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Well ID: 37-125-27716 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Washington | |
Municipality: North Bethlehem Township | |
Operator Name: RICE DRILLING B LLC | |
Well Pad ID: 150477 | |
Farm/Lease Name: IRON MAN 1H | |
License Status: | |
Spud Date: | |
Permit Date: 2015-08-21 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 40.101494 | |
Longitude: -80.126497 |
Date | Event |
---|---|
2015-08-21 | New Permit Application |
2015-08-25 | Performed Spud Operation |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2016-02-06 | 2016-02-18 | 7,366 | 15,342,900 | 0 |
2 | 2016-01-14 | 2016-01-31 | 7,366 | 16,387,200 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | 100 Mesh | WFT | Proppant | Crystalline Silica in the form of Quartz | 14808-60-7 | 100 | 8.91425 | 12,883,700.0 |
7.5% HCL | WFT | Acid | Hydrochloric Acid | 7647-01-0 | 7.5 | 0.011691 | 16897 | |
WIC-641L | WFT | Iron Control | Citric acid | 77-92-9 | 60 | 0.000713102 | 1030.64 | |
Bio- | WFT | Bactericide | Dibromoacetonitrile | 3252-43-5 | 0.5 | 0.000118601 | 171.413 | |
2,2-dibromo-3-nitriloproppionamide | 10222-01-2 | 5 | 0.00118601 | 1714.13 | ||||
Polyethylene Glycol | 25322-68-3 | 65 | 0.0154181 | 22283.7 | ||||
Sodium Bromide | 7647-15-6 | 1.5 | 0.000355803 | 514.239 | ||||
WFR-68LC | WFT | Friction Reducer | Petroleum Hydrotreated Light Distillate | 64742-47-8 | 25 | 0.000390764 | 564.769 | |
WAI-251LC | WFT | Inhibitor | 1-Octanol | 111-87-5 | 5 | 0.00001019 | 14.733 | |
Triethylphosphate | 78-40-0 | 5 | 0.00001019 | 14.733 | ||||
Tar bases, quinoline derivs, benzyl chloride-quaternized | 72480-70-7 | 10 | 0.00002039 | 29.466 | ||||
Isopropyl Alcohol | 67-63-0 | 5 | 0.00001019 | 14.733 | ||||
2-Butoxyethanol | 111-76-2 | 10 | 0.00002039 | 29.466 | ||||
1-Decanol | 112-30-1 | 5 | 0.00001019 | 14.733 | ||||
Ethylene Glycol | 111-76-2 | 40 | 0.00008155 | 117.865 | ||||
N,N-Dimethylformamide | 68-12-2 | 20 | 0.00004078 | 58.932 | ||||
Ethoxylated Nonylphenol | 68412-54-4 | 5 | 0.00001019 | 14.733 | ||||
Water | Rice Energy | Carrier / Base Fluid | Carrier / Base Fluid - Water | 7732-18-5 | 100 | 88.5884 | 128,036,000.0 | |
WSI-648L | WFT | Inhibitor | Ammonia | 7664-41-7 | 25 | 0.00755933 | 10925.4 | |
Phosphonic Acid | Proprietary | 50 | 0.0151187 | 21850.9 | ||||
Methanol | 67-56-1 | 3 | 0.000907119 | 1311.05 | ||||
Ammonium Chloride | 12125-02-9 | 20 | 0.00604746 | 8740.35 | ||||
WFR-66LC | WFT | Friction Reducers | Petroleum distillates, hydrotreated light | 64742-47-8 | 40 | 0.0139009 | 20090.9 | |
Sodium Chloride | 7647-14-5 | 20 | 0.00695046 | 10045.4 | ||||
15% HCL | WFT | Acid | Hydrochloric Acid | 7647-01-0 | 15 | 0.0026921 | 3890.88 | |
40/70 Premium | WFT | Proppant | Crystalline Silica in the form of Quartz | 14808-60-7 | 100 | 2.23189 | 3,225,740.0 | |
Other Chemicals | Dioxane | 123-91-1 | 0 | 0 | 0 | |||
Cinnamaldehyde | 104-55-2 | 0 | 0 | 0 | ||||
Alcohol Ethoxylate Surfactants | Proprietary | 0 | 0 | 0 | ||||
Ethylene Oxide | 75-21-8 | 0 | 0 | 0 | ||||
Acetaldehyde | 75-07-0 | 0 | 0 | 0 | ||||
Cationic Polyacrylamide copolymer | Proprietary | 0 | 0 | 0 | ||||
2 | Bio- | WFT | Bactericide | Sodium Bromide | 7647-15-6 | 1.5 | 0.000333592 | 517.463 |
Dibromoacetonitrile | 3252-43-5 | 0.5 | 0.000111197 | 172.488 | ||||
Polyethylene Glycol | 25322-68-3 | 65 | 0.0144557 | 22423.4 | ||||
2,2-dibromo-3-nitriloproppionamide | 10222-01-2 | 5 | 0.00111197 | 1724.88 | ||||
WIC-641L | WFT | Iron Control | Citric acid | 77-92-9 | 60 | 0.00154498 | 2396.55 | |
Water | Rice Energy | Carrier / Base Fluid | Carrier / Base Fluid - Water | 7732-18-5 | 100 | 88.1593 | 136,751,000.0 | |
15% HCL | WFT | Acid | Hydrochloric Acid | 7647-01-0 | 15 | 0.0422901 | 65599.8 | |
WAI-251LC | WFT | Inhibitor | Isopropyl Alcohol | 67-63-0 | 5 | 0.00002216 | 34.377 | |
Triethylphosphate | 78-40-0 | 5 | 0.00002216 | 34.377 | ||||
1-Decanol | 112-30-1 | 5 | 0.00002216 | 34.377 | ||||
Tar bases, quinoline derivs, benzyl chloride-quaternized | 72480-70-7 | 10 | 0.00004432 | 68.754 | ||||
1-Octanol | 111-87-5 | 5 | 0.00002216 | 34.377 | ||||
