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Well ID: 34-127-23376 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Reading Township | |
Operator Name: ALNA ENERGY LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLER FLORENCE | |
License Status: Producing | |
License Date: 1973-11-05 | |
Spud Date: 1973-11-19 | |
Spud Drilling Contractor: | |
Final Drill Date: 1973-12-31 | |
Well Total Depth: 3236 ft | |
Configuration: Vertical | |
Latitude: 39.754598599 | |
Longitude: -82.28524550 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1973-11-05 | 137 ALTHEIRS OIL INC GeoDate 11/5/73 |
Original Spud | 1973-11-19 | |
Completed | 1973-12-31 | |
Reached Total Depth | 1973-12-31 | |
Change of Owner | 2002-02-12 | Operator changed from 137, ALTHEIRS OIL INC to 1429, ALTIER BROTHERS INC |
Change of Owner | 2008-11-18 | Operator changed from 1429, ALTIER BROTHERS INC to 8240, BAUER JOHN S |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 4500 Bbl | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ALTHEIRS OIL INC | 0 | 307 | 365 |
1985 | ALTHEIRS OIL INC | 0 | 360 | 260 |
1986 | ALTHEIRS OIL INC | 0 | 242 | 365 |
1987 | ALTHEIRS OIL INC | 0 | 300 | 365 |
1988 | NOBLE OIL CORP | 0 | 157 | 365 |
1989 | ALTHEIRS OIL INC | 0 | 158 | 0 |
1990 | ALTHEIRS OIL INC | 0 | 384 | 365 |
1991 | ALTHEIRS OIL INC | 0 | 229 | 365 |
1992 | ALTHEIRS OIL INC | 0 | 310 | 365 |
1993 | ALTHEIRS OIL INC | 0 | 309 | 365 |
2008 | ALNA ENERGY LLC | 0 | 222 | 156 |
2009 | ALNA ENERGY LLC | 0 | 157 | 156 |
2010 | ALNA ENERGY LLC | 0 | 142 | 300 |
2011 | ALNA ENERGY LLC | 0 | 60 | 0 |
2012 | ALNA ENERGY LLC | 0 | 79 | 52 |
2013 | ALNA ENERGY LLC | 0 | 79 | 52 |
2014 | ALNA ENERGY LLC | 0 | 148 | 160 |
2015 | ALNA ENERGY LLC | 0 | 56 | 160 |
2016 | ALNA ENERGY LLC | 0 | 64 | 160 |
2017 | ALNA ENERGY LLC | 0 | 0 | 160 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1985 | ALTHEIRS OIL INC | Brine | 0 | 260 |
1986 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1987 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1988 | NOBLE OIL CORP | Brine | 0 | 365 |
1989 | ALTHEIRS OIL INC | Brine | 0 | 0 |
1990 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1991 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1992 | ALTHEIRS OIL INC | Brine | 0 | 365 |
1993 | ALTHEIRS OIL INC | Brine | 0 | 365 |
2008 | ALNA ENERGY LLC | Brine | 420 | 156 |
2009 | ALNA ENERGY LLC | Brine | 840 | 156 |
2010 | ALNA ENERGY LLC | Brine | 0 | 300 |
2011 | ALNA ENERGY LLC | Brine | 210 | |
2012 | ALNA ENERGY LLC | Brine | 540 | 52 |
2013 | ALNA ENERGY LLC | Brine | 130 | 52 |
2014 | ALNA ENERGY LLC | Brine | 420 | 160 |
2015 | ALNA ENERGY LLC | Brine | 210 | 160 |
2016 | ALNA ENERGY LLC | Brine | 210 | 160 |
2017 | ALNA ENERGY LLC | Brine | 140 | 160 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1788982986 | 2018-07-20 | Production Wells | Violations Noted | I was on location today to do a field inspection on this well. During my inspection I found the salt water tank has leaked inside of the dike. I contacted the company to let them know about it. They will have a track hoe on location tomorrow to remove the tank and clean up the contamination. I will check back next week on the progress. |
1887229419 | 2018-12-04 | Production Wells | No Violations | I was back on location today to do a follow-up inspection on this well. The company has conducted the clean-up at the tank pad. The well is no longer in violation. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1788982986 | US-OH-117830 | 2018-12-18 | 9-1-07 | Well operation causing pollution and contamination |
For data sources see[8]