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Well ID: 34-089-22412 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Perry Township | |
Operator Name: MFC DRILLING INC | |
Well Pad ID: | |
Farm/Lease Name: HOLBERT | |
License Status: Final Restoration | |
License Date: 2016-10-17 | |
Spud Date: 1966-10-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1966-11-03 | |
Well Total Depth: 3047 ft | |
Configuration: Vertical | |
Latitude: 40.100474281 | |
Longitude: -82.19601380 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1966-10-03 | IP. OIL = 2 1/2 BBLS. UPDATED COORDINATES PER SURVEYOR COORDINATES-ALE 06/20/2017. |
Completed | 1966-11-03 | IP. OIL = 2 1/2 BBLS. UPDATED COORDINATES PER SURVEYOR COORDINATES-ALE 06/20/2017. |
Reached Total Depth | 1966-11-03 | IP. OIL = 2 1/2 BBLS. UPDATED COORDINATES PER SURVEYOR COORDINATES-ALE 06/20/2017. |
Change of Owner | 2008-08-25 | Operator changed from 550, GEITGEY DONALD W JR to 3059, MFC DRILLING INC |
APP | 2016-10-17 | Proposed Formations:CLINTON, Issued Date:10/17/2016, Expired Date:10/17/2018 12:00:00 PM, Drilling unit acres:75, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-02-13 | IP. OIL = 2 1/2 BBLS. UPDATED COORDINATES PER SURVEYOR COORDINATES-ALE 06/20/2017. |
Record Last Modified | 2017-09-22 | IP. OIL = 2 1/2 BBLS. UPDATED COORDINATES PER SURVEYOR COORDINATES-ALE 06/20/2017. |
Construction Permit Expires | 2018-10-17 | IP. OIL = 2 1/2 BBLS. UPDATED COORDINATES PER SURVEYOR COORDINATES-ALE 06/20/2017. |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2374 Bbl | 330000 | 2 TONS ROCK SALT, 800# W. HULLS, TREATED @ 1200#. |
For data sources see[3]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1985 | ALTHEIRS OIL INC | Brine | 0 | 260 |
1986 | GEITGEY DONALD W JR | Brine | 118 | 365 |
1987 | GEITGEY DONALD W JR | Brine | 240 | 365 |
1988 | GEITGEY DONALD W JR | Brine | 290 | 366 |
1989 | GEITGEY DONALD W JR | Brine | 390 | 365 |
1990 | GEITGEY DONALD W JR | Brine | 380 | 365 |
1991 | GEITGEY DONALD W JR | Brine | 0 | 365 |
1992 | GEITGEY DONALD W JR | Brine | 80 | 365 |
1993 | GEITGEY DONALD W JR | Brine | 70 | 365 |
1994 | GEITGEY DONALD W JR | Brine | 80 | 365 |
1995 | GEITGEY DONALD W JR | Brine | 75 | 365 |
1996 | GEITGEY DONALD W JR | Brine | 60 | 366 |
1998 | GEITGEY DONALD W JR | Brine | 0 | 0 |
1999 | GEITGEY DONALD W JR | Brine | 28 | 365 |
2000 | GEITGEY DONALD W JR | Brine | 0 | 365 |
2002 | GEITGEY DONALD W JR | Brine | 0 | 365 |
2003 | GEITGEY DONALD W JR | Brine | 20 | 0 |
2004 | GEITGEY DONALD W JR | Brine | 0 | 365 |
2005 | GEITGEY DONALD W JR | Brine | 0 | 365 |
2006 | GEITGEY DONALD W JR | Brine | 0 | 365 |
2008 | MFC DRILLING INC | Brine | 0 | 0 |
2009 | MFC DRILLING INC | Brine | 1640 | 365 |
2010 | MFC DRILLING INC | Brine | 420 | 365 |
2011 | MFC DRILLING INC | Brine | 0 | 0 |
2012 | MFC DRILLING INC | Brine | 0 | 366 |
2013 | MFC DRILLING INC | Brine | 0 | 365 |
2014 | MFC DRILLING INC | Brine | 0 | 365 |
2015 | MFC DRILLING INC | Brine | 70 | 365 |
2016 | MFC DRILLING INC | Brine | 0 | 365 |
2017 | MFC DRILLING INC | Brine | 194 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0303660934 | 2015-01-26 | Production Wells | No Violations | This inspection was conducted as a status check. The rods and tubing have been removed. The well will be placed into production as a swab well. A 100 barrel tank has been brought in. The well had a 4 to 2 swage with a 2 valve in the closed position. Identification will need to be posted once tank battery is built and well is in production. Time of inspection: 1:30 PM. Weather: 27 degrees F, 4 snow |
0381376239 | 2017-09-15 | Final Restoration | No Violations | The inspection revealed that the 100 barrel tank has been removed and grass seed was applied. The well location meets ORC 1509.072 requirements. Time of inspection: 1:15 PM. Weather: 71*F, Partly cloudy |
