X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-005-22515

Well Details

Well ID: 34-005-22515
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Jackson Township
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name: BROWN UNIT
License Status: Active Injection
License Date: 1986-07-14
Spud Date: 1986-07-30
Spud Drilling Contractor: P&N DRLG
Final Drill Date: 1987-01-15
Well Total Depth: 748 ft
Configuration: Vertical
Latitude: 40.901972611
Longitude: -82.14671376

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1986-07-07 133 QUAKER STATE OIL REF CORP GeoDate 7/7/86
Enhanced Recovery 1986-07-07 Issued Date 7/14/86 Expired Date 7/14/87 Acres 0150047 Tool Type NT Proposed Formation BEREA Proposed Depth 00748 Proposed Drill Depth 00748
Original Spud 1986-07-30 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
First Injection 1986-12-03 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
Completion Report Received 1987-01-12 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
Completed 1987-01-15 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
Reached Total Depth 1987-01-15 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
Construction Permit Expires 1987-07-14 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
CO 1995-10-18 182 BELDEN & BLAKE CO GeoDate 7/7/86
Annulus Pressure Monitoring Approved 1998-06-09 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
Last Compliance Report 2000-01-14 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD
Change of Owner 2002-02-07 Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER
Change of Owner 2008-04-24 Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC
Record Last Modified 2017-02-15 CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-23 670 720 0
2000-05-23 675 705 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 40 Qts 0 FOR ERP
NITR 0 100 Qts 0 FOR PRODUCTION

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 QUAKER STATE OIL REF CORP 0 0 0
1985 QUAKER STATE OIL REF CORP 0 0 0
1986 QUAKER STATE OIL REF CORP 0 7 365
1987 QUAKER STATE OIL REF CORP 0 20 365
1988 QUAKER STATE OIL REF CORP 0 49 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 QUAKER STATE OIL REF CORP Brine 0 0
1985 QUAKER STATE OIL REF CORP Brine 0 0
1986 QUAKER STATE OIL REF CORP Brine 0 365
1987 QUAKER STATE OIL REF CORP Brine 46 365
1988 QUAKER STATE OIL REF CORP Brine 48 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0016078257 2016-11-01 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0096674668 2014-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0098663015 2005-12-01 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0142504724 2018-05-02 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0187265422 2017-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0209075839 2010-12-16 Enhanced Recovery Project Violations Noted Injection and annulus pressure test. ERP# 19, W-6.
0257465535 2009-04-27 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0358586615 2012-05-31 Enhanced Recovery Project No Violations Inspect Well.
0370412118 2012-12-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0453286750 2010-04-06 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0468045381 2008-12-18 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0509274170 2017-11-14 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0770744265 2003-08-07 Enhanced Recovery Project No Violations CANNOT ACCESS INJECTION PSI, NEED TO REPLACE WITH 1/2 OR 1/4 VALVE FOR GAUGE
0875210395 2009-10-07 Enhanced Recovery Project No Violations Injection and annulus pressure test.
0906784221 2015-05-18 Enhanced Recovery Project No Violations The well is an injection well in the waterflood enhanced recovery project. ID posted.
0943677300 2010-12-17 Enhanced Recovery Project No Violations Pressured up annulus to 280 psi. No drop in pressure in 15 minutes. W-6
0944436228 2014-03-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0980994820 2012-03-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
0981320109 2004-11-17 Enhanced Recovery Project No Violations Injection pressure test.
1011304060 2006-08-21 Enhanced Recovery Project No Violations Injection and annulus pressure test. Sun, 75 degrees.
1018852456 2017-01-05 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1062308488 2008-03-13 Enhanced Recovery Project No Violations Annulus and injection pressure test.
1166552149 2006-12-19 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1230778509 2005-04-27 Enhanced Recovery Project No Violations Injection well test.
1285411367 2014-07-17 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1445429518 2015-10-20 Enhanced Recovery Project No Violations Notified by operator the well was serviced and worked over. Inspected well for compliance. The 2-3/8 inch casing failed at the well head. A hanger bracket caused the casing to rust through. The casing was cut off below grade and new casing was welded in place. The tubing packer was not released during the workover. The compliance order of 8/28/2015 was released.
1446048412 2015-10-26 Enhanced Recovery Project No Violations On June 11, 1998 a total of 24 joints of one inch tubing at 25 feet long were set in the hole at 600 feet. On October 9, 2015 notified by operator the well was serviced and worked over. The 2-3/8 inch casing split open and failed at the well head. A hanger bracket caused the casing to rust through. The well head was excavated and the casing was cut off below grade. The casing was threaded and new casing was installed and reassembled. The tubing and packer set in compression was not released during the workover. One inch of the one inch injection tubing was cut off and re-threaded. The compliance order of 8/28/2015 was resolved. Conduct a mechanical integrity test on well. Well annulus was pressured to 360 psi and held for 15 minutes with zero pressure loss. Well passes. Well is put into production. Compliance notice has been resolved.
1453264915 2012-09-11 Enhanced Recovery Project No Violations Inspect Well. Site ok.
1568085131 2018-08-20 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1592563039 2014-05-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1607016907 2017-04-24 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1626257319 2018-10-10 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1684121092 2016-01-06 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1752943849 2007-10-17 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1756283585 2013-04-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test.
1803023632 2016-04-15 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1832805483 2013-10-29 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1853055022 2019-01-04 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1867454530 2015-03-19 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.
1886404824 2007-05-24 Enhanced Recovery Project No Violations Injection and annulus pressure test.
1943737110 2012-02-06 Enhanced Recovery Project No Violations inspect well.
1953276135 2011-07-11 Enhanced Recovery Project No Violations inspect well.
1998582579 2015-05-20 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The injection valve is leaking.
2010575679 2011-10-18 Enhanced Recovery Project No Violations Inspect well.
2033086035 2015-08-28 Enhanced Recovery Project Violations Noted Inspect well for integrity and pressure. The well is shut in. the injection tubing valve is broken.
2044282527 2018-01-18 Enhanced Recovery Project No Violations Inspect well for integrity and pressure.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0209075839 US-OH-121353 2010-12-16 Failure to conduct or pass mech. integrity test
1998582579 US-OH-120287 2015-07-17 Mechanical failure/contamination
2033086035 US-OH-120669 2015-12-15 Violation of injection tubing/fitting requirements

For data sources see[9]

References