill cuttings.Opr did not implement E&S plan as outlined.Eight culverts were to be installed along access road.Five culverts installed with first culvert at road entrance replaced by ditch turnouts.Opr installed silt fence along perimeter of pad instead of diversion ditches as outlined in plan.Structural integrity of silt fence compromised, which could result in a potential pollution event.Dept recommends Opr maintains BMPs.Direction of AR altered. AR extremely rutted, not maintained/properly constructed.Add'l viols being issued for failure to maintain freeboard and failure to maintain BMPs.Outstanding viol exist |
2161991 | Primary Facility | 2013-04-09 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Site ID sign, drilling permit, and E&S plan all on-site. At time of inspection, well equipped for production. Brine tank sound. Below-grade drill pit backfilled and pad regraded. Silt fence around pad perimeter maintained. Previously issued violations for failure to maintain at least two feet freeboard in drill pit and failure to maintain BMPs (inspection record 2149784) resolved. |
2162067 | Primary Facility | 2013-04-25 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | Follow-up inspection to violations issued under inspection record 2146573 for failure to implement E&S plan as outined. Access road still improperly constructed/not maintained, hence violation still outstanding. |
2162740 | Primary Facility | 2013-04-29 | Follow-up Inspection | Violation(s) & Outstanding Violations | Follow-up inspection to viol issued under inspection record 2146573 for failure to implement E&S plan as outined. AR still improperly constructed/not maintained, hence viol still outstanding. |
2196625 | Primary Facility | 2013-07-24 | Compliance Evaluation | No Violations Noted | CEI for violations issued under inspection records 2146573, 2162740. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2146573 | 662520 | 03/06/2013 | 2013-03-06 | 102.4 - Failure to minimize accelerated erosion, implement E&S plan, maintain E&S controls. Failure to stabilize site until total site restoration under OGA Sec 206(c)(d) | Environmental Health & Safety | Failure to implement ES Plan as designed. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
662520 | 295082 | NOV - Notice of Violation |
For data sources see[6]