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Difference between revisions of "34-073-60300"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-073-60300
 
| Well ID: 34-073-60300
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.565438242, -82.31856642 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.56, -82.31 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
Line 11: Line 11:
 
| County: [[Hocking_County,_Ohio|Hocking]]
 
| County: [[Hocking_County,_Ohio|Hocking]]
 
|-
 
|-
| Municipality: [[Falls Township,_Hocking_County,_Ohio|Falls Township]]
+
| Municipality: [[Green_Township,_Hocking_County,_Ohio|Green Township]]
 
|-
 
|-
 
| Operator Name: [[GRIM PAUL A]]
 
| Operator Name: [[GRIM PAUL A]]
Line 33: Line 33:
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Latitude: 39.565438242
+
| Latitude: 39.560000
 
|-
 
|-
| Longitude: -82.31856642
+
| Longitude: -82.310000
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Well History ==
 
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 77: Line 77:
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  | title = Risk Based Data Management System - Well and WellHistry Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<!--== Perforation Treatments ==
 
<!--== Perforation Treatments ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 133: Line 133:
 
| 2002
 
| 2002
 
| [[GRIM PAUL A]]
 
| [[GRIM PAUL A]]
| style="text-align: right;" | 0
+
| style="text-align: right;" | 0.00
| style="text-align: right;" | 0
+
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
|-
 
|-
 
| 2003
 
| 2003
 
| [[GRIM PAUL A]]
 
| [[GRIM PAUL A]]
| style="text-align: right;" | 0
+
| style="text-align: right;" | 0.00
| style="text-align: right;" | 0
+
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
|-
 
|-
Line 147: Line 147:
 
  | title = Risk Based Data Management System - Production Table - Oil and Gas Data
 
  | title = Risk Based Data Management System - Production Table - Oil and Gas Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<ref>{{cite web
 
<ref>{{cite web
 
  | title = Combined Production - Oil and Gas Data
 
  | title = Combined Production - Oil and Gas Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable"
 
{| class="wikitable sortable"
Line 180: Line 180:
 
  | title = Risk Based Data Management System - Production Table - Brine Data
 
  | title = Risk Based Data Management System - Production Table - Brine Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
<ref>{{cite web
 
<ref>{{cite web
 
  | title = Combined Production - Brine Data
 
  | title = Combined Production - Brine Data
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2019-05-07
+
  | date = 2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 
==== Inspections Performed ====
 
==== Inspections Performed ====
Line 197: Line 197:
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Result
 
!scope="col" style="text-align: center"| Inspection Comments
 
!scope="col" style="text-align: center"| Inspection Comments
 +
|-
 +
| -1000056686
 +
| 2008-5-1 0:00:0
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -10063694
 +
| 2007-12-12 0:00
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -1085143051
 +
| 2008-3-21 0:00:
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -1173838615
 +
| 2007-8-9 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -12150849
 +
| 2007-12-27 0:00
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -1357237036
 +
| 2007-1-29 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1414488377
 +
| 2007-3-8 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1418520551
 +
| 2007-7-17 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1426938645
 +
| 2007-8-24 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1469815706
 +
| 2007-5-1 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1474514639
 +
| 2007-3-12 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -147749570
 +
| 2007-11-29 0:00
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -1505078640
 +
| 2007-8-20 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1754705
 +
| 2007-3-27 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1798488863
 +
| 2007-7-6 0:00:0
 +
| AM
 +
| No Violations
 +
|
 +
|-
 +
| -1953962125
 +
| 2007-1-5 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -1993194513
 +
| 2007-9-7 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -199452399
 +
| 2007-9-12 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -2022898350
 +
| 2007-11-19 0:00
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -2086023468
 +
| 2007-5-30 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -2091978877
 +
| 2007-10-16 0:00
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -249657727
 +
| 2006-4-19 0:00:
 +
| PW
 +
| No Violations
 +
|
 +
|-
 +
| -445102940
 +
| 2004-10-19 0:00
 +
| PW
 +
| No Violations
 +
|
 +
|-
 +
| -543169590
 +
| 2007-4-9 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -562228820
 +
| 2008-1-4 0:00:0
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| -563377575
 +
| 2007-10-19 0:00
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -710406226
 +
| 2007-2-8 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -717364399
 +
| 2007-8-21 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -764307877
 +
| 2007-2-26 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| -779582953
 +
| 2007-8-28 0:00:
 +
| PB
 +
| No Violations
 +
|
 
|-
 
|-
 
| 0001754705
 
| 0001754705
Line 611: Line 791:
 
| No Violations
 
| No Violations
 
| An inspection revealed that Paul Grim is working on final restoration.
 
| An inspection revealed that Paul Grim is working on final restoration.
 +
|-
 +
| 206254081
 +
| 2007-9-17 0:00:
 +
| PB
 +
| No Violations
 +
|
 
|-
 
|-
 
| 2086023468
 
| 2086023468
Line 635: Line 821:
 
| No Violations
 
| No Violations
 
| No activity at the well site.
 
