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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-111-24494 | | Well ID: 34-111-24494 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.83, -81.26 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | Municipality: | + | | State: Ohio |
+ | |- | ||
+ | | County: [[Monroe_County,_Ohio|Monroe]] | ||
+ | |- | ||
+ | | Municipality: [[Seneca_Township,_Monroe_County,_Ohio|Seneca Township]] | ||
|- | |- | ||
| Operator Name: [[ANTERO RESOURCES CORPORATION]] | | Operator Name: [[ANTERO RESOURCES CORPORATION]] | ||
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: [[US-OH-001063]] |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: LORADITCH UNIT |
|- | |- | ||
− | | | + | | License Status: Producing |
|- | |- | ||
− | | | + | | License Date: 2015-01-20 |
|- | |- | ||
| Spud Date: 2014-09-15 | | Spud Date: 2014-09-15 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[PATTERSON DRILLING]] |
− | |||
− | |||
|- | |- | ||
− | | | + | | Final Drill Date: 2015-02-24 |
|- | |- | ||
− | | | + | | Well Total Depth: 17331.00 ft |
|- | |- | ||
− | | | + | | Configuration: Horizontal |
|- | |- | ||
− | | | + | | Latitude: 39.830000 |
|- | |- | ||
+ | | Longitude: -81.260000 | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Well History == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | + | !scope="col" style="text-align: center"| Well Status |
− | + | !scope="col" style="width: 15%;text-align: center"| Well Status Date | |
− | !scope="col" | + | !scope="col" style="text-align: center"| Comment |
− | |||
− | !scope="col" | ||
− | |||
− | |||
|- | |- | ||
− | | - | + | | APP |
+ | | 2014-06-16 | ||
+ | | Proposed Formations:POINT PLEASANT, Issued Date:6/16/2014, Expired Date:6/15/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT | ||
+ | |- | ||
+ | | APP | ||
+ | | 2014-11-10 | ||
+ | | Proposed Formations:POINT PLEASANT, Issued Date:11/10/2014, Expired Date:11/9/2016 12:00:00 PM, Drilling unit acres:659.424, Proposed Well Type:OG, Proposed Well Class:POOL | ||
+ | |- | ||
+ | | APP | ||
+ | | 2015-01-20 | ||
+ | | Proposed Formations:POINT PLEASANT, Issued Date:1/20/2015, Expired Date:1/19/2017 12:00:00 PM, Drilling unit acres:659.424, Proposed Well Type:OG, Proposed Well Class:POOL | ||
+ | |- | ||
+ | | Reached Total Depth | ||
| 2015-02-24 | | 2015-02-24 | ||
| | | | ||
− | | | + | |- |
+ | | Correction to Well | ||
+ | | 2015-04-24 | ||
+ | | CHANGE IN TARGET & TAKE-POINT INFORMATION (FOOTAGES & COORDINATES) FROM AS DRILLED SURVEY PLAT. UNIT SIZE INCREASED. | ||
+ | |- | ||
+ | | Completion Report Received | ||
+ | | 2015-11-13 | ||
+ | | | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2017-01-19 | ||
| | | | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2017-10-23 | ||
| | | | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | | 2015-11-16 | ||
+ | | style="text-align: right;" | 8626 | ||
+ | | style="text-align: right;" | 17243 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | | ||
+ | | style="text-align: right;" | 8626 | ||
+ | | style="text-align: right;" | 17243 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
| | | | ||
+ | | style="text-align: right;" | 8626 | ||
+ | | style="text-align: right;" | 17243 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Perfs Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | | 1 | ||
+ | | 04/26/2015 | ||
+ | | 06/18/2015 | ||
+ | | style="text-align: right;" | 8464 | ||
+ | | style="text-align: right;" | 12,701,100.0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |} | ||
+ | ==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="50"| 1 | ||
+ | | rowspan="1"| Ferrotrol 300L | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Iron Control | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0021802 | ||
+ | | style="text-align: right;" | 2563.37 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Scaletrol 720 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Scale Inhibitor | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0150208 | ||
+ | | style="text-align: right;" | 17661.1 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| GW-3 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Gelling Agent | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0389437 | ||
+ | | style="text-align: right;" | 45789 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| GW-3LDF | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Gelling Agent | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.005494 | ||
+ | | style="text-align: right;" | 6459.75 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| FRW-18 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Friction Reducer | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0691998 | ||
+ | | style="text-align: right;" | 81363.4 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Water | ||
+ | | rowspan="1"| Operator | ||
+ | | rowspan="1"| Carrier | ||
+ | | Water | ||
+ | | 7732-18-5 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 90.0387 | ||
+ | | style="text-align: right;" | 105,899,000.0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| CI-39 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Corrosion Inhibitor | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.0006807 | ||
+ | | style="text-align: right;" | 800.4 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| HCl, 10.1 - 15% | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Acidizing | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.327064 | ||
+ | | style="text-align: right;" | 384553 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Sand, White, 40/70 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Proppant | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 4.46594 | ||
