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Well ID: 34-099-23149 | Loading map...
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Country: United States | |
State: Ohio | |
County: Mahoning | |
Municipality: Poland Township | |
Operator Name: BOCOR HOLDINGS, LLC | |
Well Pad ID: | |
Farm/Lease Name: ZIMMERMAN | |
License Status: Producing | |
License Date: 2011-04-25 | |
Spud Date: 2011-07-31 | |
Spud Drilling Contractor: G & G DRLG | |
Final Drill Date: 2011-08-02 | |
Well Total Depth: 5855 ft | |
Configuration: Vertical | |
Latitude: 41.059617239 | |
Longitude: -80.54788555 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-04-25 | Proposed Formations:CLINTON/MEDINA, Issued Date:4/25/2011, Expired Date:4/24/2013 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2011-08-02 | |
Completion Report Received | 2011-09-27 | |
Construction Permit Expires | 2012-04-24 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-12-08 | 5585 | 5641 | 69 |
2011-12-08 | 5730 | 5736 | 13 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2011-08-15 | H2O | 15 | 83050 Gal | 60000 | Universal Well Services Inc. | 82 perforations, 13 perf balls dropped. No significant pressure change throughout fracturing procedure. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
0 | 0 | 0 | ||
2011 | BOCOR HOLDINGS, LLC | 376 | 0 | 127 |
2012 | BOCOR HOLDINGS, LLC | 8658 | 0 | 366 |
2013 | BOCOR HOLDINGS, LLC | 3511 | 0 | 365 |
2014 | BOCOR HOLDINGS, LLC | 2953 | 0 | 365 |
2015 | BOCOR HOLDINGS, LLC | 1891 | 0 | 368 |
2016 | BOCOR HOLDINGS, LLC | 1483 | 0 | 365 |
2017 | BOCOR HOLDINGS, LLC | 1416 | 0 | 365 |
2018 | BOCOR HOLDINGS, LLC | 1038 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | BOCOR HOLDINGS, LLC | Brine | 630 | 127 |
2012 | BOCOR HOLDINGS, LLC | Brine | 325 | 366 |
2013 | BOCOR HOLDINGS, LLC | Brine | 340 | 365 |
2014 | BOCOR HOLDINGS, LLC | Brine | 170 | 365 |
2015 | BOCOR HOLDINGS, LLC | Brine | 165 | 368 |
2016 | BOCOR HOLDINGS, LLC | Brine | 146 | 365 |
2017 | BOCOR HOLDINGS, LLC | Brine | 58 | 365 |
2018 | BOCOR HOLDINGS, LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0017612493 | 2011-09-13 | Preliminary Restoration | No Violations | Still grading out top soil, very muddy. Chain link fencing around well head and tank battery, ID sign posted. Still needs seeded. Does not pass Preliminary Restoration at this time. |
0701829882 | 2011-08-02 | Drill / Deepen / Reopen | No Violations | G&H Rig # 91 not drilling, hooking up BOP. Loading pits. Witnessed BOP test - pressured up to 360 psi at 14:54, held for 15 minutes, showed 340 psi at 15:09. No leaks or spills. No violations at this time. |
0754814357 | 2011-08-23 | Preliminary Restoration | No Violations | Pits closed but mounds of top soil still surround location. Crew is on site constructing tank battery and running production line. Does not pass Preliminary Restoration at this time. |
0850137557 | 2011-08-11 | Preliminary Restoration | No Violations | Pits still open, top soil berms and orange fences around pits. Crew moving frac tanks onto location. No violations at this time. |
1227712089 | 2011-10-13 | Preliminary Restoration | No Violations | All top soil graded out but not seeded. Area to be planted with agricultural crops per restoration plan. Chain link fencing installed around well head and tank battery and ID sign posted. Locking tube gate installed at lease road entrance. This site passes Preliminary Restoration. |
1312485055 | 2011-08-04 | Drill / Deepen / Reopen | No Violations | G&H Rig #91 drilling on air, at a depth of 3896. Permit properly displayed in doghouse and at lease road entrance. H2S gas detector on rig, 300 bbl brine in pit. Walked site. Pit liners in good condition. No leaks or spills. No violations at this time. |
1313752075 | 2011-08-15 | Completion Testing | No Violations | On site to witness frac job. Pit liners in good condition. Universal Well Service conducting frac job. No fluid returns from annulus observed during or after frac job. No leaks or spills. No violations at this time. |
1417182919 | 2011-08-01 | Drill / Deepen / Reopen | No Violations | G&H Rig #91 drilling on fluid. At depth of 280. Permit properly displayed in doghouse and at lease road entrance. H2S gas detector on rig. Security fence in place around pits. Walked site. Pit liners in good condition. Silt fence in place along west side of location. No leaks or spills. No violations at this time. |
1528994163 | 2018-06-11 | Production Wells | No Violations | The purpose of my inspection was to conduct a status check on well #2-3149. On 6/08/2018 a local resident reported a gas release from the tank battery. ODNR-DOGRM Emergency operations and response coordinator Fred Romeo responded to the incident with local fire personnel. RBDMS indicated reported production was current. Access to the well and tank battery remained drivable and stable. The well was located within a locked chain-link fence enclosure. The 8.625 well head was below grade. The 4.5 production casing was equipped with a plunger lift assembly. The master gate valve was closed. No leaks were observed. A gauge fitted to the tubing string indicated 180 psi. A domestic supply connection was present. A stable earthen dike that was free of fluid was present around the production equipment. A locked chain-link fence enclosure was present on top of the dike. Equipment on location consisted of one (1) mechanical separator, one (1) 140 bbl production tank and one (1) 50 bbl poly brine tank. The separator was shut in. At the time of my inspection, I did not witness any impact from the gas release. The production tank remained in good repair and contained correct identification. Valves were closed, locked and plugged. The hatch lid of the tank remained unbolted and removed from the tank body. The poly brine tank remained in good repair. The inlet valve was closed. I will contact Bocor Holdings to determine the status of repairs and source of failure. |
For data sources see[9]