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Well ID: 37-115-20958 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Susquehanna | |
Municipality: Silver Lake Township | |
Operator Name: SWN PROD CO LLC | |
Well Pad ID: 148916 | |
Farm/Lease Name: MOORE 1 1H | |
License Status: | |
Spud Date: | |
Permit Date: 2012-08-03 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Conservation: No | |
Latitude: 41.897181 | |
Longitude: -75.896722 |
Date | Event |
---|---|
2012-08-03 | New Permit Application |
2012-09-08 | Performed Spud Operation |
2012-10-03 | Drilling Completion |
2013-01-21 | Perforation |
2013-01-21 | Performed Stimulation |
2013-05-01 | DEVIATED |
For data sources see[4]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 2013-01-21 | 2013-01-21 | 6,261 | 3,530,162 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | BE-9M | Halliburton Energy Services | Biocide | Tri-n-butyl tetradecyl phosphonium chloride | 81741-28-8 | 10.00 | 0.00478000 | |
Methanol | 67-56-1 | 30.00 | 0.01 | |||||
FR-66 Friction Reducer | Halliburton Energy Services | Friction Reducer | Distillates, petroleum, hydrotreated light | 64742-47-8 | 30.00 | 0.01 | ||
GBW-30 Breaker | Halliburton Energy Services | Breaker | Hemicellulase enzyme | 9012-54-8 | 15.00 | 0.00020000 | ||
Carbohydrates | 95.00 | 0.00129000 | ||||||
WG-36 Gelling Agent | Halliburton Energy Services | Gel | ||||||
Guar gum | 9000-30-0 | 100.00 | 0.00164000 | |||||
LP-65 | Halliburton Energy Services | Scale Inhibitor | Ammonium chloride | 12125-02-9 | 10.00 | 0.00395000 | ||
Hydrochloric Acid | Halliburton Energy Services | Acid | Hydrochloric acid | 7647-01-0 | 30.00 | 0.07 | ||
Water | Carrier/Base Fluid | Water | 100.00 | 85.83 | ||||
Sand- Silica Sand | Halliburton Energy Services | Proppant | Quartz | 14808-60-7 | 100.00 | 14.02 | ||
SP Breaker | Halliburton Energy Services | Breaker | Sodium persulfate | 7775-27-1 | 100.00 | 0.00136000 | ||
Cla-Web | Halliburton Energy Services | Clay Control | ||||||
Proprietary | 60.00 | 0.02 |
For data sources see[5]
Stimulation Date | Phase Number | Chemical Agent | Volume (gal) | Treating Pressure (psi) | Breakdown Pressure (psi) |
---|---|---|---|---|---|
2013-01-21 | 0 | 0 | 0 |
For data sources see[6]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2012 | XPR RESOURCES LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | XPR RESOURCES LLC | 230,971.46 | 259 | 0.00 | 0 | 0.00 | 0 |
2014 | XPR RESOURCES LLC | 191,283.01 | 331 | 0.00 | 0 | 0.00 | 0 |
2015 | SWN PROD CO LLC | 156,423.82 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | SWN PROD CO LLC | 117,612.00 | 334 | 0.00 | 0 | 0.00 | 0 |
2017 | SWN PROD CO LLC | 56,034.00 | 109 | 0.00 | 0 | 0.00 | 0 |
2018 | SWN PROD CO LLC | 104,770.00 | 351 | 0.00 | 0 | 0.00 | 0 |
2019 | SWN PROD CO LLC | 74,172.00 | 323 | 0.00 | 0 | 0.00 | 0 |
For data sources see[7]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2012 | XPR RESOURCES LLC | Drill Cuttings | 884.52 Tons | LANDFILL | 8-0728-0004/013 |
2012 | XPR RESOURCES LLC | Drilling Fluid Waste | 220.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC006 |
2013 | XPR RESOURCES LLC | Produced Fluid | 484.71 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123SW018 |
2013 | XPR RESOURCES LLC | Produced Fluid | 971.90 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR119 |
2013 | XPR RESOURCES LLC | Produced Fluid | 1,292.53 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC010 |
2013 | XPR RESOURCES LLC | Fracing Fluid Waste | 110.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2013 | XPR RESOURCES LLC | Produced Fluid | 2,119.50 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2013 | XPR RESOURCES LLC | Produced Fluid | 1,712.01 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 |
2013 | XPR RESOURCES LLC | Produced Fluid | 757.76 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123 |
2013 | XPR RESOURCES LLC | Produced Fluid | 1,554.76 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123NC010 |
2013 | XPR RESOURCES LLC | Produced Fluid | 105.79 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR123SW018 |
2014 | XPR RESOURCES LLC | Produced Fluid | 336.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR119 |
2014 | XPR RESOURCES LLC | Produced Fluid | 618.15 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC010 |
