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Well ID: 34-073-22025 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hocking | |
Municipality: Green Township | |
Operator Name: HOCKING HILLS ENERGY AND WELL | |
Well Pad ID: | |
Farm/Lease Name: NUTTER LOWELL | |
License Status: Producing | |
License Date: 1977-10-27 | |
Spud Date: 1977-10-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-12-12 | |
Well Total Depth: 2850 ft | |
Configuration: Vertical | |
Latitude: 39.550243626 | |
Longitude: -82.34874958 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1977-10-20 | |
CO | 1977-10-27 | 566 GRIM PAUL A GeoDate 10/27/77 |
Completed | 1977-12-12 | |
Reached Total Depth | 1977-12-12 | |
Change of Owner | 2001-10-29 | Operator changed from 566, GRIM PAUL A to 5755, CHIEFTAIN ENERGY CORP. |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 10000 Bbl | 15000 |
For data sources see[3]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | GRIM PAUL A | Brine | 0 | 365 |
1985 | GRIM PAUL A | Brine | 365 | 365 |
1986 | GRIM PAUL A | Brine | 0 | 365 |
1987 | GRIM PAUL A | Brine | 0 | 365 |
1988 | GRIM PAUL A | Brine | 0 | 365 |
1989 | GRIM PAUL A | Brine | 0 | 365 |
1990 | GRIM PAUL A | Brine | 0 | 365 |
1991 | GRIM PAUL A | Brine | 0 | 365 |
1992 | GRIM PAUL A | Brine | 28 | 365 |
1993 | GRIM PAUL A | Brine | 44 | 365 |
1994 | GRIM PAUL A | Brine | 0 | 365 |
1995 | GRIM PAUL A | Brine | 90 | 365 |
1996 | GRIM PAUL A | Brine | 0 | 365 |
1997 | GRIM PAUL A | Brine | 56 | 365 |
1998 | GRIM PAUL A | Brine | 40 | 365 |
1999 | GRIM PAUL A | Brine | 0 | 365 |
2000 | GRIM PAUL A | Brine | 0 | 365 |
2001 | GRIM PAUL A | Brine | 70 | 365 |
2002 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2003 | HOCKING HILLS ENERGY AND WELL | Brine | 40 | 40 |
2004 | HOCKING HILLS ENERGY AND WELL | Brine | 42 | 365 |
2005 | HOCKING HILLS ENERGY AND WELL | Brine | 55 | 365 |
2006 | HOCKING HILLS ENERGY AND WELL | Brine | 62 | 365 |
2007 | HOCKING HILLS ENERGY AND WELL | Brine | 30 | 365 |
2008 | HOCKING HILLS ENERGY AND WELL | Brine | 30 | 365 |
2009 | HOCKING HILLS ENERGY AND WELL | Brine | 30 | 365 |
2010 | HOCKING HILLS ENERGY AND WELL | Brine | 24 | 0 |
2011 | HOCKING HILLS ENERGY AND WELL | Brine | 38 | 365 |
2012 | HOCKING HILLS ENERGY AND WELL | Brine | 300 | 366 |
2013 | HOCKING HILLS ENERGY AND WELL | Brine | 238 | 365 |
2014 | HOCKING HILLS ENERGY AND WELL | Brine | 322 | 365 |
2017 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0100573243 | 2006-10-18 | Production Wells | Violations Noted | A complaint was received alleging that the Parley and Lowell Nutter wells are idle. According to the owner of Chieftain Energy, Mr. Doug Kitchen, and the landowner, Mr. Lowell Nutter all seven wells are tied into each other to produce house gas. Mr. Nutter states that little gas is obtained from these wells. Mr. Kitchen admitted that a few wells need some work. Mr. Kitchen will be given credit for 1 well since some house gas is generated. The other 6 wells must be plugged or produced. Mr. Kitchen was given a verbal NOV on 10/18/2006. |
0537491107 | 2009-03-17 | Production Wells | Violations Noted | A complaint was received alleging that a flowline has leaked oil onto the ground surface, in a pasture field, located on Maysville Williams Road. An inspection of the flowline revealed that a 2 steel line from this well has leaked approximately 2 (length) x 5 (width) of oil in pasture field near a creek. At this location, the flowline contained a metal band clamp that appears to have been used to repair a previous leak. The oil does not appear to be fresh and the well is shut down. Note: Class B Wastewater from the City of Logan is applied to the pasture field. The well owner has been contacted by telephone and instructed to perform repair and cleanup. |
0568200906 | 2009-04-06 | Production Wells | No Violations | A follow-up inspection revealed that the flowline has been repaired. A new band clamp has been placed around the steel casing. Chieftain Energy has been informed that if line locations leak again, the lines would have to be replaced. |
0970623744 | 2010-10-04 | Production Wells | No Violations | FOLLOW UP TO NOV # -1339441971 FOLLOW UP TO NOV # 1288292020 The Division received a landowner complaint alleging non-production from this well. The landowner alleges that said well has not produced since, the Division last issued Notice of Violation back in 2006. An inspection revealed that the well was shut-in |
1199051089 | 2014-03-20 | Production Wells | No Violations | Compliance notice follow-up. The well is in compliance, this satisfies the compliance notice. |
