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34-173-61183

Well Details

Well ID: 34-173-61183
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Country: United States
State: Ohio
County: <County>
Municipality: Portage Township
Operator Name: LANDOWNER GRANT PROGRAM 2011
Well Pad ID:
Farm/Lease Name: CARPENTER ROBERT (BATESON RICHARD)
License Status: Final Restoration
License Date: 2011-08-03
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.283807353
Longitude: -83.55227884

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 2007-12-02 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
APP 2011-08-03 Proposed Formations:, Issued Date:8/3/2011, Expired Date:8/2/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2011-08-03 Operator changed from 9999, UNKNOWN OWNER to 8825, LANDOWNER GRANT PROGRAM 2011
Plugged by Orphan Well Program 2012-05-16 Plugged by Orphan Well Program
Plugged/Abandoned 2012-05-16 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
Construction Permit Expires 2013-08-02 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.
Record Last Modified 2019-06-14 NO PREVIOUS RECORD OF WELL. INSPECTION ON 10/27/1993 FOUND 8" SURFACE CASING ONLY. I&O CASE # 1994 10 092. WILL NEED TO CORRECT THE WELL LOCATION WHEN GET A GPS LOCATION.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0136721053 2012-04-30 Orphan No Violations At the time of my inspection the cable tool rig was set up on the well and 5.5 bit was ran to about 400 until an unknown obstruction was encountered. The crew is now setting up to run tubing in and circulate hole.
0376435608 2012-05-01 Orphan No Violations At the time of my inspection a new piece oc casing had to be welded on existing 8 to attach a wellhead. 2 tubing was then ran to 400 to circulate oil out of the wellbore. The tubing is starting to hang up on what we believe is a few remaining pieces of 6 surface casing around 270 (bottom of the Big Lime).
0511940394 2012-05-03 Orphan No Violations At the time of my inspection another obstruction was hit at 745 and tubing continues to hang up not only on the way down but on the way out as well. Continued circulation has produced no more oil from wellbore.
0587709463 2012-05-17 Orphan No Violations At the time of my inspection the plate has been welded on the top of casing and buried four feet below grade. The pit is also being closed and field tile is being replaced.
1337181753 2012-05-04 Plug / Plug Back No Violations Plugging Contractor is Black Swamp Oilfield Services, Mike Coyer. Plug set at TD of 744 due to the collapsing shale formation and a crooked hole. The drill pipe is catching on pieces of the surface casing still left in the hole from when it was removed. See Plug Report for details.
1337184796 2012-05-15 Plug / Plug Back No Violations On site for setting of plug 2 from 342 to 48. Cement pumped through 2 tubing with circulation of cement to surface. Fresh water formation is taking some cement so level is dropping. See Plug Report for details.
1939794195 2012-05-16 Plug / Plug Back No Violations At the time of my inspection the well was topped off from 48 to the surface with 28 sacks of Sackrete.
1955094967 2012-05-02 Orphan No Violations Rain in the area delayed continuatiun of claenout till mid afternnoon. At the time of my inspection the 2 tubing was at 452 and continued to 545. The tubing was to hang up and is getting worse as they go deeper.
2012623642 2012-12-04 Final Restoration No Violations At the time of my inspection the area was cleared of all equipment and all pits were closed. The area was then roughly graded for farm use next year. Final Restoration Passed.

For data sources see[3]

References