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Well ID: 34-029-21550 | Loading map...
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Country: United States | |
State: Ohio | |
County: Columbiana | |
Municipality: Franklin Township | |
Operator Name: MOORE RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: FUREY ALTA | |
License Status: Producing | |
License Date: 1992-05-01 | |
Spud Date: 1992-05-11 | |
Spud Drilling Contractor: ADVENT DRLG | |
Final Drill Date: 1992-06-07 | |
Well Total Depth: 6285 ft | |
Configuration: Vertical | |
Latitude: <Latitude> | |
Longitude: -80.85307733 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1992-05-01 | Issued Date 5/1/92 Expired Date 5/1/93 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06285 Proposed Drill Depth 06285 |
Completed | 1992-06-07 | |
Reached Total Depth | 1992-06-07 | |
Original Spud | 1992-07-18 | |
Completion Report Received | 1992-09-25 | |
CO | 1992-10-01 | 3069 MURNANE JOSEPH M GeoDate 5/1/92 |
Construction Permit Expires | 1993-05-01 | |
CO | 1994-02-14 | 213 LOMAK OPERATING CO GeoDate 5/1/92 |
Change of Owner | 2000-06-27 | Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2009-11-16 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 5660, S & S ENERGY CORPORATION |
Change of Owner | 2017-01-11 | Operator changed from 5660, S & S ENERGY CORPORATION to 7988, MOORE RESOURCES LLC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 6038 | 6162 | 0 |
2006-09-11 | 6039 | 6157 | 42 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 91250 Gal | 0 | FRAC W/91,250 GAL SLICKWATER |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0565814047 | 2016-10-19 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check of well # 2-1550. RBDMS indicates the operator is delinquent in reporting production. Lease access is through an agricultural field road that is stable and in good repair. The well site is within an agricultural field and is stable with well-established vegetation. Correct and legible identification is posted at the well head. The 8.625 surface casing is near grade, with the side ports containing a plug on one side and a valve placed in the closed position on the other side. The 4.5 production casing is equipped with a plunger lift assembly. Production valves are in the open position. No audible or visual leaks were detected. The earthen dike perimeter constructed around the production equipment is weathered but sufficient for containment. Production equipment within the dike consists of one (1) horizontal separator and one (1) 100 bbl production tank. Minimum spacing requirements are met. The separator is in fair repair. No audible or visual leaks were detected. The interior of the separator control cabinet exhibits extensive corrosion and scaling. A current 16 day chart is in the meter house. The production tank is in good repair. No leaks were observed. Correct, legible identification is placed conspicuously on the tank body. The load line valve is closed and plugged. The drain line valve is closed and plugged. The hatch cover is closed. Per DOGRM Columbus, the operator is receiving a compliance notice for delinquent reporting of production. No other violations were observed during this inspection. |
0663286874 | 2014-12-31 | Production Wells | No Violations | I was on site to conduct a status check. Identification was posted on the tank battery and wellhead. The tank battery consists of one 100 bbl production tank and one horizontal separator. The tank valves are plugged. There is a meter box with a current chart showing production. The dike is present and in fair condition. The wellhead is equipped as a plunger lift. The access road and site are stable. No violations were observed. |
0675371147 | 2015-04-16 | Production Wells | No Violations | I was onsite to conduct a status check. No change since last inspection on Dec 31, 2014. No violations observed. |
iDIAN00135 | 1999-06-10 | Preliminary Restoration | No Violations |
For data sources see[9]