1288292020 | 2010-10-04 | Production Wells | Violations Noted | The Division received a landowner complaint alleging non-production from this well. The landowner alleges that said well has not produced since, the Division last issued Notice of Violation back in 2006. An inspection revealed that the well was shut-in and contains a shared tank battery. The top of well head contains gas leak and will need to be addressed. RBDMS shows no statement of production filed since 2006. Chieftain Energy Corps. attention shall be directed to Ohio Revised Code Chapter 1509.062 (A)1, which states that for an existing well that has no reported production for two consecutive reporting periods, as reported in accordance with section 1509.11 of the Ohio Revised Code shall plug the well in accordance with section 1509.12 of the Revised Code, obtain temporary inactive well status for the well, or perform another activity approved by Chief of DMRM. From years 2003-2006, the reported production for this well showed 9, 7, 11, and 12 bbl crude oil with no gas production. The reported production is below the required 15 bbl requirement under section 1509.062 (A)2. No reported production since 2006. Failure to comply will result in further enforcement action. |
1295020632 | 2010-12-03 | Production Wells | No Violations | A follow-up inpsection revealed non-compliance. The valve for the pumping tee has now been opened and casing valve remains closed. At time of inspection, statements of production have yet to be submitted to the Division. Currently, there are no natural gas sales from this lease. Note: The landowner, Mr. Lowell Nutter, alleges that well has not been pumped since, the last time they were sent an NOV (2006). Mr. Nutter requests plugging and abandonment of well, if company will not produce the well. Note: The flowline from this well consists of approx 1.5 steel line with half partially routed above ground alongside a creek before disappearing underground to shared tank battery. Chieftain Energy unsure of location underground before tie-in to battery. |
1339441971 | 2010-10-04 | Production Wells | No Violations | FOLLOW UP TO NOV # 1288292020 The Division received a landowner complaint alleging non-production from this well. The landowner alleges that said well has not produced since, the Division last issued Notice of Violation back in 2006. An inspection revealed that the well was shut-in |
1347024715 | 2012-09-05 | Production Wells | No Violations | Well was in operation at the time of inspection. There was no pollution and contamination. Good identification was observed. Well in compliance. |
1447850905 | 2006-12-26 | Production Wells | No Violations | A follow-up inspection revealed that the previously noted violation has been resolved. Mr. Doug Kitchen and Mr. Ron McBride stated that they replaced the piston rings and performed work on the cylinders. The well was observed pumping for 15 minutes. The company stated that the well exhibited no problems and has been running for 45 minutes. |
1449106744 | 2009-03-18 | Production Wells | No Violations | A follow-up inspection revealed that the oily soil has been removed and peat sorb applied to this location. The well remains shut down and the flowline will still need to be repaired. |
1508552963 | 2010-10-04 | Production Wells | No Violations | FOLLOW UP TO NOV # 1288292020 The Division received a landowner complaint alleging non-production from this well. The landowner alleges that said well has not produced since, the Division last issued Notice of Violation back in 2006. An inspection revealed that the well was shut-in and contains a shared tank battery. The top of well head contains gas leak and will need to be addressed. RBDMS shows no statement of production filed since 2006. Chieftain Energy Corps. attention shall be directed to Ohio Revised Code Chapter 1509.062 (A)1, which states that for an existing well that has no reported production for two consecutive reporting periods, as reported in accordance with section 1509.11 of the Ohio Revised Code shall plug the well in accordance with section 1509.12 of the Revised Code, obtain temporary inactive well status for the well, or perform another activity approved by Chief of DMRM. From years 2003-2006, the reported production for this well showed 9, 7, 11, and 12 bbl crude oil with no gas production. The reported production is below the required 15 bbl requirement under section 1509.062 (A)2. No reported production since 2006. Failure to comply will result in further enforcement action. |
2071214106 | 2006-12-22 | Production Wells | No Violations | A follow-up inspection was conducted on 12/22/2006. During the inspection, it was noted that service work would need to be performed on this well. The company was unable to keep the well running, due to a compression problem. Mr. Kitchen was instructed to have this well running the morning of 12/26/2006, or this case would be handed over to management. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0100573243 | US-OH-100373 | 2006-10-23 | Well shall be plugged | |
0537491107 | US-OH-125880 | 2009-04-13 | Inadequate pipeline strength | |
0537491107 | US-OH-125881 | 2009-04-13 | Well operation causing pollution and contamination | |
1288292020 | US-OH-108137 | 2010-10-29 | Well shall be plugged | |
1288292020 | US-OH-108138 | 2010-11-01 | Temporary inactive; failure to properly shut-in or maintain the well or associated equipment | |
1288292020 | US-OH-108139 | 2010-10-29 | Statement of annual production not filed |
For data sources see[8]