+ | | style="text-align: right;" | 5,250,940.0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Sand, White, 100 mesh | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Proppant | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 1.25914 | ||
+ | | style="text-align: right;" | 1,480,470.0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Alpha 1427 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Biocide | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0.008893 | ||
+ | | style="text-align: right;" | 10456.3 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="1"| Sand, White, 20/40 | ||
+ | | rowspan="1"| Baker Hughes | ||
+ | | rowspan="1"| Proppant | ||
+ | | MSDS and Non-MSDS Ingredients Listed Below | ||
+ | | N/A | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 3.73971 | ||
+ | | style="text-align: right;" | 4,397,060.0 | ||
+ | |- | ||
+ | |- valign="top" | ||
+ | | rowspan="38"| Ingredients in Additive(s) (MSDS and non-MSDS) | ||
+ | | rowspan="38"| Baker Hughes | ||
+ | | rowspan="38"| See Trade Name(s) List | ||
+ | | Sodium Chloride | ||
+ | | 7647-14-5 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.003609 | ||
+ | | style="text-align: right;" | 4244.78 | ||
+ | |- | ||
+ | | Guar Gum | ||
+ | | 9000-30-0 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 0.0422266 | ||
+ | | style="text-align: right;" | 49664.8 | ||
+ | |- | ||
+ | | Oxyalkylated Fatty Acid | ||
+ | | 61791-002 | ||
+ | | style="text-align: right;" | 40 | ||
+ | | style="text-align: right;" | 0.0002722 | ||
+ | | style="text-align: right;" | 320.16 | ||
+ | |- | ||
+ | | Glutaraldehyde | ||
+ | | 111-30-8 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0026671 | ||
+ | | style="text-align: right;" | 3136.88 | ||
+ | |- | ||
+ | | Tar Bases, Quinoline Derivs., Benzyl Chloride-Quaternized | ||
+ | | 72480-70-7 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0002042 | ||
+ | | style="text-align: right;" | 240.12 | ||
+ | |- | ||
+ | | 1-butoxy-2-propanol | ||
+ | | 5131-66-8 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0002746 | ||
+ | | style="text-align: right;" | 322.988 | ||
+ | |- | ||
+ | | Aldehyde | ||
+ | | 104-55-2 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0002042 | ||
+ | | style="text-align: right;" | 240.12 | ||
+ | |- | ||
+ | | Ethylene Glycol | ||
+ | | 107-21-1 | ||
+ | | style="text-align: right;" | 45 | ||
+ | | style="text-align: right;" | 0.0067572 | ||
+ | | style="text-align: right;" | 7947.51 | ||
+ | |- | ||
+ | | Mineral Oil | ||
+ | | 8042-47-5 | ||
+ | | style="text-align: right;" | 70 | ||
+ | | style="text-align: right;" | 0.0038446 | ||
+ | | style="text-align: right;" | 4521.82 | ||
+ | |- | ||
+ | | Isotridecanol, ethoxylated | ||
+ | | 9043-30-5 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0002746 | ||
+ | | style="text-align: right;" | 322.988 | ||
+ | |- | ||
+ | | Sulfurized polyolefin | ||
+ | | 68037-13-8 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.00003400 | ||
+ | | style="text-align: right;" | 40.02 | ||
+ | |- | ||
+ | | 2-Propenoic, Polymer with Sodium Phosphinate, Sodium Salt | ||
+ | | 71050-62-9 | ||
+ | | style="text-align: right;" | 20 | ||
+ | | style="text-align: right;" | 0.0030032 | ||
+ | | style="text-align: right;" | 3532.22 | ||
+ | |- | ||
+ | | Petroleum Distillates | ||
+ | | 64742-47-8 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0016477 | ||
+ | | style="text-align: right;" | 1937.93 | ||
+ | |- | ||
+ | | Quaternary Ammonium Compound | ||
+ | | 68424-85-1 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0004785 | ||
+ | | style="text-align: right;" | 562.832 | ||
+ | |- | ||
+ | | Crystalline Silica (Quartz) | ||
+ | | 14808-60-7 | ||
+ | | style="text-align: right;" | 100 | ||
+ | | style="text-align: right;" | 9.46176 | ||
+ | | style="text-align: right;" | 11,128,500.0 | ||
+ | |- | ||
+ | | Formic Acid | ||
+ | | 64-18-6 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0002042 | ||
+ | | style="text-align: right;" | 240.12 | ||
+ | |- | ||
+ | | Polyaklylene | ||
+ | | 7756-94-7 | ||
+ | | style="text-align: right;" | 1 | ||
+ | | style="text-align: right;" | 0.00000680 | ||
+ | | style="text-align: right;" | 8.004 | ||
+ | |- | ||
+ | | Oleamide DEA | ||
+ | | 93-83-4 | ||
+ | | style="text-align: right;" | 2 | ||
+ | | style="text-align: right;" | 0.0013836 | ||
+ | | style="text-align: right;" | 1627.27 | ||
+ | |- | ||
+ | | Paraffinic Petroleum Distillate | ||
+ | | 64742-55-8 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0016477 | ||
+ | | style="text-align: right;" | 1937.93 | ||
+ | |- | ||
+ | | Alcohols, C12-16, ethoxylated | ||
+ | | 68551-12-2 | ||
+ | | style="text-align: right;" | 2 | ||
+ | | style="text-align: right;" | 0.0013836 | ||
+ | | style="text-align: right;" | 1627.27 | ||
+ | |- | ||
+ | | Polyoxythylene Sorbitan Monooleate | ||
+ | | 9005-65-6 | ||
+ | | style="text-align: right;" | 0.5 | ||
+ | | style="text-align: right;" | 0.0003459 | ||
+ | | style="text-align: right;" | 406.817 | ||
+ | |- | ||
+ | | Crystalline Silica: Quartz | ||
+ | | 14808-60-7 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0002746 | ||
+ | | style="text-align: right;" | 322.988 | ||
+ | |- | ||
+ | | Citric Acid | ||
+ | | 77-92-9 | ||
+ | | style="text-align: right;" | 60 | ||
+ | | style="text-align: right;" | 0.0013077 | ||
+ | | style="text-align: right;" | 1538.02 | ||
+ | |- | ||
+ | | Didecyl Dimethyl Ammonium Chloride | ||
+ | | 7173-51-5 | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 0.000889 | ||
