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Well ID: 34-031-22393 | Loading map...
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Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Oxford Township | |
Operator Name: GRESS OIL & GAS | |
Well Pad ID: | |
Farm/Lease Name: WATERS PAUL C | |
License Status: Producing | |
License Date: 1985-09-26 | |
Spud Date: 1974-06-17 | |
Spud Drilling Contractor: | |
Final Drill Date: 1987-03-17 | |
Well Total Depth: 4460 ft | |
Configuration: Vertical | |
Latitude: 40.272984018 | |
Longitude: -81.66916612 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1974-05-09 | 124 MOORE JERRY INC GeoDate 5/9/74 |
Original Spud | 1974-06-17 | IP. A.F. 1.5 MMCFG |
CO | 1985-09-26 | 124 MOORE JERRY INC GeoDate 9/26/85 |
Oil and Gas | 1985-09-26 | Issued Date 9/26/85 Expired Date 9/26/86 Acres 0210400 Tool Type RTF Proposed Formation ORISKANY Proposed Depth 00000 Proposed Drill Depth 00000 |
Plugged Back | 1985-09-28 | IP. A.F. 1.5 MMCFG |
Construction Permit Expires | 1986-09-26 | IP. A.F. 1.5 MMCFG |
Completed | 1987-03-17 | IP. A.F. 1.5 MMCFG |
Completion Report Received | 1987-03-17 | IP. A.F. 1.5 MMCFG |
Reached Total Depth | 1987-03-17 | IP. A.F. 1.5 MMCFG |
Change of Owner | 1999-11-04 | Operator changed from 124, MOORE JERRY INC to 5378, GRESS OIL & GAS |
Record Last Modified | 2013-10-03 | IP. A.F. 1.5 MMCFG |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4332 | 4400 | 27 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 46000 Gal | 45000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | COLUMBIA GAS TRANSMISSION LLC | 891 | 0 | 0 |
1985 | COLUMBIA GAS TRANSMISSION LLC | 0 | 5 | 0 |
1987 | JERRY MOORE INC | 2751 | 0 | 365 |
1988 | JERRY MOORE INC | 1801 | 0 | 365 |
1989 | JERRY MOORE INC | 1954 | 47 | 365 |
1990 | JERRY MOORE INC | 1062 | 30 | 365 |
1991 | JERRY MOORE INC | 0 | 0 | 365 |
1992 | JERRY MOORE INC | 2276 | 0 | 365 |
1993 | JERRY MOORE INC | 1984 | 0 | 365 |
1994 | JERRY MOORE INC | 1293 | 0 | 365 |
1995 | JERRY MOORE INC | 966 | 0 | 365 |
1996 | JERRY MOORE INC | 1014 | 32 | 365 |
1997 | JERRY MOORE INC | 2117 | 37 | 365 |
1998 | JERRY MOORE INC | 2079 | 50 | 365 |
1999 | JERRY MOORE INC | 1142 | 44 | 365 |
2000 | GRESS OIL & GAS | 1133 | 0 | 365 |
2001 | GRESS OIL & GAS | 988 | 0 | 365 |
2002 | GRESS OIL & GAS | 605 | 0 | 365 |
2003 | GRESS OIL & GAS | 745 | 0 | 365 |
2004 | GRESS OIL & GAS | 893 | 0 | 365 |
2005 | GRESS OIL & GAS | 780 | 0 | 365 |
2006 | GRESS OIL & GAS | 717 | 0 | 365 |
2007 | GRESS OIL & GAS | 661 | 0 | 365 |
2008 | GRESS OIL & GAS | 571 | 0 | 365 |
2009 | GRESS OIL & GAS | 527 | 0 | 365 |
2010 | GRESS OIL & GAS | 558 | 0 | 365 |
2011 | GRESS OIL & GAS | 537 | 0 | 365 |
2012 | GRESS OIL & GAS | 432 | 0 | 366 |
2013 | GRESS OIL & GAS | 420 | 0 | 365 |
2014 | GRESS OIL & GAS | 386 | 0 | 365 |
2015 | GRESS OIL & GAS | 335 | 0 | 365 |
2016 | GRESS OIL & GAS | 300 | 0 | 365 |
2017 | GRESS OIL & GAS | 303 | 0 | 365 |
2018 | GRESS OIL & GAS | 138 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
1985 | COLUMBIA GAS TRANSMISSION LLC | Brine | 0 | 0 |
1987 | JERRY MOORE INC | Brine | 0 | 365 |