Ethoxylated Nonylphenol | 68412-54-4 | 5 | 0.00002216 | 34.377 | ||||
2-Butoxyethanol | 111-76-2 | 10 | 0.00004432 | 68.754 | ||||
N,N-Dimethylformamide | 68-12-2 | 20 | 0.00008865 | 137.509 | ||||
Ethylene Glycol | 111-76-2 | 40 | 0.000177295 | 275.018 | ||||
Other Chemicals | Dioxane | 123-91-1 | 0 | 0 | 0 | |||
Alcohol Ethoxylate Surfactants | Proprietary | 0 | 0 | 0 | ||||
Cinnamaldehyde | 104-55-2 | 0 | 0 | 0 | ||||
Cationic Polyacrylamide copolymer | Proprietary | 0 | 0 | 0 | ||||
Acetaldehyde | 75-07-0 | 0 | 0 | 0 | ||||
Ethylene Oxide | 75-21-8 | 0 | 0 | 0 | ||||
40/70 Premium | WFT | Proppant | Crystalline Silica in the form of Quartz | 14808-60-7 | 100 | 2.2995 | 3,566,960.0 | |
WFR-66LC | WFT | Friction Reducers | Petroleum distillates, hydrotreated light | 64742-47-8 | 40 | 0.0177604 | 27549.7 | |
Sodium Chloride | 7647-14-5 | 20 | 0.00888022 | 13774.9 | ||||
WSI-648L | WFT | Inhibitor | Ammonia | 7664-41-7 | 25 | 0.00921584 | 14295.5 | |
Ammonium Chloride | 12125-02-9 | 20 | 0.00737267 | 11436.4 | ||||
Phosphonic Acid | Proprietary | 50 | 0.0184317 | 28590.9 | ||||
Methanol | 67-56-1 | 3 | 0.0011059 | 1715.46 | ||||
100 Mesh | WFT | Proppant | Crystalline Silica in the form of Quartz | 14808-60-7 | 100 | 9.15274 | 14,197,600.0 |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2015 | RICE DRILLING B LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | RICE DRILLING B LLC | 2,367,149.28 | 257 | 0.00 | 0 | 0.00 | 0 |
2017 | RICE DRILLING B LLC | 1,423,552.66 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | RICE DRILLING B LLC | 402,497.00 | 202 | 0.00 | 0 | 0.00 | 0 |
2019 | RICE DRILLING B LLC | 566,462.00 | 297 | 0.00 | 0 | 0.00 | 0 |
For data sources see[6]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2015 | RICE DRILLING B LLC | Drilling Fluid Waste | 79.17 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2015 | RICE DRILLING B LLC | Fracing Fluid Waste | 51.67 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2015 | RICE DRILLING B LLC | Drilling Fluid Waste | 560.83 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW005 |
2015 | RICE DRILLING B LLC | Drill Cuttings | 17.65 Tons | LANDFILL | PAD059087072 |
2015 | RICE DRILLING B LLC | Drill Cuttings | 284.06 Tons | LANDFILL | 100592 |
2015 | RICE DRILLING B LLC | Produced Fluid | 211.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW005 |
2015 | RICE DRILLING B LLC | Produced Fluid | 3,167.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2015 | RICE DRILLING B LLC | Fracturing Fluid Waste | 7.10 Tons | LANDFILL | 100592 |
2015 | RICE DRILLING B LLC | Drill Cuttings | 831.50 Tons | RESIDUAL WASTE TRANSFER FACILITY | 301071 |
2015 | RICE DRILLING B LLC | Drill Cuttings | 402.36 Tons | LANDFILL | 100172 |
2016 | RICE DRILLING B LLC | Fracturing Fluid Waste | 2.13 Tons | RESIDUAL WASTE PROCESSING FACILITY | 2014-541 |
2016 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 359.08 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 3.33 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW019 |
2016 | RICE DRILLING B LLC | Fracturing Fluid Waste | 10,300.46 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | RICE DRILLING B LLC | Produced Fluid | 756.50 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW019 |
2016 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 64.14 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2016 | RICE DRILLING B LLC | Produced Fluid | 368.44 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123SW019 |
2016 | RICE DRILLING B LLC | Produced Fluid | 19,101.63 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | RICE DRILLING B LLC | Filter Socks | 0.05 Tons | RESIDUAL WASTE PROCESSING FACILITY | 301280 |
2016 | RICE DRILLING B LLC | Fracturing Fluid Waste | 1,629.62 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123SW019 |
2016 | RICE DRILLING B LLC | Fracturing Fluid Waste | 10.14 Tons | LANDFILL | 100592 |
2016 | RICE DRILLING B LLC | Waste Water Treatment Sludge | 2.49 Tons | RESIDUAL WASTE PROCESSING FACILITY | 2014-541 |