+ | | style="text-align: right;" | 1045.63 | ||
+ | |- | ||
+ | | Poly (acrylamide-co-acrylic acid) partial sodium salt | ||
+ | | 62649-23-4 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0207533 | ||
+ | | style="text-align: right;" | 24409 | ||
+ | |- | ||
+ | | 2-butoxy-1-propanol | ||
+ | | 15821-83-7 | ||
+ | | style="text-align: right;" | 0.1 | ||
+ | | style="text-align: right;" | 0.00000550 | ||
+ | | style="text-align: right;" | 6.45975 | ||
+ | |- | ||
+ | | Water | ||
+ | | 7732-18-5 | ||
+ | | style="text-align: right;" | 95 | ||
+ | | style="text-align: right;" | 0.331567 | ||
+ | | style="text-align: right;" | 389973 | ||
+ | |- | ||
+ | | Isopropanol | ||
+ | | 67-63-0 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.00003400 | ||
+ | | style="text-align: right;" | 40.02 | ||
+ | |- | ||
+ | | Potassium Acetate | ||
+ | | 127-08-2 | ||
+ | | style="text-align: right;" | 0.5 | ||
+ | | style="text-align: right;" | 0.00000340 | ||
+ | | style="text-align: right;" | 4.002 | ||
+ | |- | ||
+ | | Potassium Chloride | ||
+ | | 7447-40-7 | ||
+ | | style="text-align: right;" | 1 | ||
+ | | style="text-align: right;" | 0.0001502 | ||
+ | | style="text-align: right;" | 176.611 | ||
+ | |- | ||
+ | | Ammonium Chloride | ||
+ | | 12125-02-9 | ||
+ | | style="text-align: right;" | 3 | ||
+ | | style="text-align: right;" | 0.0020753 | ||
+ | | style="text-align: right;" | 2440.9 | ||
+ | |- | ||
+ | | Sorbitan Monooleate | ||
+ | | 1338-43-8 | ||
+ | | style="text-align: right;" | 0.5 | ||
+ | | style="text-align: right;" | 0.0003459 | ||
+ | | style="text-align: right;" | 406.817 | ||
+ | |- | ||
+ | | Hydrochloric Acid | ||
+ | | 7647-01-0 | ||
+ | | style="text-align: right;" | 15 | ||
+ | | style="text-align: right;" | 0.0490438 | ||
+ | | style="text-align: right;" | 57683 | ||
+ | |- | ||
+ | | Hemicellulase Enzyme Concentrate | ||
+ | | 9025-56-3 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0006313 | ||
+ | | style="text-align: right;" | 742.481 | ||
+ | |- | ||
+ | | Ethanol | ||
+ | | 64-17-5 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0004445 | ||
+ | | style="text-align: right;" | 522.813 | ||
+ | |- | ||
+ | | Calcium Chloride | ||
+ | | 10043-52-4 | ||
+ | | style="text-align: right;" | 5 | ||
+ | | style="text-align: right;" | 0.0007508 | ||
+ | | style="text-align: right;" | 883.056 | ||
+ | |- | ||
+ | | Hydrotreated Light Distillate | ||
+ | | 64742-47-8 | ||
+ | | style="text-align: right;" | 30 | ||
+ | | style="text-align: right;" | 0.0207533 | ||
+ | | style="text-align: right;" | 24409 | ||
+ | |- | ||
+ | | Potassium Iodide | ||
+ | | 7681-11-0 | ||
+ | | style="text-align: right;" | 2 | ||
+ | | style="text-align: right;" | 0.00001360 | ||
+ | | style="text-align: right;" | 16.008 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = FracFocus Fracking Chemicals Database | ||
+ | | date = 2019-04-02 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-06-19 }}</ref> | ||
+ | == Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | | 2015-06-18 | ||
+ | | H2O | ||
+ | | style="text-align: right;" | 15 | ||
+ | | style="text-align: right;" | 6092 Bbl | ||
+ | | style="text-align: right;" | 223993 | ||
+ | | [[BAKER-HUGHES]] | ||
+ | | STAGE 49/49 | ||
+ | 36 SHOTS | ||
+ | |- | ||
+ | | 2015-05-11 | ||
+ | | H2O | ||
+ | | style="text-align: right;" | 15 | ||
+ | | style="text-align: right;" | 6483 Bbl | ||
+ | | style="text-align: right;" | 238862 | ||
+ | | [[BAKER-HUGHES]] | ||
+ | | STAGE 1/49 | ||
+ | 36 SHOTS | ||
+ | STAGES 2-48 SEE IMAGES | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblStimulation Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | style="text-align: right;" | 2064683 | ||
+ | | style="text-align: right;" | 47 | ||
+ | | style="text-align: right;" | 153 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | style="text-align: right;" | 2177378 | ||
+ | | style="text-align: right;" | 51 | ||
+ | | style="text-align: right;" | 366 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | style="text-align: right;" | 846886 | ||
+ | | style="text-align: right;" | 164 | ||
+ | | style="text-align: right;" | 364 | ||
+ | |- | ||
+ | | 2018 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | style="text-align: right;" | 554771 | ||
+ | | style="text-align: right;" | 213 | ||
+ | | style="text-align: right;" | 363 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | style="text-align: right;" | 90089 | ||
+ | | style="text-align: right;" | 69 | ||
+ | | style="text-align: right;" | 90 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2015 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 28521 | ||
+ | | style="text-align: right;" | 153 | ||
+ | |- | ||
+ | | 2016 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 20761 | ||
+ | | style="text-align: right;" | 366 | ||
+ | |- | ||
+ | | 2017 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 7997 | ||
+ | | style="text-align: right;" | 364 | ||
|- | |- | ||
+ | | 2018 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 5838 | ||
+ | | style="text-align: right;" | 363 | ||
+ | |- | ||
+ | | 2019 | ||
+ | | [[ANTERO RESOURCES CORPORATION]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 1043 | ||
+ | | style="text-align: right;" | 90 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2020-11-16 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2020-11-16 }}</ref> | ||
+ | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Inspection Date | ||
+ | !scope="col" style="text-align: center"| Inspection Type | ||
+ | !scope="col" style="text-align: center"| Inspection Result | ||
