X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-063-25488

Well Details

Well ID: 37-063-25488
Loading map...
Country: United States
State: Pennsylvania
County: Indiana
Municipality: Grant Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: HELEN DAUGHERTY 1
License Status: ACTIVE
Spud Date: 1980-05-09
Permit Date: 1980-04-29
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.751196
Longitude: -78.927043

For data sources see[1][2][3]

Well History

Date Event
1980-04-29 New Permit Application
1980-05-09 Performed Spud Operation
1980-05-13 Drilling Completion
1980-05-27 Perforation
1980-08-11 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 PHILLIPS PROD CO 1390.00 198 0.00 0 0.00 0
1993 PHILLIPS PROD CO 1524.00 140 0.00 0 0.00 0
1994 PHILLIPS PROD CO 1517.00 202 0.00 0 0.00 0
1995 PHILLIPS PROD CO 2165.00 273 0.00 0 0.00 0
1996 PHILLIPS PROD CO 1377 365 0.00 0 0.00 0
1997 PHILLIPS PROD CO 1519 279 0.00 0 0.00 0
1998 PHILLIPS PROD CO 1695 318 0.00 0 0.00 0
1999 PHILLIPS PROD CO 1192 299 0.00 0 0.00 0
2000 PHILLIPS PROD CO 1376 329 0.00 0 0.00 0
2001 PHILLIPS PROD CO 1195 292 0.00 0 0.00 0
2002 PHILLIPS PROD CO 1201 246 0.00 0 0.00 0
2003 PHILLIPS PROD CO 1096 364 0 364 0.00 0
2004 PHILLIPS PROD CO 1257 360 0.00 0 0.00 0
2005 PHILLIPS PROD CO 1310 357 0.00 0 0.00 0
2006 PHILLIPS PROD CO 1,009.00 365 0.00 0 0.00 0
2007 PHILLIPS PROD CO 997.00 365 0.00 0 0.00 0
2008 PHILLIPS PROD CO 586.00 277 0.00 0 0.00 0
2009 PHILLIPS PROD CO 546.00 333 0.00 0 0.00 0
2010 PHILLIPS PROD CO 267.00 361 0.00 0 0.00 0
2011 PHILLIPS PROD CO 454.00 268 0.00 0 0.00 0
2012 XTO ENERGY INC 644.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 610.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 514.00 299 0.00 0 0.00 0
2015 XTO ENERGY INC 556.36 365 0.00 0 0.00 0
2016 XTO ENERGY INC 523.00 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 387.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 454.00 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1994 PHILLIPS PROD CO Brine 164.00 Bbl
1995 PHILLIPS PROD CO Brine 154.00 Bbl
1996 PHILLIPS PROD CO Brine 70.00 Bbl Treated On-Site, NPDES Discharge
1997 PHILLIPS PROD CO Brine 180.00 Bbl Brine or Industrial Waste Treatment Plt GROUP
1998 PHILLIPS PROD CO Brine 151.00 Bbl Brine or Industrial Waste Treatment Plt 033-WAST2
1999 PHILLIPS PROD CO Brine 70.00 Bbl Brine or Industrial Waste Treatment Plt SEE END
2000 PHILLIPS PROD CO Brine 80.00 Bbl Brine or Industrial Waste Treatment Plt SEE END
2001 PHILLIPS PROD CO Brine 70.00 Bbl Brine or Industrial Waste Treatment Plt
2002 PHILLIPS PROD CO Brine 80.00 Bbl Brine or Industrial Waste Treatment Plt
2003 PHILLIPS PROD CO Brine 65.00 Bbl Brine or Industrial Waste Treatment Plt
2004 PHILLIPS PROD CO Brine 30.00 Bbl Brine or Industrial Waste Treatment Plt
2005 PHILLIPS PROD CO Brine 160.00 Bbl Brine or Industrial Waste Treatment Plt PA0095273
2006 PHILLIPS PROD CO Brine 80.00 Bbl Brine or Industrial Waste Treatment Plt PA0095443
2015 XTO ENERGY INC Produced Fluid 47 Bbl CENT WASTE TRT FAC NPDES PA0095273
2015 XTO ENERGY INC Produced Fluid 47.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2213631 Primary Facility 2013-10-15 Administrative/File Review In Compliance with Policy On-site meeting as requested by XTO representative Dan Rice to discuss maintenance/replacement of access road galvanized culvert; AR is shared by landowner.
2283439 Primary Facility 2014-06-25 Routine/Partial Inspection In Compliance with Policy On-site inspt to monitor replacement and installation of twin culverts as original culvert became structurally compromised, thereby restricting water flow.Dept notified of culvert failure on 6/20. Opr submitted an emergency permit application on 6/20 which the Dept subsequently approved.Culvert shared by homeowner and Opr.General permit previously not issued to Opr and/or homeowner as culvert was installed prior to GP regulatory requirements.At time of inspt, replacement culverts on-site, not yet installed.Compromised culvert previously removed with temporary wooden bridge in place.E&S BMPs not yet installed.While on-site, Dept contacted Opr rep Dan Rice via phone to inquire about timeline for the culvert installations.Mr. Rice stated that Opr was waiting for the delivery of the second culvert, in which Dept confirmed that second culvert is now on-site.Mr. Rice stated that he will notify the contractor to begin work immediately.Inspection conducted with WQSS April Weiland, WPBS Dan Counahan, and Environmental Engineer Tae-Uk Kim.

For data sources see[7]

References