2014 | XPR RESOURCES LLC | Produced Fluid | 2,190.55 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2014 | XPR RESOURCES LLC | Produced Fluid | 948.19 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2015 | SOUTHWESTERN ENERGY PROD CO | Produced Fluid | 2,696.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | SWN PROD CO LLC | Other Oil & Gas Wastes | 1,648.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2016 | SWN PROD CO LLC | Soil Contaminated by Oil | 41.50 Tons | LANDFILL | THR029 |
2016 | SWN PROD CO LLC | Soil Contaminated by Oil & Gas Related Spills | 41.50 Tons | LANDFILL | THR029 |
2016 | SWN PROD CO LLC | Produced Fluid | 759.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NC018 |
2016 | SWN PROD CO LLC | Produced Fluid | 1,426.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2017 | SWN PROD CO LLC | Soil Contaminated by Oil | 16.00 Tons | LANDFILL | THR029 |
2017 | SWN PROD CO LLC | Drilling Fluid Waste | 600.00 Bbl | REUSE (AT WELL PAD) | |
2017 | SWN PROD CO LLC | Other Oil & Gas Wastes | 2,594.00 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2017 | SWN PROD CO LLC | Produced Fluid | 1,552.00 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2017 | SWN PROD CO LLC | Other Oil & Gas Wastes | 313.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2017 | SWN PROD CO LLC | Soil Contaminated by Oil & Gas Related Spills | 16.00 Tons | LANDFILL | THR029 |
2018 | SWN PROD CO LLC | Produced Fluid | 220.00 Bbl | SURFACE IMPOUNDMENT | 826342 |
2018 | SWN PROD CO LLC | Produced Fluid | 790.00 Bbl | REUSE (AT WELL PAD) | |
2018 | SWN PROD CO LLC | Produced Fluid | 1,371.00 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2018 | SWN PROD CO LLC | Other Oil & Gas Wastes | 414.15 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2019 | SWN PROD CO LLC | Produced Fluid | 125.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC035 |
2019 | SWN PROD CO LLC | Other Oil & Gas Wastes | 131.74 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2019 | SWN PROD CO LLC | Produced Fluid | 1,023.00 Bbl | SURFACE IMPOUNDMENT | 95-16-65420-013 |
2019 | SWN PROD CO LLC | Produced Fluid | 110.00 Bbl | REUSE (AT WELL PAD) | |
2019 | SWN PROD CO LLC | Produced Fluid | 553.00 Bbl | SURFACE IMPOUNDMENT | 826342 |
For data sources see[8]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2099709 | Primary Facility | 2012-09-13 | Drilling/Alteration | Pending | Orion Rig- Polaris. Company Man notified inspector via email that during 13 3/8" cement job had 154' of fall back due to air pocket. Operator performed top job. Tagged TOC at 154' with plumb line. Ran 1" tremie pipe to only 0'. Pumped total of 28 bbls of neat cement (15.6 ppg). REprted returns of good cement to surface during top job. Drilling ahead @ 743' on air to @1600'. Once completed drilling intermediate section will run gyro and then CBL. Operator will contat DEP prior to running 9 5/8" casing. |
2106871 | Primary Facility | 2012-09-25 | Drilling/Alteration | No Violations Noted | Polaris - Orion Rig. Co. Man - Fred Webb. Plan to run 5 1/2" casing on Thursday am. BOP charts posted. Walked site with Tool Pusher and Safety Officer. Secondary containment in place and in good condition. Drillers log on site and up to date. No violations observed at this time. TD of hole proposed to be 11630'. |
2204579 | Primary Facility | 2013-09-16 | Routine/Complete Inspection | No Violations Noted | |
2306348 | Primary Facility | 2014-09-23 | Complaint Inspection | No Violations Noted | |
2358334 | Primary Facility | 2015-04-06 | Routine/Complete Inspection | No Violations Noted | |
2362965 | Primary Facility | 2015-04-22 | Administrative/File Review | No Violations Noted | |
2363196 | Primary Facility | 2015-04-21 | Routine/Complete Inspection | Pending | On 4/21/2015 the Department was on site to conduct a routine full inspection of the Moore Well Pad. |
2413918 | Primary Facility | 2015-10-07 | Routine/Complete Inspection | No Violations Noted | At time of inspection, arrived on site at 11:10 a.m., the cellar was full of gravel, the vent pipe was closed and set up with a Taylor plug, there was no gas detected at the perimeter of the cellar, there was 266psi on the production casing and 205psi on the production line. I took a walk around the location, everything looked OK. |
