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Well ID: 34-013-21242 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Mead Township | |
Operator Name: GULFPORT ENERGY CORPORATION | |
Well Pad ID: US-OH-001470 | |
Farm/Lease Name: TIGER 210475 | |
License Status: Producing | |
License Date: 2017-05-05 | |
Spud Date: 2017-05-21 | |
Spud Drilling Contractor: PIONEER DRILLING | |
Final Drill Date: 2017-06-20 | |
Well Total Depth: 18337 ft | |
Configuration: Horizontal | |
Latitude: 39.928434537 | |
Longitude: -80.84029547 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2017-05-05 | Proposed Formations:UTICA/POINT PLEASANT, Issued Date:5/5/2017, Expired Date:5/5/2019 12:00:00 PM, Drilling unit acres:547.771, Proposed Well Type:OG, Proposed Well Class:EOUT |
Reached Total Depth | 2017-06-20 | STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018 |
Correction to Well | 2018-03-09 | UPDATE TARGET/TAKE PER AS-DRILLED PLAT |
Completion Report Received | 2018-07-02 | STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018 |
Record Last Modified | 2018-07-11 | STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018 |
Construction Permit Expires | 2019-05-05 | STATUS PER OPERATOR TELEPHONE CONVERSATION ALE 03/12/2018 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2018-07-10 | 10701 | 10845 | 50 |
2018-07-10 | 18070 | 18172 | 30 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 01/07/2018 | 02/13/2018 | 10544 | 14,844,400.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Plexslick 920 | Chemplex | Friction Reducer | Petroleum Distillate | 64742-47-8 | 20 | 0.0105044 | 14657.5 |
Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00105044 | 1465.75 | ||||
Ammonium Chloride | 12125-02-9 | 1 | 0.00052522 | 732.875 | ||||
Water | 7732-18-5 | 45 | 0.0236349 | 32979.4 | ||||
Copolymer of 2-propenamide | 69418-26-4 | 30 | 0.0157566 | 21986.2 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00105044 | 1465.75 | ||||
Sand (Silca) | Muskie | Proppant | Silica Substrate | 14808-60-7 | 100 | 10.8823 | 15,184,800.0 | |
Hostastim TCA6038 | Clariant | Corrosion Inhibitor/Iron Control | Methanol | 67-56-1 | 70 | 0.000354379 | 494.489 | |
4-Nonylphenol, branched, ethoxylated | 127087-87-0 | 10 | 0.00005063 | 70.641 | ||||
Pyridinium, 1-(phenylmethyl)-,
ethyl methy derivatives, chlorides |
68909-18-2 | 30 | 0.000151877 | 211.924 | ||||
2-Ethylhexanol | 104-76-7 | 10 | 0.00005063 | 70.641 | ||||
NEFE-180 | Chemplex | Corrosion Inhibitor/Iron Control | Methanol | 67-56-1 | 35 | 0.000201008 | 280.48 | |
Acetic acid | 64-19-7 | 65 | 0.0003733 | 520.891 | ||||
Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00002872 | 40.069 | ||||
Olefin | Proprietary | 5 | 0.00002872 | 40.069 | ||||
2-Ethylhexanol | 104-76-7 | 10 | 0.00005743 | 80.137 | ||||
Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00002872 | 40.069 | ||||
2-Propyn-1-ol | 107-19-7 | 5 | 0.00002872 | 40.069 | ||||
Fatty acids, tall oil | 61790-12-3 | 5 | 0.00002872 | 40.069 | ||||
Other Chemical(s) | Listed Above | See Trade Name(s) List | Water | 7732-18-5 | 45 | 0.0236349 | 32979.4 | |
Quaternary Ammonium chloride | 68424-85-1 | 3 | 0.00104377 | 1456.44 | ||||
Hydrochloric Acid | 7647-01-0 | 3 | 0.000214051 | 298.68 | ||||
Petroleum Distillate | 64742-47-8 | 20 | 0.0105044 | 14657.5 | ||||
Methanol | 67-56-1 | 1 | 0.00007135 | 99.56 | ||||
2-Propyn-1-ol | 107-19-7 | 5 | 0.00002872 | 40.069 | ||||
2-Ethylhexanol | 104-76-7 | 10 | 0.00005743 | 80.137 | ||||
Fatty acids, tall oil | 61790-12-3 | 5 | 0.00002872 | 40.069 | ||||
Oleic Acid Diethanolamide | 93-83-4 | 2 | 0.00105044 | 1465.75 | ||||
Olefin | Proprietary | 5 | 0.00002872 | 40.069 | ||||
Ammonium Chloride | 12125-02-9 | 1 | 0.00052522 | 732.875 | ||||
Methanol | 67-56-1 | 35 | 0.000201008 | 280.48 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 2 | 0.00105044 | 1465.75 | ||||