+ | !scope="col" style="text-align: center"| Inspection Comments | ||
+ | |- | ||
+ | | -1028932448 | ||
+ | | 2015-2-24 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 1.50 | ||
|- | |- | ||
| -1128438036 | | -1128438036 | ||
+ | | 2015-2-3 0:00:0 | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 3.00 | ||
+ | |- | ||
+ | | -1438525445 | ||
+ | | 2015-2-11 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 2.00 | ||
+ | |- | ||
+ | | -1604591490 | ||
+ | | 2018-3-7 0:00:0 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.20 | ||
+ | |- | ||
+ | | -1733321021 | ||
+ | | 2018-3-7 0:00:0 | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.20 | ||
+ | |- | ||
+ | | -178828843 | ||
+ | | 2019-1-14 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.30 | ||
+ | |- | ||
+ | | -705108963 | ||
+ | | 2015-2-12 0:00: | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 2.30 | ||
+ | |- | ||
+ | | -967130156 | ||
+ | | 2015-2-9 0:00:0 | ||
+ | | DD | ||
+ | | No Violations | ||
+ | | 2.00 | ||
+ | |- | ||
+ | | -968533127 | ||
+ | | 2020-6-30 0:00: | ||
+ | | PW | ||
+ | | No Violations | ||
+ | | 0.40 | ||
+ | |- | ||
+ | | 0178828843 | ||
+ | | 2019-01-14 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On this day, I spoke with Antero Company Representative Jayson Lukes during the inspection. The producing wells on the pad (permit numbers 4489, 4490, 4492, 4494) are being prepped per Anteros SIMOPS plan that was submitted and reviewed by the ODNR DOGRM, before Stalnaker Energy rigs-up for the plug and abandonment of permit numbers 4491 and 4493. TekSolv is currently onsite setting the back pressure valve. The producing wells have been blown down, are having back pressure valves installed in the tubing hangers, steel cages placed over the wellheads, LEL monitors in place, and concrete Jersey barriers spotted around the perimeter of the wellheads. It will be noted that a 2-way check valve will not be placed in the tubing, as the SIMOPS plan originally stated. I spoke with Jayson Lukes and ODNR Inspector Ken Frye about the amendment to the plan. | ||
+ | |- | ||
+ | | 0705108963 | ||
+ | | 2015-02-12 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Status check inspection on the current drilling process found Patterson Drilling rig 343 on location drilling the horizontal wellbore section at a current depth of 10,342 in the directional azimuth of 330 degrees at 90.92 degrees using 15.5# drilling mud with a current influx of 2,169 units of gas. | ||
+ | |- | ||
+ | | 0967130156 | ||
+ | | 2015-02-09 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | My inspection today finds the well has been drilled to a depth of 9235. The top drive is broke down. Drilling will resume as soon as the top drive is repaired. | ||
+ | |- | ||
+ | | 1028932448 | ||
+ | | 2015-02-24 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Status check inspection on the drilling progress found Patterson Drilling rig 343 has recently completed the drilling of the 8.5 production borehole to a measured depth of 17,331 in the directional azimuth of 331.73 degrees with a true vertical depth of 8,326 at the casing shoe. 17,355 of 5.5 23# -P- | ||
+ | |- | ||
+ | | 1128438036 | ||
| 2015-02-03 | | 2015-02-03 | ||
− | | | + | | Drill / Deepen / Reopen |
+ | | No Violations | ||
| I am onsite to witness part of the blow out preventer (BOP) testing. The annular section of the BOP did not pass and is being rebuilt. The testing services are being provided by Gas Field Resources. The company representative was instructed to email copies of the test as soon as available. | | I am onsite to witness part of the blow out preventer (BOP) testing. The annular section of the BOP did not pass and is being rebuilt. The testing services are being provided by Gas Field Resources. The company representative was instructed to email copies of the test as soon as available. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1330479029 | | 1330479029 | ||
| 2014-09-18 | | 2014-09-18 | ||
− | | | + | | Casing String Witnessed |
− | | Status check inspection found Rocky Mountain drillings top hole rig has drilled a 32 | + | | No Violations |
− | + | | Status check inspection found Rocky Mountain drillings top hole rig has drilled a 32 x 80 conductor borehole and set 80 of 26 conductor in place with a variance granted by the Division to set 80 of conductor due to being in solid limestone bedrock at 60 freshwater was also encountered at 27. Allied cement services are on location and cementing the casing using 228 sacks of class A-2% calcium .25 pps flake with 30% open hole excess ran and 46.5 barrels of fresh water used for cement displacement with good cement returns to surface. The hole was spudded on 09/15/14. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1416440338 | | 1416440338 | ||
| 2014-11-19 | | 2014-11-19 | ||
− | | | + | | Casing String Witnessed |
− | | 11/19/2014 Dallas Morris rig # 24 is now on the hole and has drilled a | + | | No Violations |
− | + | | 11/19/2014 Dallas Morris rig # 24 is now on the hole and has drilled a 24x 397 surface casing borehole on air and ran 376 of 18.625 -87.50# J-55 casing with a Texas style guide shoe and float collar ran along with proper centralizer placement demonstrated. Allied Cement services are on location to cement the casing using 737 sacks of class A-2% calcium .25 pps flake along with 100% open hole excess cement used with circulation established prior to cementing and 25 bbl of 6% gel ran ahead of the cement and the casing pressure tested to 500 psi over displacement lift pressure upon the landing of the cement plug and good cement returns witnessed to surface. The cement weight was verified and the mix water tested showing no chlorides. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1416868294 | | 1416868294 | ||
