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Well ID: 34-119-23483 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Brush Creek Township | |
Operator Name: NGO DEVELOPMENT CORP. | |
Well Pad ID: | |
Farm/Lease Name: MARTIN FARMS | |
License Status: Final Restoration | |
License Date: 2013-10-29 | |
Spud Date: 1974-08-14 | |
Spud Drilling Contractor: | |
Final Drill Date: 1974-10-07 | |
Well Total Depth: 4061 ft | |
Configuration: Vertical | |
Latitude: 39.799312765 | |
Longitude: -81.99636392 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1974-08-14 | |
Completed | 1974-10-07 | |
Reached Total Depth | 1974-10-07 | |
CO | 1980-06-23 | 627 KENOIL GeoDate 6/23/80 |
CO | 1996-03-27 | 98 NGO DEVELOPMENT CORP. GeoDate 6/23/80 |
APP | 2013-10-29 | Proposed Formations:CLINTON, Issued Date:10/29/2013, Expired Date:10/29/2015 12:00:00 PM, Drilling unit acres:42, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-04-11 | |
Construction Permit Expires | 2015-10-29 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 4025 Bbl | 5000 | 36BPM, 850 PSI |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KENOIL LLC | 0 | 129 | 0 |
1985 | KENOIL LLC | 0 | 124 | 0 |
1986 | KENOIL LLC | 0 | 95 | 365 |
1987 | KENOIL LLC | 0 | 76 | 365 |
1988 | KENOIL LLC | 0 | 89 | 365 |
1989 | KENOIL LLC | 0 | 91 | 365 |
2008 | NGO DEVELOPMENT CORP. | 0 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | KENOIL LLC | Brine | 0 | 0 |
1985 | KENOIL LLC | Brine | 269 | 0 |
1986 | KENOIL LLC | Brine | 181 | 365 |
1987 | KENOIL LLC | Brine | 158 | 365 |
1988 | KENOIL LLC | Brine | 212 | 365 |
1989 | KENOIL LLC | Brine | 184 | 365 |
2008 | NGO DEVELOPMENT CORP. | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0557507330 | 2013-04-23 | Production Wells | No Violations | I met Greg Mason and Dean Limbacher of NGO and the Landowners. NGO will apply for plugging permit and plug in the Fall after crops are done. |
0626222408 | 2015-06-03 | Final Restoration | No Violations | Final Restoration passed on 6-3-15 by Patrick Shreve. Well was plugged in compliance OAC 1501-9-11. The land was restored back under ORC 1509.072. |
0627813546 | 2014-04-11 | Plug / Plug Back | No Violations | Well was plugged back to surface. Compliance Notice is resolved on 4-11-14 by Patrick Shreve. |
0937451024 | 2007-02-06 | Production Wells | No Violations | Leaked fixed. |
1187720739 | 2007-01-26 | Production Wells | No Violations | Pumping. Heater-treater leaking where 2 goes in to it. Called Greg Mason and we was to send someone out. Told him to get better ID on tank, too. |
1244185784 | 2014-04-10 | Plug / Plug Back | No Violations | R&B Drilling has the service rig over well plugging for NGO. The 1.5tubing was pulled and ran in to depth of 2990. The plug was set in 3.5casing. The plug ran from 2990-2590 and Cemenco ran 20 sacks of class A cement. The rig then pulled all the 1.5tubing. Then company started welding up the riser pipe and getting a control device for the well. Appalachain Wireline shot casing off with a collar buster at 2005. Then rig started pulling the 3.5casing. |
1365773642 | 2013-04-01 | Production Wells | No Violations | Well is producing well with a Pumping unit and 3.5x1.5well head,1.5tubing. The rod annulus is open and the tubing annulus is closed. No production has been filed since 1989. I will get with Greg Mason on well to find out the production problem. |
1399341769 | 2014-04-11 | Plug / Plug Back | No Violations | R&B Drilling is running 1.5 tubing in to plug well. Cemenco is setting cement plugs. Set lime plug at 1990-1790. Set 44 sacks of Class A cement at 4%gel. Berea plug was set at 743-582. Ran 36 sacks at 4%gel. Bottom of 8.625 plug is at 515-315 and ran 45 sacks of Class A cement@ 4% gel. 300-0 ran 80 sacks of Class A cement. Circulation was established. |
1991366315 | 2007-01-26 | Production Wells | No Violations | 2 leaking where it comes into separator. Called NGO and they will take care of problem. What little is leaking is inside dike. |
For data sources see[8]