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37-083-04427

Well Details

Well ID: 37-083-04427
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Country: United States
State: Pennsylvania
County: McKean
Municipality: Sergeant Township
Operator Name: DIVERSIFIED OIL & GAS LLC
Well Pad ID:
Farm/Lease Name: MANOR REAL ESTATE 1103
License Status: Active
Spud Date: 1800-01-01
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 41.6782
Longitude: -78.6617

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1992 NATL FUEL GAS SUPPLY CORP 1,172.00 335 0.00 0 0.00 0
1996 SENECA RESOURCES CO LLC 1,146.00 365 0.00 0 0.00 0
1997 SENECA RESOURCES CO LLC 1,024.00 365 0.00 0 0.00 0
1998 SENECA RESOURCES CO LLC 880.00 365 0.00 0 0.00 0
1999 SENECA RESOURCES CO LLC 880.00 365 0.00 0 0.00 0
2000 SENECA RESOURCES CO LLC 66.00 365 0.00 0 0.00 0
2001 SENECA RESOURCES CO LLC 587.00 365 0.00 0 0.00 0
2002 SENECA RESOURCES CO LLC 636.00 365 0.00 0 0.00 0
2003 SENECA RESOURCES CO LLC 1,142.00 365 0.00 0 0.00 0
2004 SENECA RESOURCES CO LLC 875.00 365 0.00 0 0.00 0
2006 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2007 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 46.00 365 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2014 SENECA RESOURCES CO LLC 69.00 365 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2016 DIVERSIFIED OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2017 DIVERSIFIED OIL & GAS LLC 0.00 0 0.00 0 0.00 0
2018 DIVERSIFIED OIL & GAS LLC 220.00 365 0.00 0 0.00 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2814853 Primary Facility 2018-12-13 Administrative/File Review No Violations Noted Administrative inspection to update the wells location, the latitude and longitude were provided by the operator.
2815615 Primary Facility 2018-12-13 Routine/Complete Inspection Violation(s) Noted This is an open flowing well with the pumpjack removed. It is uncertain whether the valve on the line is opened or not, due to the age of this well and equipment. No sound of gas can be heard flowing through this line, however. The access road was highly rutted and had a tree fallen across it, indicating lack of recent operator access. There was no production reported for this well on the 2017 annual production report - comments provided in the report indicate “Well Temporarily Not Producing”.

This well is abandoned as defined in section 3203 of the 2012 Oil & Gas Act.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2815615 836311 2018-12-13 2019-03-07 OGA3220(A) Environmental Health & Safety
2815615 836312 2018-12-13 2019-03-07 OGA3211(H) Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
836311 369710 NOV - Notice of Violation 2019-03-07
836311 372946 COA - Consent Order and Agreement
836312 369710 NOV - Notice of Violation 2019-03-07

For data sources see[5]

References