| 2014-11-24 | | 2014-11-24 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Status check inspection on the current drilling process found Dallas Morris rig # 24 on location picking up the 12.250 | + | | No Violations |
− | + | | Status check inspection on the current drilling process found Dallas Morris rig # 24 on location picking up the 12.250 bottom hole drilling assembly to begin running in the hole with the drill string to drill the 12.250 2nd intermediate well bore section on air. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1423484050 | | 1423484050 | ||
| 2015-02-08 | | 2015-02-08 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Status check inspection on the drilling process found Patterson Drilling rig 343 on location drilling the 8.750 | + | | No Violations |
− | + | | Status check inspection on the drilling process found Patterson Drilling rig 343 on location drilling the 8.750 production borehole at a depth of 8,685 in the directional azimuth of 337.82 using 13.8# mud weight with a viscosity of 77, the 3rp party gas units are at 2452. The projected well bore total drilling depth will be 17,450. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1430484733 | | 1430484733 | ||
| 2015-02-15 | | 2015-02-15 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Status check inspection on the current drilling process found Patterson drilling rig 343 on the hole drilling the 8.750 | + | | No Violations |
− | | | + | | Status check inspection on the current drilling process found Patterson drilling rig 343 on the hole drilling the 8.750 production borehole at a depth of 12,963 in the directional azimuth of 327.19 degrees and inclination of 90.65 degrees with a true vertical well bore depth of 8,404 carrying a 15.1# mud weight. The drilling rig has adequate containment and the perimeter drainage system valves are in the closed position during drilling operations. |
− | | | + | |- |
− | | | + | | 1434475612 |
+ | | 2015-06-16 | ||
+ | | Completion Testing | ||
+ | | No Violations | ||
+ | | Status check inspection on the well stimulation process found Baker Hughes pressure pumping service on location stimulating stage 43 of 49 to be completed with the annular pressure being monitored electronically. Allied Horizontal wireline service is on location and has perforated the stage (43) with a solid completion plug set at 9,851 and 60 perforations shot in 10 clusters of 6 shots utilizing a shoot on the fly method of 38 a minute travel speed between the depths of 9,813 and 9,682 in the horizontal well bore section. | ||
|- | |- | ||
+ | | 1436453808 | ||
+ | | 2015-07-09 | ||
+ | | Completion Testing | ||
+ | | No Violations | ||
+ | | Status check inspection on the well completion process found Fortis Well Service on location drilling out the completion plugs at a current depth of 14,985 with Cudd Services providing well control during the drill out process. The rig and all support equipment is located on containment and Myers well service is on location recovering surface water created from the recent rain fall event. | ||
|- | |- | ||
− | | | + | | 1438525445 |
| 2015-02-11 | | 2015-02-11 | ||
− | | | + | | Drill / Deepen / Reopen |
+ | | No Violations | ||
| My inspection today finds the rig is circulating the well at 30 strokes (3 barrels) per minute. Gas levels have been minimized and the Pason system is reading 60 units of gas. The company representative Matt Manderfield stated that the mud will be built up to 15.1 pounds per gallon before controlled drilling will resume. | | My inspection today finds the rig is circulating the well at 30 strokes (3 barrels) per minute. Gas levels have been minimized and the Pason system is reading 60 units of gas. The company representative Matt Manderfield stated that the mud will be built up to 15.1 pounds per gallon before controlled drilling will resume. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1604591490 | ||
+ | | 2018-03-07 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | On site inspection accompanied by ODNR Inspector Tom Thomas. On this day the well was observed to be production off the production tree with (2) manual production valves present along with a single (ESD) Emergency Shut Down valve. The ESD has remote shut down buttons located at the well pad entrance along with the production facility and the gas processing units. The well is equipped with steel lines on the 13.375 and 9.625 casing well heads with valves and gauges present to monitor annular pressures. The 13.375 well head section was observed to have 0 pounds pressure on it at surface and the 9.625 section was observed to have 50 pounds on it at surface. In conversation with Anteros Production Supervisor Doug Stebbins all annular pressures are being monitored and evaluated. The well pad has an earthen berm established. The production fluid facility is located on a adjoining site pad and consists of (8) steel construction tanks of 400 barrels fluid capacity each. The tanks are situated inside a polymer lined steel containment dike area. | ||
|- | |- | ||
− | | | + | | 1733321021 |
− | | | + | | 2018-03-07 |
− | | | + | | Production Wells |
− | | | + | | No Violations |
− | + | | On this day, I accompanied ODNR Inspector William Stolarik. Please refer to his comments for a detailed report. The well is equipped with annular pressure monitoring devices. Concrete barriers surround the wellheads. The facility is gated with an electronic shutdown button on the left-hand side, prior to the pad. The back of the pad is equipped with (8) 400 barrel steel tanks within containment. There are (4) gas processing units along the front right side of the pad, and a midstream facility along the back right side. | |
