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Well ID: 34-155-20026 | Loading map...
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Country: United States | |
State: Ohio | |
County: Trumbull | |
Municipality: Newton Township | |
Operator Name: ERIC PETROLEUM CORP | |
Well Pad ID: | |
Farm/Lease Name: BIGGARD C L UNIT | |
License Status: Producing | |
License Date: 1971-09-02 | |
Spud Date: 1971-09-11 | |
Spud Drilling Contractor: | |
Final Drill Date: 1971-11-09 | |
Well Total Depth: 4782 ft | |
Configuration: Vertical | |
Latitude: 41.142269355 | |
Longitude: -80.91094230 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1971-09-02 | 2936 COLUMBIA NATURAL RES INC GeoDate 9/2/71 |
Original Spud | 1971-09-11 | |
Completed | 1971-11-09 | |
Reached Total Depth | 1971-11-09 | |
Change of Owner | 2010-10-27 | Operator changed from 2936, CHESAPEAKE APPALACHIA LLC to 5054, ERIC PETROLEUM CORP |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 34340 Gal | 26000 | BROKE @ 3M#. TRTD. 3900-2800# @ 23 BBLS./MIN. ISIP 1M. |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1051193891 | 2014-01-15 | Production Wells | No Violations | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a vertical separator. There was a plug on the load line. The dike met containment requirements with a 4 drain and cap. An identification sign was proper posted on the tank. The lease road was in good condition. |
For data sources see[8]