4-Nonylphenol, branched, ethoxylated | 127087-87-0 | 10 | 0.00005063 | 70.641 | ||||
2-Ethylhexanol | 104-76-7 | 10 | 0.00005063 | 70.641 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 1.5 | 0.000321655 | 448.827 | ||||
Water | 7732-18-5 | 74 | 0.0257462 | 35925.4 | ||||
Water | 7732-18-5 | 60 | 0.0128662 | 17953.1 | ||||
Alcohols, C14-15, ethoxylated | 68951-67-7 | 5 | 0.00002872 | 40.069 | ||||
Coconut oil acid diethanolamine | 68603-42-9 | 5 | 0.00002872 | 40.069 | ||||
Ammonium Chloride | 12125-02-9 | 2 | 0.000428874 | 598.437 | ||||
Pyridinium, 1-(phenylmethyl)-,
ethyl methy derivatives, chlorides |
68909-18-2 | 30 | 0.000151877 | 211.924 | ||||
Didecyl dimethyl Ammonium Chloride | 7173-51-5 | 3 | 0.00104377 | 1456.44 | ||||
Water | 7732-18-5 | 80 | 0.0203518 | 28398.2 | ||||
Oleic Acid Diethanolamide | 93-83-4 | 1.5 | 0.000321655 | 448.827 | ||||
Hydrochloric Acid (28%) | Oxy | Acidizing | Hydrochloric Acid (Hydrogen Chloride) | 7647-01-0 | 28 | 0.0539112 | 75226 | |
Water | Gulfport Energy | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 88.7767 | 123,876,000.0 | |
Biotreat 15588 | Clariant | Biocide | Quaternary Ammonium chloride | 68424-85-1 | 3 | 0.00104377 | 1456.44 | |
Didecyl dimethyl Ammonium Chloride | 7173-51-5 | 3 | 0.00104377 | 1456.44 | ||||
Glutaraldehyde | 111-30-8 | 20 | 0.00695843 | 9709.57 | ||||
Water | 7732-18-5 | 74 | 0.0257462 | 35925.4 | ||||
Plexslick 957 | Chemplex | Friction Reducer | Water | 7732-18-5 | 60 | 0.0128662 | 17953.1 | |
Ammonium Chloride | 12125-02-9 | 2 | 0.000428874 | 598.437 | ||||
Oleic Acid Diethanolamide | 93-83-4 | 1.5 | 0.000321655 | 448.827 | ||||
Petroleum Distillate | 64742-47-8 | 20 | 0.00428874 | 5984.37 | ||||
Alcohols, C12-16, Ethoxylated | 68551-12-2 | 1.5 | 0.000321655 | 448.827 | ||||
Flotreat 15502 | Clariant | Friction Reducer | Proprietary | Proprietary | 20 | 0.00508795 | 7099.56 | |
Water | 7732-18-5 | 80 | 0.0203518 | 28398.2 | ||||
Scaletreat 30 | Clariant | Scale inhibitor | Sodium polyacrylate | 9003-04-7 | 20 | 0.001212 | 1691.18 | |
SC-82 | Clariant | Scale inhibitor | Hydrochloric Acid | 7647-01-0 | 3 | 0.000214051 | 298.68 | |
Sodium polyphosphonate | proprietary | 1 | 0.00007135 | 99.56 | ||||
Methanol | 67-56-1 | 1 | 0.00007135 | 99.56 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2018-01-07 | H2O | 15 | 8975 Bbl | 375510 | STINGRAY PRESSURE PUMPING LLC | STAGE 1/42
STAGES 2-41 SEE IMAGES |
2018-02-13 | H2O | 15 | 7091 Bbl | 380580 | STINGRAY PRESSURE PUMPING LLC | STAGE 42/42
STAGES 2-41 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | GULFPORT ENERGY CORPORATION | 3762627 | 0 | 245 |
2019 | GULFPORT ENERGY CORPORATION | 658387 | 0 | 89 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2018 | GULFPORT ENERGY CORPORATION | Brine | 32843 | 245 |
2019 | GULFPORT ENERGY CORPORATION | Brine | 4570 | 89 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0532557564 | 2017-06-21 | Drill / Deepen / Reopen | No Violations | During this inspection Pioneer Rig 71 had reached the total depth of the 8.5 inch diameter open hole section of the well bore. Cementing of the 5.5 inch diameter casing had commenced. Once the cementing process is completed the company will skid and begin drilling the next well on this pad |