0423871367 | 2017-02-13 | Plug / Plug Back | No Violations | I returned to this well today to witness the plugging of it. The rig crew was able to work the 5.5 inch casing free after pulling 6 joints. We then set a 250 feet Big Lime plug at this point. From there the rig crew pulled the 5.5 inch casing up the hole to set the bottom of the surface plug at the 7 inch casing since the Berea was behind pipe. We pumped a 200 foot plug at the bottom of the surface. After that plug was set we pulled the 5.5 inch diameter casing up to set a 200 foot surface plug. The cement held at the surface. The well is now plugged. |
0845703305 | 2017-08-03 | Final Restoration | No Violations | The purpose of this inspection is to document a phone conversation with Mr. Jim Aslanides of MFC Drilling Inc. regarding the final restoration. Mr. Aslanides was informed that the restoration is almost due to be complete as it has been approximately 6 months since the well has been plugged. Mr. Aslanides informed be that he would have someone look at it and work on getting it completed. Time of phone call: 1:17 PM. |
1374968115 | 2014-11-04 | Production Wells | No Violations | This inspection was conducted as a production well status check. The well consisted of rods and tubing but no pumping unit or flow line. No tank battery or identification. |
1405673296 | 2017-06-13 | Final Restoration | No Violations | This inspection was conducted as a status check. The well has been plugged. The final restoration is due to be completed by 8/13/2017. The inspection revealed that a 100 barrel tank and metal flow line has not been removed as of this date. A compliance notice will be issued if restoration is not complete by 8/13/2017. A phone call was placed to MFC Drilling President Mr. Jim Aslanides to inform him of what all needs done. Mr. Aslanides was made aware of the time frame to have it completed by. Time of inspection: 2:00 PM. Weather: 85*F, Sunny |
1411905024 | 2015-04-15 | Production Wells | No Violations | Inspect well. No change in status. A phone call was placed to Jeff Harmon with MFC Drilling. Mr. Harmon stated that this well is scheduled to be plugged this year. Time of inspection: 2:30 PM. Weather: 64*F, Sunny |
1584217845 | 2017-08-18 | Final Restoration | No Violations | During the inspection the well location was observed. The final restoration has not been completed. It appears that the flow line has been removed but a 100 barrel tank was still at the well location. It will be suggested to spread some grass seed/straw on some areas that vegetation is sparse. The company will be granted an extension of 30 days. A compliance notice will be issued on or after 9/18/2017 if the restoration is not complete. MFC Drilling President Jim Aslanides was contacted via phone conversation and was advised of the due date. Time of inspection: 10:00 AM. Weather: 79*F, Partly cloudy |
1922074639 | 2017-02-10 | Plug / Plug Back | No Violations | I was on location today to witness the plugging of this well. MFC Drilling has there service rig in on the well to plug it. Today I witnessed the bottom plug being set through the 5.5 inch diameter casing. We bullheaded the bottom plug because the well was dry instead of pumping the plug through the tubing. Once the plug was set the rig crew ran the ripping tools in the well to rip the 5.5 inch diameter casing. The rig crew was able to find the telegraph at 1670 feet indicating the pipe was free at this spot. The rig crew was able to rip the casing at 1670 feet but the pipe was hung at this point. The rig crew worked the pipe up and down to free it up in the hole. They ended up shutting down at 4 pm. They will be working on freeing up the casing Monday morning. |
2111274998 | 2014-11-06 | Administrative Inspection | No Violations | A phone call was placed to Jeff Harmon with MFC Drilling regarding the status of this well. Mr. Harmon stated that this well is scheduled to be plugged next year. |
For data sources see[8]