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34-127-23376

Well Details

Well ID: 34-127-23376
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Country: United States
State: Ohio
County: Perry
Municipality: Reading Township
Operator Name: ALNA ENERGY LLC
Well Pad ID:
Farm/Lease Name: MILLER FLORENCE
License Status: Producing
License Date: 1973-11-05
Spud Date: 1973-11-19
Spud Drilling Contractor:
Final Drill Date: 1973-12-31
Well Total Depth: 3236 ft
Configuration: Vertical
Latitude: 39.754598599
Longitude: -82.28524550

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1973-11-05 137 ALTHEIRS OIL INC GeoDate 11/5/73
Original Spud 1973-11-19
Completed 1973-12-31
Reached Total Depth 1973-12-31
Change of Owner 2002-02-12 Operator changed from 137, ALTHEIRS OIL INC to 1429, ALTIER BROTHERS INC
Change of Owner 2008-11-18 Operator changed from 1429, ALTIER BROTHERS INC to 8240, BAUER JOHN S
Record Last Modified 2013-10-03

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 4500 Bbl 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ALTHEIRS OIL INC 0 307 365
1985 ALTHEIRS OIL INC 0 360 260
1986 ALTHEIRS OIL INC 0 242 365
1987 ALTHEIRS OIL INC 0 300 365
1988 NOBLE OIL CORP 0 157 365
1989 ALTHEIRS OIL INC 0 158 0
1990 ALTHEIRS OIL INC 0 384 365
1991 ALTHEIRS OIL INC 0 229 365
1992 ALTHEIRS OIL INC 0 310 365
1993 ALTHEIRS OIL INC 0 309 365
2008 ALNA ENERGY LLC 0 222 156
2009 ALNA ENERGY LLC 0 157 156
2010 ALNA ENERGY LLC 0 142 300
2011 ALNA ENERGY LLC 0 60 0
2012 ALNA ENERGY LLC 0 79 52
2013 ALNA ENERGY LLC 0 79 52
2014 ALNA ENERGY LLC 0 148 160
2015 ALNA ENERGY LLC 0 56 160
2016 ALNA ENERGY LLC 0 64 160
2017 ALNA ENERGY LLC 0 0 160

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ALTHEIRS OIL INC Brine 0 365
1985 ALTHEIRS OIL INC Brine 0 260
1986 ALTHEIRS OIL INC Brine 0 365
1987 ALTHEIRS OIL INC Brine 0 365
1988 NOBLE OIL CORP Brine 0 365
1989 ALTHEIRS OIL INC Brine 0 0
1990 ALTHEIRS OIL INC Brine 0 365
1991 ALTHEIRS OIL INC Brine 0 365
1992 ALTHEIRS OIL INC Brine 0 365
1993 ALTHEIRS OIL INC Brine 0 365
2008 ALNA ENERGY LLC Brine 420 156
2009 ALNA ENERGY LLC Brine 840 156
2010 ALNA ENERGY LLC Brine 0 300
2011 ALNA ENERGY LLC Brine 210
2012 ALNA ENERGY LLC Brine 540 52
2013 ALNA ENERGY LLC Brine 130 52
2014 ALNA ENERGY LLC Brine 420 160
2015 ALNA ENERGY LLC Brine 210 160
2016 ALNA ENERGY LLC Brine 210 160
2017 ALNA ENERGY LLC Brine 140 160

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1788982986 2018-07-20 Production Wells Violations Noted I was on location today to do a field inspection on this well. During my inspection I found the salt water tank has leaked inside of the dike. I contacted the company to let them know about it. They will have a track hoe on location tomorrow to remove the tank and clean up the contamination. I will check back next week on the progress.
1887229419 2018-12-04 Production Wells No Violations I was back on location today to do a follow-up inspection on this well. The company has conducted the clean-up at the tank pad. The well is no longer in violation.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1788982986 US-OH-117830 2018-12-18 9-1-07 Well operation causing pollution and contamination

For data sources see[8]

References