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Well ID: 37-059-01570 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Greene | |
Municipality: Richhill Township | |
Operator Name: LEATHERWOOD INC | |
Well Pad ID: | |
Farm/Lease Name: F. P. HEADLEY 1 | |
License Status: Plugged and Abandoned | |
Spud Date: | |
Permit Date: | |
Well Type: OIL | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 39.889181 | |
Longitude: -80.415994 |
Date | Event |
---|---|
1902-11-13 | Drilling Completion |
1903-01-01 | Old Well |
2015-10-21 | Begin Plugging |
2015-11-16 | Finished Plugging |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1991 | GREENRIDGE OIL CO INC | 0.00 | 0 | 204.00 | 365 | 0.00 | 0 |
1997 | MTN ENERGY | 0.00 | 0 | 204 | 365 | 0.00 | 0 |
1998 | MTN ENERGY | 0.00 | 0 | 188 | 365 | 0.00 | 0 |
1999 | MTN ENERGY | 0.00 | 0 | 224 | 365 | 0.00 | 0 |
2001 | MTN ENERGY | 0.00 | 0 | 156 | 365 | 0.00 | 0 |
2002 | MTN ENERGY | 0.00 | 0 | 148 | 365 | 0.00 | 0 |
2003 | MTN ENERGY | 0.00 | 0 | 167 | 365 | 0.00 | 0 |
2004 | MTN ENERGY | 0.00 | 0 | 155 | 365 | 0.00 | 0 |
2005 | LEATHERWOOD INC | 0.00 | 0 | 85 | 214 | 0.00 | 0 |
2006 | LEATHERWOOD INC | 0.00 | 0 | 350.00 | 365 | 0.00 | 0 |
2007 | LEATHERWOOD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2008 | LEATHERWOOD INC | 265.00 | 156 | 0.00 | 0 | 0.00 | 0 |
2009 | LEATHERWOOD INC | 0.00 | 0 | 257.00 | 156 | 0.00 | 0 |
2010 | LEATHERWOOD INC | 0.00 | 0 | 231.00 | 156 | 0.00 | 0 |
2011 | LEATHERWOOD INC | 0.00 | 0 | 172.00 | 156 | 0.00 | 0 |
2012 | LEATHERWOOD INC | 0.00 | 0 | 133.00 | 156 | 0.00 | 0 |
2013 | LEATHERWOOD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | LEATHERWOOD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | LEATHERWOOD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2432710 | Primary Facility | 2015-11-05 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Coastal Rig #214. Pulled 2,990’ of sucker rods. Pulled 3,012’ of tubing. Pulled 2,354’ of 5 ½” casing. Cement plug set from 3,015’ to 2,000’. Currently pulling 7” casing. Conduct site inspection. Notify operator of erosion and sedimentation control plan deficiencies. |
2465337 | Primary Facility | 2016-02-11 | Routine/Complete Inspection | Violation(s) Noted | On 2/11/2016, I performed an inspection of the CNX FP Headley #1 well plugging site with Joel Keller (DEP/OGI) and Joe Laslo (DEP/SMCI). Present at time of inspection was Doug Dinger (Consol). The site is located in Richhill Twp., Greene County. The inspection was performed as a site inspection after a reported sheen in an unnamed trib. to Pollen Run.
Consol Bailey Mine personnel informed the DEP that an oil sheen was documented in an unnamed trib. to Polen Run during stream monitoring associated with mining of the Bailey 2L longwall panel. At time of inspection a noted weathered brown hydrocarbon material was observed in the unnamed trib. to Polen Run down gradient from the recently plugged FP Headley #1 well site (plugged 11/16/15). |
2466352 | Primary Facility | 2016-03-01 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On 3/1/2016, I performed an inspection of the CNX FP Headley #1 well plugging site with Joel Keller (DEP/OGI). The site is located in Richhill Twp., Greene County. The inspection was performed as a follow up inspection after a reported sheen in an unnamed trib. to Pollen Run.
Consol Bailey Mine personnel informed the DEP that an oil sheen was documented in an unnamed trib. to Polen Run during stream monitoring associated with mining of the Bailey 2L longwall panel. At time of inspection a noted weathered brown hydrocarbon material was observed in the unnamed trib. to Polen Run down gradient from the recently plugged FP Headley #1 well site (plugged 11/16/15). The booms placed by Consol in the stream channel remain. The seep of hydrocarbon from beneath a rock ledge near the headwaters of the unnamed trib. to Polen Run persists. |
2498190 | Primary Facility | 2016-06-14 | Compliance Evaluation | No Violations Noted | On 6/14/2016, I performed an inspection of the CNX FP Headley #1 well plugging site. The site is located in Richhill Twp., Greene County. The inspection was performed as a compliance evaluation inspection after a reported sheen in an unnamed trib. to Pollen Run.
Consol Bailey Mine personnel informed the DEP that an oil sheen was documented in an unnamed trib. to Polen Run during stream monitoring associated with mining of the Bailey 2L longwall panel. At time of inspection a noted weathered brown hydrocarbon material was observed in the unnamed trib. to Polen Run down gradient from the recently plugged FP Headley #1 well site (plugged 11/16/15). The booms placed by Consol in the stream channel have been removed. The seep of hydrocarbon from beneath a rock ledge near the headwaters of the unnamed trib. to Polen Run has stopped, due to the flow from the seep has stopped. No sheen was noted in the stream channel at time of inspection. Flow in the stream channel has decreased with the mining of the 2L lon |
536648 | Primary Facility | 1988-04-26 | Routine/Complete Inspection | No Violations Noted | E&S OK |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2465337 | 754467 | 2016-02-11 | 2016-07-22 | 78.54 | Environmental Health & Safety | |
2465337 | 754469 | 2016-02-11 | 2016-07-22 | CSL 401 | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
754467 | 340842 | NOV - Notice of Violation | 2016-09-09 | ||||
754469 | 340842 | NOV - Notice of Violation | 2016-09-09 |
For data sources see[6]