2016 | RICE DRILLING B LLC | Produced Fluid | 590.96 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2016 | RICE DRILLING B LLC | Produced Fluid | 1,442.34 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW005 |
2016 | RICE DRILLING B LLC | Produced Fluid | 17.03 Bbl | INJECTION DISPOSAL WELL | 34-157-25511 |
2016 | RICE DRILLING B LLC | Fracturing Fluid Waste | 32.85 Tons | LANDFILL | 100172 |
2016 | RICE DRILLING B LLC | Fracturing Fluid Waste | 818.01 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW005 |
2016 | RICE DRILLING B LLC | Synthetic Liner Materials | 6.87 Tons | LANDFILL | 100663 |
2017 | RICE DRILLING B LLC | Produced Fluid | 75.03 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW019 |
2017 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 94.04 Bbl | REUSE (AT WELL PAD) | |
2017 | RICE DRILLING B LLC | Produced Fluid | 2,337.20 Bbl | REUSE (AT WELL PAD) | |
2017 | RICE DRILLING B LLC | Produced Fluid | 28.17 Bbl | INJECTION DISPOSAL WELL | 34-059-24202 |
2017 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 56.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2017 | RICE DRILLING B LLC | Waste Water Treatment Sludge | 1.76 Tons | RESIDUAL WASTE TRANSFER FACILITY | 101532 |
2017 | RICE DRILLING B LLC | Produced Fluid | 1,081.12 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2017 | RICE DRILLING B LLC | Produced Fluid | 17.27 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW010 |
2018 | RICE DRILLING B LLC | Produced Fluid | 14.15 Bbl | RESIDUAL WASTE PROCESSING FACILITY | |
2018 | RICE DRILLING B LLC | Produced Fluid | 99.82 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2018 | RICE DRILLING B LLC | Produced Fluid | 20.28 Bbl | REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA | |
2018 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 73.33 Bbl | REUSE (AT WELL PAD) | |
2018 | RICE DRILLING B LLC | Produced Fluid | 128.81 Bbl | REUSE (AT WELL PAD) | |
2019 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 242.50 Bbl | REUSE (AT WELL PAD) | |
2019 | RICE DRILLING B LLC | Produced Fluid | 336.93 Bbl | REUSE (AT WELL PAD) | |
2019 | RICE DRILLING B LLC | Produced Fluid | 36.43 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW005 |
2019 | RICE DRILLING B LLC | Other Oil & Gas Wastes | 36.67 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123SW010 |
2019 | RICE DRILLING B LLC | Synthetic Liner Materials | 4.01 Tons | LANDFILL | 100419 |
2019 | RICE DRILLING B LLC | Produced Fluid | 11.17 Bbl | REUSE AT A WELL PAD OUTSIDE PENNSYLVANIA |
For data sources see[7]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2407575 | Primary Facility | 2015-09-15 | Drilling/Alteration | No Violations Noted | Butch’s Rat Hole Service auger rig |
2409351 | Primary Facility | 2015-09-22 | Complaint Inspection | No Violations Noted | Falcon Schramm rig onsite. |
2409782 | Primary Facility | 2015-09-24 | Drilling/Alteration | No Violations Noted | Falcon Drilling Rig #29 |
2411573 | Primary Facility | 2015-07-24 | Routine/Complete Inspection | No Violations Noted | |
2424389 | Primary Facility | 2015-11-12 | Drilling/Alteration | No Violations Noted | Patterson-UTI Drilling Rig #349 |
2444793 | Primary Facility | 2016-01-27 | Incident- Response to Accident or Event | No Violations Noted | On 1/27/16, I performed an incident inspection at the Ironman Pad in response to these concerns and identified violations including the following:
•My Inspection indicates that either portions of the initial slide or a new slide are currently outside the LOD and within a stream bed directly impacting an operator delineated stream. •A sump outlet shown in the plans extending south east from the southern corner of the pad had a pipe extension added conducting it an additional ~50 feet to a CFS dam not shown or redlined on site plans. Water was running under the CFS dam still carrying sediment and then continuing around perimeter CFS, out of the LOD and into the adjacent stream channel. •In the area where the LOD extends along a spur line NW of the pad a number of hay bales and sections of silt sock have been added in an operator delineated intermittent stream. •An erosion channel was found extending from the north side of the pad near the spur line into the intermittent stream bed. -->Further details in fu |
