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Well ID: 34-005-22555 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Mifflin Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: STAUFFER DONALD | |
License Status: Storage Well | |
License Date: 1966-12-16 | |
Spud Date: 1966-12-05 | |
Spud Drilling Contractor: | |
Final Drill Date: 1967-02-14 | |
Well Total Depth: 2712 ft | |
Configuration: Vertical | |
Latitude: 40.808025427 | |
Longitude: -82.35333754 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1966-12-05 | STORAGE-47, RE-OPEN 12-22-66, GL=1265.07 |
Completed | 1967-02-14 | STORAGE-47, RE-OPEN 12-22-66, GL=1265.07 |
Reached Total Depth | 1967-02-14 | STORAGE-47, RE-OPEN 12-22-66, GL=1265.07 |
Record Last Modified | 2017-02-15 | STORAGE-47, RE-OPEN 12-22-66, GL=1265.07 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | COLUMBIA GAS TRANSMISSION LLC | 0 | 0 | 0 |
2002 | COLUMBIA GAS TRANSMISSION LLC | 0 | 0 | 0 |
2003 | COLUMBIA GAS TRANSMISSION LLC | 0 | 0 | 0 |
2004 | COLUMBIA GAS TRANSMISSION LLC | 0 | 0 | 0 |
2005 | COLUMBIA GAS TRANSMISSION LLC | 0 | 0 | 0 |
2006 | COLUMBIA GAS TRANSMISSION LLC | 0 | 0 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
2002 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
2003 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
2004 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
2005 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
2006 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0012600972 | 2016-08-18 | Work Over Reconditioning | No Violations | Hagan Well Service is rigged up on the well. The well is shut in on the 8.625 inch casing with a swage. The operator advises that they have a problem with the 3.5 inch production casing but the casing is cemented to surface. The well currently has a bridge plug in it and is killed. |
0522368896 | 2018-03-28 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is open. The well is equipped with a separator. |
1135282892 | 2019-03-07 | Storage Well | No Violations | Performed annual inspection for Columbia Gas Storage Well #10742 on 03/07/2019. The well is equipped with a flanged wellhead with 1-master valve and 1-wing valve, and a drip. The well is equipped with satellite monitoring. Well identification is clearly displayed. No problems were noted at the time of the inspection. |
1196209947 | 2016-09-26 | Work Over Reconditioning | No Violations | Hagan Well Service has a service rig on the well. The 3.5 inch casing has been milled out above the cut. The well is going to be produced using the 5.5 inch casing which is also cemented to surface. The 5.5 inch casing was pressure tested successfully. Gas remains on the backside of the drive pipe. There is no gas on the drive-surface annulus. The well is currently killed with a bridge plug in the production casing. |
1311812140 | 2017-04-24 | Storage Well | No Violations | ID is posted and the location is maintained. The annulus is open. The well is equipped with a separator. |
1393042405 | 2016-05-26 | Storage Well | No Violations | ID is posted and the location is maintained. The well is shut in and locked out. There is a 25 barrel tank at the well. The connection to the separator has been removed from the tank. The tank is wrapped in a tarp. |
1506330784 | 2014-09-08 | Storage Well | No Violations | ID posted, location maintained. 25 Bbl tank at the well site. The side gate valve is closed. |
1579329860 | 2013-10-22 | Storage Well | No Violations | ID posted, site maintained. Gas on surface annulus registered LEL and CO sensors on the detector. The well is equipped with a 50 Bbl tank. Flow was audible from the separator to the tank and the tank was at 1/2 capacity. There is also a leak from a gauge tap on the well head. Columbia is being contacted. |
1721764434 | 2015-07-22 | Storage Well | No Violations | ID is posted at the well. The valves on the wellhead are open. The backside valve is open. There is a 25 barrel tank at the well. The tank is not plumbed into the well. |
For data sources see[8]