1988 | JERRY MOORE INC | Brine | 15 | 365 |
1989 | JERRY MOORE INC | Brine | 0 | 365 |
1990 | JERRY MOORE INC | Brine | 0 | 365 |
1991 | JERRY MOORE INC | Brine | 0 | 365 |
1992 | JERRY MOORE INC | Brine | 0 | 365 |
1993 | JERRY MOORE INC | Brine | 0 | 365 |
1994 | JERRY MOORE INC | Brine | 0 | 365 |
1995 | JERRY MOORE INC | Brine | 0 | 365 |
1996 | JERRY MOORE INC | Brine | 0 | 365 |
1997 | JERRY MOORE INC | Brine | 0 | 365 |
1998 | JERRY MOORE INC | Brine | 0 | 365 |
1999 | JERRY MOORE INC | Brine | 0 | 365 |
2000 | GRESS OIL & GAS | Brine | 0 | 365 |
2001 | GRESS OIL & GAS | Brine | 0 | 365 |
2002 | GRESS OIL & GAS | Brine | 0 | 365 |
2003 | GRESS OIL & GAS | Brine | 0 | 365 |
2004 | GRESS OIL & GAS | Brine | 0 | 365 |
2005 | GRESS OIL & GAS | Brine | 0 | 365 |
2006 | GRESS OIL & GAS | Brine | 0 | 365 |
2007 | GRESS OIL & GAS | Brine | 0 | 365 |
2008 | GRESS OIL & GAS | Brine | 0 | 365 |
2009 | GRESS OIL & GAS | Brine | 0 | 365 |
2010 | GRESS OIL & GAS | Brine | 0 | 365 |
2011 | GRESS OIL & GAS | Brine | 0 | 365 |
2012 | GRESS OIL & GAS | Brine | 0 | 366 |
2013 | GRESS OIL & GAS | Brine | 0 | 365 |
2014 | GRESS OIL & GAS | Brine | 0 | 365 |
2015 | GRESS OIL & GAS | Brine | 0 | 365 |
2016 | GRESS OIL & GAS | Brine | 0 | 365 |
2017 | GRESS OIL & GAS | Brine | 0 | 365 |
2018 | GRESS OIL & GAS | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0833244790 | 2018-01-19 | Production Wells | No Violations | On the day of my inspection I found that the well was equipped with a casing plunger. The flow lines were connected and the valve was open. The production equipment consisted of one 100 barrel steel tank and one horizontal separator. There was no containment dike around the equipment. Correct, legible identification was posted on the tank. The ground was snow covered, but I found no signs of leaks around the wellhead or production equipment. |
1134502865 | 2012-09-28 | Production Wells | No Violations | On the day of my inspection I found that the leak had been stopped by welding a steel containment box to the 8 well head and the tubing. The box contains escaping brine and is equipped with a release valve to dispose of fluid when full. The contaminated soil around the well head was removed and replaces with clean soil. This violation is resolved. |
1346338847 | 2012-08-29 | Production Wells | Violations Noted | On the day of my inspection I found that the well head was open flow from 2-7/8 tubing set on 8-5/8 casing with a casing hanger. The 8-5/8 casing was buried and water was bubbling from the soil around the 2-7/8 tubing. The tank battery consisted of one 100 barrel stock tank and a separator, proper ID was posted. I called Jeff Gress (740-502-2163) to report the leak. He met me at the location to dig around the well head. The water was coming from the annulus between the 2-7/8 tubing and the 8-5/8 casing. He said he will get a service rig out as soon as possible to install a proper well head to control the escape of gas and fluid from the well. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1346338847 | US-OH-110037 | 2012-08-30 | Well operation causing pollution and contamination |
For data sources see[9]