2527007 | Primary Facility | 2016-03-08 | Follow-up Inspection | No Violations Noted | On 3/8/16, I performed a follow up inspection at the Iron Man Pad regarding an NOV from 1/27/16 (enforcement ID: 333960/Inspection ID: 2444782) accompanied by DEP Engineer Emmanuel Nwaobilo and made the following observations:
•While the pipe extension from the sump outlet noted in the previous extension was removed and additional sections of sock and erosion matting has been added erosion damage outside the LOD and pollution to the Waters of the Commonwealth appears to be ongoing. This constitutes a continuation of the violations of 35 P.S. § 691.401, 78.53, 102.4(B)1, and 102.11(A)1 noted in the inspection from 1/27/16 by continuing in failing to design, implement, and maintain the site E&S BMP’s in such a manner that it prevents and minimizes erosion and sedimentation resulting in a discharge of sediment to Waters of the Commonwealth. •Erosion control measures and stabilization around the landslide that crossed the site LOD have been modified, however no observable effort has been made to remediate the |
2527359 | Primary Facility | 2016-06-28 | Follow-up Inspection | No Violations Noted | On 6/28/16 I performed a follow up inspection of the Iron Man site accompanied by DEP WQS John Parry and Rice representative Jonathan Davis in response to violations noted during inspections on 1/27/16 (ID: 2444782) and 3/8/16 (ID: 2527004) and made the following observations:
•The land slide located along the site LOD on the south eastern border of the site remained unremediated at the time of inspection and continues to impact the Waters of the Commonwealth. This constitutes a continuation of the violations of 35 P.S. § 691.401, 78.53, 102.4(B)1, and 102.11(A)1 noted in the inspection from 1/27/16 by continuing in failing to design, implement, and maintain the site E&S BMP’s in such a manner that it prevents and minimizes erosion and sedimentation resulting in a discharge of sediment to Waters of the Commonwealth. •The area within the site LOD directly up gradient of the slide may be showing additional ground movement but significant disturbance of the area by cattle made definitive assessment unfeasible |
2527825 | Primary Facility | 2016-09-30 | Routine/Partial Inspection | No Violations Noted | Routine/Partial inspection conducted to assess an ongoing issue at the site. |
2657464 | Primary Facility | 2017-10-12 | Follow-up Inspection | No Violations Noted | On 10/12/17 a FUI inspection was conducted of Ironman well site accompanied by DEP WQSS John Carson, DEP Engineer Emmanuel Nwaobilo, DEP Compliance Chief David McDermott, and various Rice Energy representatives in response to an operator request for a meeting regarding current and potential site modifications. The following was observed:
>>Inspection of the contested slide first noted during a site inspection on 1/27/2016 found that the slide had not been remediated but had not notably progressed. Potential remediation by stabilizing the slide edge and vegetating the area. >>An additional slide was found in the vicinity of the previous slides below the south west corner of the pad. An erosion channel ran from the edge of the new slide out of the site LOD into the same area as the contested slide first documented in the 1/27/16 inspection. >>Rice Energy representatives will propose additional measures to continue remediation of site issues. |
2788162 | Primary Facility | 2018-10-11 | Routine/Complete Inspection | No Violations Noted | On Thursday October 11, 2018 I conducted a routine-complete inspection at the Iron Man Well Site located in North Bethlehem Township, Washington County.
Gas well Ironman 1H (125-27716) and the associated infrastructure appeared to be in good condition and functioning properly. The gas well was tagged with identification. No violations were identified during the inspection. |
For data sources see[8]