− | |||
− | |||
− | |||
|- | |- | ||
− | | | + | | 2089784016 |
− | | 2015- | + | | 2015-11-09 |
− | | | + | | Preliminary Restoration |
− | | | + | | No Violations |
− | + | | Preliminary Restoration status check inspecting found the affected area by the well pad construction has properly been restored with vegetation and erosion control in place. Addressing the well head- The well drilling and completion process is now complete and the well is on line and producing along with 3 other wells on the pad. Supporting the well is a gas processing unit and 8-400 barrel production tanks located in a polymer lined metal containment dike area. Proper well identification is posted at the well head. | |
− | |||
− | |||
|- | |- | ||
|} | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2020-11-16 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2020-11-16 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
+ | [[Category:FracFocus]] |
Well ID: 34-111-24494 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Seneca Township | |
Operator Name: ANTERO RESOURCES CORPORATION | |
Well Pad ID: US-OH-001063 | |
Farm/Lease Name: LORADITCH UNIT | |
License Status: Producing | |
License Date: 2015-01-20 | |
Spud Date: 2014-09-15 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2015-02-24 | |
Well Total Depth: 17331.00 ft | |
Configuration: Horizontal | |
Latitude: 39.830000 | |
Longitude: -81.260000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2014-06-16 | Proposed Formations:POINT PLEASANT, Issued Date:6/16/2014, Expired Date:6/15/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2014-11-10 | Proposed Formations:POINT PLEASANT, Issued Date:11/10/2014, Expired Date:11/9/2016 12:00:00 PM, Drilling unit acres:659.424, Proposed Well Type:OG, Proposed Well Class:POOL |
APP | 2015-01-20 | Proposed Formations:POINT PLEASANT, Issued Date:1/20/2015, Expired Date:1/19/2017 12:00:00 PM, Drilling unit acres:659.424, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2015-02-24 | |
Correction to Well | 2015-04-24 | CHANGE IN TARGET & TAKE-POINT INFORMATION (FOOTAGES & COORDINATES) FROM AS DRILLED SURVEY PLAT. UNIT SIZE INCREASED. |
Completion Report Received | 2015-11-13 | |
Construction Permit Expires | 2017-01-19 | |
Record Last Modified | 2017-10-23 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2015-11-16 | 8626 | 17243 | 0 |
8626 | 17243 | 0 | |
8626 | 17243 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 04/26/2015 | 06/18/2015 | 8464 | 12,701,100.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | Ferrotrol 300L | Baker Hughes | Iron Control | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0021802 | 2563.37 |
Scaletrol 720 | Baker Hughes | Scale Inhibitor | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0150208 | 17661.1 | |
GW-3 | Baker Hughes | Gelling Agent | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0389437 | 45789 | |
GW-3LDF | Baker Hughes | Gelling Agent | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.005494 | 6459.75 | |
FRW-18 | Baker Hughes | Friction Reducer | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0691998 | 81363.4 | |
Water | Operator | Carrier | Water | 7732-18-5 | 100 | 90.0387 | 105,899,000.0 | |
CI-39 | Baker Hughes | Corrosion Inhibitor | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.0006807 | 800.4 | |
HCl, 10.1 - 15% | Baker Hughes | Acidizing | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.327064 | 384553 | |
Sand, White, 40/70 | Baker Hughes | Proppant | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 4.46594 | 5,250,940.0 | |
Sand, White, 100 mesh | Baker Hughes | Proppant | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 1.25914 | 1,480,470.0 | |
Alpha 1427 | Baker Hughes | Biocide | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 0.008893 | 10456.3 | |
Sand, White, 20/40 | Baker Hughes | Proppant | MSDS and Non-MSDS Ingredients Listed Below | N/A | 0 | 3.73971 | 4,397,060.0 | |
Ingredients in Additive(s) (MSDS and non-MSDS) | Baker Hughes | See Trade Name(s) List | Sodium Chloride | 7647-14-5 | 5 | 0.003609 | 4244.78 | |
Guar Gum | 9000-30-0 | 100 | 0.0422266 | 49664.8 | ||||
Oxyalkylated Fatty Acid | 61791-002 | 40 | 0.0002722 | 320.16 | ||||
Glutaraldehyde | 111-30-8 | 30 | 0.0026671 | 3136.88 | ||||
Tar Bases, Quinoline Derivs., Benzyl Chloride-Quaternized | 72480-70-7 | 30 | 0.0002042 | 240.12 | ||||
1-butoxy-2-propanol | 5131-66-8 | 5 | 0.0002746 | 322.988 | ||||
Aldehyde | 104-55-2 | 30 | 0.0002042 | 240.12 | ||||
Ethylene Glycol | 107-21-1 | 45 | 0.0067572 | 7947.51 | ||||
Mineral Oil | 8042-47-5 | 70 | 0.0038446 | 4521.82 | ||||
Isotridecanol, ethoxylated | 9043-30-5 | 5 | 0.0002746 | 322.988 | ||||
Sulfurized polyolefin | 68037-13-8 | 5 | 0.00003400 | 40.02 | ||||
2-Propenoic, Polymer with Sodium Phosphinate, Sodium Salt | 71050-62-9 | 20 | 0.0030032 | 3532.22 | ||||
Petroleum Distillates | 64742-47-8 | 30 | 0.0016477 | 1937.93 | ||||
Quaternary Ammonium Compound | 68424-85-1 | 5 | 0.0004785 | 562.832 | ||||
Crystalline Silica (Quartz) | 14808-60-7 | 100 | 9.46176 | 11,128,500.0 | ||||
Formic Acid | 64-18-6 | 30 | 0.0002042 | 240.12 | ||||
Polyaklylene | 7756-94-7 | 1 | 0.00000680 | 8.004 | ||||
Oleamide DEA | 93-83-4 | 2 | 0.0013836 | 1627.27 | ||||
Paraffinic Petroleum Distillate | 64742-55-8 | 30 | 0.0016477 | 1937.93 | ||||
Alcohols, C12-16, ethoxylated | 68551-12-2 | 2 | 0.0013836 | 1627.27 | ||||
Polyoxythylene Sorbitan Monooleate | 9005-65-6 | 0.5 | 0.0003459 | 406.817 | ||||
