If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-167-23614 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.442960871,"lon":-81.62007708,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Watertown Township | |
Operator Name: POTTMEYER DAVID | |
Well Pad ID: | |
Farm/Lease Name: BARTLETT E | |
License Status: Producing | |
License Date: 1976-10-19 | |
Spud Date: 1976-10-31 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-11-03 | |
Well Total Depth: 2005 ft | |
Configuration: Vertical | |
Latitude: 39.442960871 | |
Longitude: -81.62007708 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-10-19 | 2176 OIL FUNDS MANAGEMENT INC GeoDate 10/19/76 |
Original Spud | 1976-10-31 | |
Completed | 1976-11-03 | |
Reached Total Depth | 1976-11-03 | |
CO | 1996-07-15 | 3133 PETROEL GeoDate 10/19/76 |
Change of Owner | 1998-09-01 | Operator changed from 3133, PETROEL to 6173, MARIETTA NATURAL GAS, LLC |
Change of Owner | 2000-01-31 | Operator changed from 6173, MARIETTA NATURAL GAS, LLC to 3133, PETROEL |
Change of Owner | 2000-04-20 | Operator changed from 3133, PETROEL to 5557, POTTMEYER DAVID A |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1921 | 1926 | 13 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1100 Bbl | 36000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1995 | PETROEL | 0 | 0 | 0 |
1996 | PETROEL | 0 | 0 | 0 |
2001 | POTTMEYER DAVID | 380 | 4 | 365 |
2002 | POTTMEYER DAVID | 788 | 0 | 365 |
2003 | POTTMEYER DAVID | 913 | 0 | 365 |
2004 | POTTMEYER DAVID | 1146 | 19 | 365 |
2005 | POTTMEYER DAVID | 634 | 0 | 365 |
2006 | POTTMEYER DAVID | 929 | 60 | 365 |
2008 | POTTMEYER DAVID | 1187 | 45 | 365 |
2010 | POTTMEYER DAVID | 683 | 0 | 365 |
2011 | POTTMEYER DAVID | 511 | 34 | 365 |
2012 | POTTMEYER DAVID | 533 | 0 | 366 |
2013 | POTTMEYER DAVID | 431 | 29 | 365 |
2014 | POTTMEYER DAVID | 294 | 10 | 365 |
2015 | POTTMEYER DAVID | 378 | 10 | 365 |
2016 | POTTMEYER DAVID | 177 | 9 | 365 |
2017 | POTTMEYER DAVID | 74 | 0 | 365 |
2018 | POTTMEYER DAVID | 158 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1995 | PETROEL | Brine | 0 | 0 |
1996 | PETROEL | Brine | 0 | 0 |
2001 | POTTMEYER DAVID | Brine | 90 | 365 |
2002 | POTTMEYER DAVID | Brine | 0 | 365 |
2003 | POTTMEYER DAVID | Brine | 0 | 365 |
2004 | POTTMEYER DAVID | Brine | 0 | 365 |
2005 | POTTMEYER DAVID | Brine | 0 | 365 |
2006 | POTTMEYER DAVID | Brine | 0 | 365 |
2008 | POTTMEYER DAVID | Brine | 0 | 365 |
2010 | POTTMEYER DAVID | Brine | 0 | 365 |
2011 | POTTMEYER DAVID | Brine | 0 | 365 |
2012 | POTTMEYER DAVID | Brine | 0 | 366 |
2013 | POTTMEYER DAVID | Brine | 0 | 365 |
2014 | POTTMEYER DAVID | Brine | 0 | 365 |
2015 | POTTMEYER DAVID | Brine | 154 | 365 |
2016 | POTTMEYER DAVID | Brine | 82 | 365 |
2017 | POTTMEYER DAVID | Brine | 0 | 365 |
2018 | POTTMEYER DAVID | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0826086287 | 2016-03-21 | Production Wells | No Violations | Upon inspection, it was observed that the contaminated soil has been removed from inside and outside of the containment dike, the dike walls have been rebuilt, and the soil has been limed, seeded, and mulched. This satisfies the requirements of the compliance notice dated 3/15/2016. |
1639906425 | 2016-03-14 | Production Wells | Violations Noted | Received call from SE Region Supervisor Brent Bear about an anonymous complaint of an overflowing production tank associated with this well. Upon inspection, it was observed that the 100 bbl tank had overflowed and released oil and brine into the containment dike surrounding the tank. The dike wall is breached in the SE corner and allowed brine and oil to flow approximately 60 downhill from the tank battery. The operator knows of the contamination and has initiated cleanup efforts by spreading peat moss over the oil soaked areas to help slow its migration. It is unclear how much product was lost from the tank, however there is <0.5 bbls of oil and brine laying inside the containment dike area. There is 1 of headspace in the top of the tank, indicating some product was removed after it overflowed. Field testing with Hach Quantab Titration Strips showed a chloride level of over 6215 ppm in the fluid laying inside the containment dike. Photos were taken to support the findings of this inspeciton. The operator, David Pottmeyer, shall meet the following requirements within 14 days of receiving this notice: 1.) Remove all contaminated soil from inside and outside of the containment dike and dispose of it at an OEPA approved landfill; 2.) Reconstruct the containment dike walls to meet SPCC guidelines; 3.) Lime/fertilize and seed/mulch the affected area to encourage vegetation growth. |
2131345672 | 2004-05-24 | Production Wells | No Violations | Inspection this day found well producing, current chart in meter, big 200-bbl tank with no dike, good IDs but wrong permit no. - I corrected it. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1639906425 | US-OH-116136 | 2016-03-31 | Well operation causing pollution and contamination | |
1639906425 | US-OH-116137 | 2016-03-31 | Dike or pit not able to prevent escape of brine or other wastes |
For data sources see[9]