2472165 | Primary Facility | 2016-03-10 | Routine/Complete Inspection | No Violations Noted | The Department was on site to inspect the former WPX (Now SWN) site of the Moore Well Pad (WR45)(ESX12-115-0078). The last E&S inspection was performed on 3/7/2016. The wells associated with this site are as follows:
115-20958 115-20959 115-20960 115-20961 There were no erosional issues with the site, all slopes were stable and there were no failures of BMPs to note. There was however, a large spoil pile on the site, probably in excess of 100 tons. This spoil pile was mostly rock, and was not eroding or sending sediment off site but was not mulched, and it would be suggested that a SWN representative assess this pile for future concerns. There were no violations. If there are any questions please feel free to call me at (570) 346-5539. |
2488706 | Primary Facility | 2016-05-03 | Routine/Complete Inspection | No Violations Noted | The Department was on site to inspect the former WPX (Now SWN) site of the Moore Well Pad (WR45)(ESX12-115-0078). The wells associated with this site are as follows:
115-20958 115-20959 115-20960 115-20961 There were no erosional issues with the site, all slopes were stable and there were no failures of BMPs to note. There was however, a large spoil pile on the site, probably in excess of 100 tons. There were no violations. If there are any questions please feel free to call me at (570) 346-5539. |
2508240 | Primary Facility | 2016-08-04 | Routine/Complete Inspection | No Violations Noted | At time of inspection, arrived on site at 13:40p.m., the cellar was full of gravel and no gas was detected. The vent pipe was open and set up with a Tayler plug to check for pressure, there was 185psi on the production casing and 145psi on the production line. I took a walk around the location and everything looked OK.
I left the site at 14:05p.m. |
2542144 | Primary Facility | 2016-12-01 | Incident- Response to Accident or Event | Pending | Michael Williams, Evan Brandt and Chris Becker, Environmental Health and Safety Specialist of SWN contacted me at 4:07 PM on 11/30/16 to report a release of gas discovered at 2:30 PM on 11/30/16. They stated that a subsurface production fluid dump line failed creating the potential for an impact to the pad in the general area where the dump line is located. Mr. Brandt forwarded me an email at 5:11 PM on 11/30/16. The email stated the following. "Per our conversation earlier, a suspected buried dump line (area between the wellhead and production tank) failure occurred on the WR-45-Moore Pad earlier this afternoon. At this time, we are unaware of any environmental impacts outside of the dump line ditch. SWN Regulatory has been continually testing the surface throughout the afternoon and has found no elevated conductivity levels. All wells on location are shut in and we will begin investigating the subsurface area tomorrow morning 12/1/2016 at 9:00 am. Resource Environmental has been contracted to perform |
2546885 | Primary Facility | 2016-12-21 | Administrative/File Review | Violation(s) Noted | On December 1, 2016, the Department and SWN Production Company, LLC (Southwestern) collected groundwater samples from the excavation at the SWNPC Moore Pad. Upon review of the Department’s and SWNPC's groundwater sample results, it was noted that the sample results had elevated concentrations of barium, strontium, aluminum, chloride, iron and manganese. Barium was detected above the Act 2, Residential and Non-residential Medium Specific Concentration (MSC) for groundwater of 2,000 micrograms per liter (µg/l) with a concentration of 33,570 µg/l detected in the Department’s sample and 34,500 µg/l detected in SWNPC's sample. Strontium was detected above the Act 2, Residential and Non-residential MSC for groundwater of 4,000 µg/l with a concentration of 52,200 µg/l detected in the Department’s sample and 48,800 µg/l detected in SWNPC's sample. Aluminum was detected above the Act 2 Secondary Maximum Contaminant Level (SMCL) of 200 µg/l with a concentration of 9,581 µg/l detected in the Department’s sample and |
2548815 | Primary Facility | 2017-01-03 | Follow-up Inspection | No Violations Noted | The Department, represented by Frank Hoehle, was on site to conduct a Follow Up Inspection of the Moore well site (West Range Unit 45) (ESX12-115-0078). This well site had a release occur on 12/1/2016 with subsequent sampling events and NOV occurring.