Crystalline Silica: Quartz | 14808-60-7 | 5 | 0.0002746 | 322.988 | ||||
Citric Acid | 77-92-9 | 60 | 0.0013077 | 1538.02 | ||||
Didecyl Dimethyl Ammonium Chloride | 7173-51-5 | 10 | 0.000889 | 1045.63 | ||||
Poly (acrylamide-co-acrylic acid) partial sodium salt | 62649-23-4 | 30 | 0.0207533 | 24409 | ||||
2-butoxy-1-propanol | 15821-83-7 | 0.1 | 0.00000550 | 6.45975 | ||||
Water | 7732-18-5 | 95 | 0.331567 | 389973 | ||||
Isopropanol | 67-63-0 | 5 | 0.00003400 | 40.02 | ||||
Potassium Acetate | 127-08-2 | 0.5 | 0.00000340 | 4.002 | ||||
Potassium Chloride | 7447-40-7 | 1 | 0.0001502 | 176.611 | ||||
Ammonium Chloride | 12125-02-9 | 3 | 0.0020753 | 2440.9 | ||||
Sorbitan Monooleate | 1338-43-8 | 0.5 | 0.0003459 | 406.817 | ||||
Hydrochloric Acid | 7647-01-0 | 15 | 0.0490438 | 57683 | ||||
Hemicellulase Enzyme Concentrate | 9025-56-3 | 5 | 0.0006313 | 742.481 | ||||
Ethanol | 64-17-5 | 5 | 0.0004445 | 522.813 | ||||
Calcium Chloride | 10043-52-4 | 5 | 0.0007508 | 883.056 | ||||
Hydrotreated Light Distillate | 64742-47-8 | 30 | 0.0207533 | 24409 | ||||
Potassium Iodide | 7681-11-0 | 2 | 0.00001360 | 16.008 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2015-06-18 | H2O | 15 | 6092 Bbl | 223993 | BAKER-HUGHES | STAGE 49/49
36 SHOTS |
2015-05-11 | H2O | 15 | 6483 Bbl | 238862 | BAKER-HUGHES | STAGE 1/49
36 SHOTS STAGES 2-48 SEE IMAGES |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ANTERO RESOURCES CORPORATION | 2064683 | 47 | 153 |
2016 | ANTERO RESOURCES CORPORATION | 2177378 | 51 | 366 |
2017 | ANTERO RESOURCES CORPORATION | 846886 | 164 | 364 |
2018 | ANTERO RESOURCES CORPORATION | 554771 | 213 | 363 |
2019 | ANTERO RESOURCES CORPORATION | 90089 | 69 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2015 | ANTERO RESOURCES CORPORATION | Brine | 28521 | 153 |
2016 | ANTERO RESOURCES CORPORATION | Brine | 20761 | 366 |
2017 | ANTERO RESOURCES CORPORATION | Brine | 7997 | 364 |
2018 | ANTERO RESOURCES CORPORATION | Brine | 5838 | 363 |
2019 | ANTERO RESOURCES CORPORATION | Brine | 1043 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1028932448 | 2015-2-24 0:00: | DD | No Violations | 1.50 |
-1128438036 | 2015-2-3 0:00:0 | DD | No Violations | 3.00 |
-1438525445 | 2015-2-11 0:00: | DD | No Violations | 2.00 |
-1604591490 | 2018-3-7 0:00:0 | PW | No Violations | 0.20 |
-1733321021 | 2018-3-7 0:00:0 | PW | No Violations | 0.20 |
-178828843 | 2019-1-14 0:00: | PW | No Violations | 0.30 |
-705108963 | 2015-2-12 0:00: | DD | No Violations | 2.30 |
-967130156 | 2015-2-9 0:00:0 | DD | No Violations | 2.00 |
-968533127 | 2020-6-30 0:00: | PW | No Violations | 0.40 |
0178828843 | 2019-01-14 | Production Wells | No Violations | On this day, I spoke with Antero Company Representative Jayson Lukes during the inspection. The producing wells on the pad (permit numbers 4489, 4490, 4492, 4494) are being prepped per Anteros SIMOPS plan that was submitted and reviewed by the ODNR DOGRM, before Stalnaker Energy rigs-up for the plug and abandonment of permit numbers 4491 and 4493. TekSolv is currently onsite setting the back pressure valve. The producing wells have been blown down, are having back pressure valves installed in the tubing hangers, steel cages placed over the wellheads, LEL monitors in place, and concrete Jersey barriers spotted around the perimeter of the wellheads. It will be noted that a 2-way check valve will not be placed in the tubing, as the SIMOPS plan originally stated. I spoke with Jayson Lukes and ODNR Inspector Ken Frye about the amendment to the plan. |
0705108963 | 2015-02-12 | Drill / Deepen / Reopen | No Violations | Status check inspection on the current drilling process found Patterson Drilling rig 343 on location drilling the horizontal wellbore section at a current depth of 10,342 in the directional azimuth of 330 degrees at 90.92 degrees using 15.5# drilling mud with a current influx of 2,169 units of gas. |
0967130156 | 2015-02-09 | Drill / Deepen / Reopen | No Violations | My inspection today finds the well has been drilled to a depth of 9235. The top drive is broke down. Drilling will resume as soon as the top drive is repaired. |
1028932448 | 2015-02-24 | Drill / Deepen / Reopen | No Violations | Status check inspection on the drilling progress found Patterson Drilling rig 343 has recently completed the drilling of the 8.5 production borehole to a measured depth of 17,331 in the directional azimuth of 331.73 degrees with a true vertical depth of 8,326 at the casing shoe. 17,355 of 5.5 23# -P- |
1128438036 | 2015-02-03 | Drill / Deepen / Reopen | No Violations | I am onsite to witness part of the blow out preventer (BOP) testing. The annular section of the BOP did not pass and is being rebuilt. The testing services are being provided by Gas Field Resources. The company representative was instructed to email copies of the test as soon as available. |
1330479029 | 2014-09-18 | Casing String Witnessed | No Violations | Status check inspection found Rocky Mountain drillings top hole rig has drilled a 32 x 80 conductor borehole and set 80 of 26 conductor in place with a variance granted by the Division to set 80 of conductor due to being in solid limestone bedrock at 60 freshwater was also encountered at 27. Allied cement services are on location and cementing the casing using 228 sacks of class A-2% calcium .25 pps flake with 30% open hole excess ran and 46.5 barrels of fresh water used for cement displacement with good cement returns to surface. The hole was spudded on 09/15/14. |