1496666296 | 2017-06-05 | Casing String Witnessed | No Violations | On site inspection to witness the mine string surface combination cement job with Pioneer Drilling rig 71 and O-Tex Cement Service along with Inspector Andrew Corder. The rig has drilled a 24 diameter surface borehole to a measured depth of 610 off of a drilling rig Kelly Bushing height of 28.6. The rig installed 608 of 18.625 diameter 87.5 pound per foot J-55 grade buttress thread casing with a casing guide shoe and float collar ran and a World Oil Tool swell packer set at 461, 4 casing centralizers and 2 cement baskets were also installed in the string. O-Tex cement service cemented the casing in 2 stages with the bottom section cemented with 43.5 barrel cement mix consisting of 202 sacks of class H cement with the cement weight verified at 15.6 pound per gallon by weight of scale and the cement displaced to the float collar with 173 barrels of fresh water, upon the landing of the plug at 170 psi pressure was increased in increments up to 560 psi and the casing was pressure tested at that point. The swell packer element was designed to set at 450 psi. The rig then proceeded to run 1 diameter tubing down the back side of the 18.625 casing to a depth of 438, the annular space was then topped off with 151 barrels of class H cement with 25 barrels of cement returns witnessed to surface. |
1558446188 | 2017-06-07 | Casing String Witnessed | No Violations | During this inspection Pioneer Rig 71 had completed running the 13.375 inch diameter casing string and anticipate to cement the same when cementers show up on location. I spoke with Inspector Bill Stolarik and he informed me that Inspector Austin Gutridge would be covering this cementing job. See his report for execution of this cement job. |
1823367444 | 2017-06-05 | Casing String Witnessed | No Violations | Onsite inspection conducted accompanied by Inspector Bill Stolarik. Pioneer Rig 71 had reached the total depth of the 24 inch diameter open hole section of this well bore at a depth of 608 feet. The 18.625 inch diameter casing was ran to total depth. O-Tex Cementing Services ran 43.5 barrels of Class H cement to stabilize the bottom of the casing. The inflatable packer element was then expanded by pressure to allow the top off job to ensue. O-Tex then pumped 151 barrels of Class H cement through 1 inch diameter tubing to established cement circulation to surface. |
2099297909 | 2018-11-14 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspection found the area affected by the well pad construction meets ORC 1509.072 with vegetation established and erosion control in place. All erosion control filter sock material placed on the outward slopes during construction have been removed. The well pad and lease road are stone construction and in good repair. Signage is posted at the lease road entry point and at each well head with hazard warning labels on the tank battery. Emergency shut down devices and fire extinguishers are situated at each critical area of the well pad. There is a 3rd party mid stream operation along the lease road on the left side entering the well pad. The lease road does have a gate to restrict access. A total of 6 wells are present on the pad with the said well equipped with an A&B section well head along with a tubing head production tree. 2 diameter riser pipes with valves and gauges are present and attached to the well head A&B sections for the purpose of annular pressure monitoring. The A section gauge which is monitoring the 13.375 casing pressure reads 600 pounds per square inch pressure (psi) the B section gauge which monitors the 9.625 diameter casing pressure reads 1,100 pounds pressure. The 5.5 diameter casing pressure is 2,000 pounds pressure and the tubing head pressure before the choke valve is 1,000 pounds pressure. The production tubing well head valves are open to the sales line and an emergency shut down device is situated on the production well head tree. There are (6) gas processing units present on location and on the rear left hand corner of the well pad is the production fluid facility that consists of (4) steel construction 400 barrel fluid volume tanks along with a 50 barrel steel tank. All situated inside a polymer lined steel containment dike area. |
For data sources see[10]