According to Mike Deming, SWN representative, screening and vac truck excavation around suspected leak area ended Thursday, December 8, 2016 and confirmatory sampling for this specific area occurred Friday December 9, 2016. Upon excavation, elevated conductivity readings were observed flowing into excavation from West side of brine tank area along back of pad. SWN will be sampling homes in the vicinity, one of which has elevated conductivity historically. SWN now digging test pits on East side of pad to check for possible contamination left over from previous ownership. There were no further violations. If there are any questions please feel free to call me at (570) 346-5539. |
2602041 | Primary Facility | 2017-06-06 | Routine/Complete Inspection | No Violations Noted | At time of inspection, arrived on site at 10:45p.m.
The cellar was full of gravel and there was no gas detected at the perimeter of the cellar. The (9x5) annulus vent pipe was open and set up with a Taylor plug to check for pressure with a Crystal pressure gauge. There was 310psi on the production casing and 116psi on the production line. I took a walk around the location and there were no obvious concerns noticed. I left the site at 11:10a.m. |
2661957 | Primary Facility | 2017-11-15 | Routine/Complete Inspection | No Violations Noted | I inspected the Moore well pad on November 15 as a Routine Complete inspection. The well pad was solid and had no current erosional issues, and was well vegetated. There had been a produced water release here approximately a year ago. The cut and fill slopes were solid and stable as was the access road.
There were no violations noted. |
2703646 | Primary Facility | 2018-03-09 | Administrative/File Review | Violation(s) Noted | Administrative Inspection record created for entering an Enforcement Record for the pollution of a private water supply in Silver Lake Township, Susquehanna County determined to be caused by a subsurface production fluid dump line failure on SWN's West Range 45 Moore Well Pad. VIOL against the Moore 1H gas well (115-20958). |
2706401 | Primary Facility | 2018-03-16 | Routine/Complete Inspection | No Violations Noted | At time of inspection.
The well was in production. The cellar was full of gravel and covered with snow, the snow insulated the gravel so it wasn't frozen and there was no gas detected at the perimeter of the cellar. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted. |
2793938 | Primary Facility | 2018-10-24 | Routine/Complete Inspection | No Violations Noted | At time of inspection.
Met with Cody Stanton (Production Foreman) for SWN. The well was in production. The cellar was full of gravel and there was no gas detected at the perimeter of the cellar. Cody used a Crystal pressure gauge to get the pressures for the ((9x5) annulus, production casing and tubing. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted. |
2814754 | Primary Facility | 2018-12-12 | Routine/Complete Inspection | No Violations Noted | I performed a RTNC inspection of the Moore well pad. The weather was overcast and about 32 degrees F. There was a light covering of snow on the ground and there was construction work being performed along the access road and the fill slope. There was stone staged near the entrance to the access road.
An infiltration basin PCSM was apparently being constructed. There were competent temporary BMPs downgradient of the ongoing construction work. The cut slope was mostly rock and appeared stable. There was a smattering of vegetation visible where suffient soil was available to support growth. The fill slope, while under construction in part, was well vegetated otherwise. The vegetation appeared to be a mix of perennial grasses. The well pad was snowcovered, solid and stable. There was a large spoils pile on site but it was not causing any problems regarding erosion and sedimentation. The well onsite was labeled properly. There were no violations noted. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2546885 | 775086 | 2016-12-21 | 2016-12-21 | CSL 402(b) | Environmental Health & Safety | Potential for pollutional substances to enter the waters of the commonwealth. |
2546885 | 775087 | 2016-12-21 | 2016-12-21 | 78.57(a) | Environmental Health & Safety | Failure to collect the brine and other fluids produced during the operation and service of the well in a tank, pit or a series of pits or tanks, or other device approved by the Department. |
2546885 | 775088 | 2016-12-21 | 2016-12-21 | SWMA 301 | Environmental Health & Safety | Failure to properly store, transport, process or dispose of a residual waste. |
2703646 | 810429 | 2018-03-09 | CSL 401 | Environmental Health & Safety | Pollution of a private water supply in Silver Lake Township, Susquehanna County determined to be caused by a subsurface production fluid dump line failure on SWN's West Range 45 Moore Well Pad. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
775086 | 349643 | NOV - Notice of Violation | 2017-05-01 | ||||
775087 | 349643 | NOV - Notice of Violation | 2017-05-01 | ||||
775088 | 349643 | NOV - Notice of Violation | 2017-05-01 | ||||
810429 | 362222 | NOV - Notice of Violation |
For data sources see[9]