1416440338 | 2014-11-19 | Casing String Witnessed | No Violations | 11/19/2014 Dallas Morris rig # 24 is now on the hole and has drilled a 24x 397 surface casing borehole on air and ran 376 of 18.625 -87.50# J-55 casing with a Texas style guide shoe and float collar ran along with proper centralizer placement demonstrated. Allied Cement services are on location to cement the casing using 737 sacks of class A-2% calcium .25 pps flake along with 100% open hole excess cement used with circulation established prior to cementing and 25 bbl of 6% gel ran ahead of the cement and the casing pressure tested to 500 psi over displacement lift pressure upon the landing of the cement plug and good cement returns witnessed to surface. The cement weight was verified and the mix water tested showing no chlorides. |
1416868294 | 2014-11-24 | Drill / Deepen / Reopen | No Violations | Status check inspection on the current drilling process found Dallas Morris rig # 24 on location picking up the 12.250 bottom hole drilling assembly to begin running in the hole with the drill string to drill the 12.250 2nd intermediate well bore section on air. |
1423484050 | 2015-02-08 | Drill / Deepen / Reopen | No Violations | Status check inspection on the drilling process found Patterson Drilling rig 343 on location drilling the 8.750 production borehole at a depth of 8,685 in the directional azimuth of 337.82 using 13.8# mud weight with a viscosity of 77, the 3rp party gas units are at 2452. The projected well bore total drilling depth will be 17,450. |
1430484733 | 2015-02-15 | Drill / Deepen / Reopen | No Violations | Status check inspection on the current drilling process found Patterson drilling rig 343 on the hole drilling the 8.750 production borehole at a depth of 12,963 in the directional azimuth of 327.19 degrees and inclination of 90.65 degrees with a true vertical well bore depth of 8,404 carrying a 15.1# mud weight. The drilling rig has adequate containment and the perimeter drainage system valves are in the closed position during drilling operations. |
1434475612 | 2015-06-16 | Completion Testing | No Violations | Status check inspection on the well stimulation process found Baker Hughes pressure pumping service on location stimulating stage 43 of 49 to be completed with the annular pressure being monitored electronically. Allied Horizontal wireline service is on location and has perforated the stage (43) with a solid completion plug set at 9,851 and 60 perforations shot in 10 clusters of 6 shots utilizing a shoot on the fly method of 38 a minute travel speed between the depths of 9,813 and 9,682 in the horizontal well bore section. |
1436453808 | 2015-07-09 | Completion Testing | No Violations | Status check inspection on the well completion process found Fortis Well Service on location drilling out the completion plugs at a current depth of 14,985 with Cudd Services providing well control during the drill out process. The rig and all support equipment is located on containment and Myers well service is on location recovering surface water created from the recent rain fall event. |
1438525445 | 2015-02-11 | Drill / Deepen / Reopen | No Violations | My inspection today finds the rig is circulating the well at 30 strokes (3 barrels) per minute. Gas levels have been minimized and the Pason system is reading 60 units of gas. The company representative Matt Manderfield stated that the mud will be built up to 15.1 pounds per gallon before controlled drilling will resume. |
1604591490 | 2018-03-07 | Production Wells | No Violations | On site inspection accompanied by ODNR Inspector Tom Thomas. On this day the well was observed to be production off the production tree with (2) manual production valves present along with a single (ESD) Emergency Shut Down valve. The ESD has remote shut down buttons located at the well pad entrance along with the production facility and the gas processing units. The well is equipped with steel lines on the 13.375 and 9.625 casing well heads with valves and gauges present to monitor annular pressures. The 13.375 well head section was observed to have 0 pounds pressure on it at surface and the 9.625 section was observed to have 50 pounds on it at surface. In conversation with Anteros Production Supervisor Doug Stebbins all annular pressures are being monitored and evaluated. The well pad has an earthen berm established. The production fluid facility is located on a adjoining site pad and consists of (8) steel construction tanks of 400 barrels fluid capacity each. The tanks are situated inside a polymer lined steel containment dike area. |
1733321021 | 2018-03-07 | Production Wells | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please refer to his comments for a detailed report. The well is equipped with annular pressure monitoring devices. Concrete barriers surround the wellheads. The facility is gated with an electronic shutdown button on the left-hand side, prior to the pad. The back of the pad is equipped with (8) 400 barrel steel tanks within containment. There are (4) gas processing units along the front right side of the pad, and a midstream facility along the back right side. |
2089784016 | 2015-11-09 | Preliminary Restoration | No Violations | Preliminary Restoration status check inspecting found the affected area by the well pad construction has properly been restored with vegetation and erosion control in place. Addressing the well head- The well drilling and completion process is now complete and the well is on line and producing along with 3 other wells on the pad. Supporting the well is a gas processing unit and 8-400 barrel production tanks located in a polymer lined metal containment dike area. Proper well identification is posted at the well head. |
For data sources see[10]