| No activity at the well site.
 +
|-
 +
| 3080695
 +
| 2008-6-10 0:00:
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| 337212012
 +
| 2007-1-3 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 40325971
 +
| 2004-2-24 0:00:
 +
| PW
 +
| No Violations
 +
|
 +
|-
 +
| 40975803
 +
| 2007-2-15 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 483174573
 +
| 2007-11-8 0:00:
 +
| FR
 +
| No Violations
 +
|
 +
|-
 +
| 571289577
 +
| 2006-4-19 0:00:
 +
| PW
 +
| No Violations
 +
|
 +
|-
 +
| 752013080
 +
| 2006-12-11 0:00
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 770999571
 +
| 2007-8-13 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 794460748
 +
| 2006-12-11 0:00
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 869256826
 +
| 2007-1-4 0:00:0
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 91391731
 +
| 2007-8-16 0:00:
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 963932219
 +
| 2006-12-28 0:00
 +
| PB
 +
| No Violations
 +
|
 +
|-
 +
| 991359368
 +
| 2007-8-6 0:00:0
 +
| PB
 +
| No Violations
 +
|
 
|-
 
|-
 
|}
 
|}
Line 673: Line 937:
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 
  |publisher = [[Ohio Department of Natural Resources]]
 
  |publisher = [[Ohio Department of Natural Resources]]
  | date =  2019-05-07
+
  | date =  2020-11-16
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2019-05-21 }}</ref>
+
  | accessdate = 2020-11-16 }}</ref>
 
==References==
 
==References==
 
<references/>
 
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Ohio Wells]]
 
[[Category:Ohio Wells]]

Latest revision as of 09:02, 12 January 2021

Well Details

Well ID: 34-073-60300
Loading map...
Country: United States
State: Ohio
County: Hocking
Municipality: Green Township
Operator Name: GRIM PAUL A
Well Pad ID:
Farm/Lease Name: BOZETT
License Status: Final Restoration
License Date: 2007-09-19
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.560000
Longitude: -82.310000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-05-06 Proposed Formations:CLINTON, Issued Date:5/6/2005, Expired Date:5/6/2006 6:00:00 AM, Drilling unit acres:160, Proposed Well Type:OG, Proposed Well Class:
APP 2006-08-04 Proposed Formations:CLINTON, Issued Date:8/4/2006, Expired Date:8/4/2007 6:00:00 AM, Drilling unit acres:160, Proposed Well Type:OG, Proposed Well Class:
APP 2007-09-19 Proposed Formations:CLINTON, Issued Date:9/19/2007, Expired Date:9/18/2008 6:00:00 AM, Drilling unit acres:160, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2007-10-19 NO RECORDS AVAILABLE.
Construction Permit Expires 2008-09-18 NO RECORDS AVAILABLE.
Record Last Modified 2013-03-14 NO RECORDS AVAILABLE.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2002 GRIM PAUL A 0.00 0.00 365
2003 GRIM PAUL A 0.00 0.00 365

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2002 GRIM PAUL A Brine 0 365
2003 GRIM PAUL A Brine 0 365

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1000056686 2008-5-1 0:00:0 FR No Violations
-10063694 2007-12-12 0:00 FR No Violations
-1085143051 2008-3-21 0:00: FR No Violations
-1173838615 2007-8-9 0:00:0 PB No Violations
-12150849 2007-12-27 0:00 FR No Violations
-1357237036 2007-1-29 0:00: PB No Violations
-1414488377 2007-3-8 0:00:0 PB No Violations
-1418520551 2007-7-17 0:00: PB No Violations
-1426938645 2007-8-24 0:00: PB No Violations
-1469815706 2007-5-1 0:00:0 PB No Violations
-1474514639 2007-3-12 0:00: PB No Violations
-147749570 2007-11-29 0:00 FR No Violations
-1505078640 2007-8-20 0:00: PB No Violations
-1754705 2007-3-27 0:00: PB No Violations
-1798488863 2007-7-6 0:00:0 AM No Violations
-1953962125 2007-1-5 0:00:0 PB No Violations
-1993194513 2007-9-7 0:00:0 PB No Violations
-199452399 2007-9-12 0:00: PB No Violations
-2022898350 2007-11-19 0:00 FR No Violations
-2086023468 2007-5-30 0:00: PB No Violations
-2091978877 2007-10-16 0:00 PB No Violations
-249657727 2006-4-19 0:00: PW No Violations
-445102940 2004-10-19 0:00 PW No Violations
-543169590 2007-4-9 0:00:0 PB No Violations
-562228820 2008-1-4 0:00:0 FR No Violations
-563377575 2007-10-19 0:00 PB No Violations
-710406226 2007-2-8 0:00:0 PB No Violations
-717364399 2007-8-21 0:00: PB No Violations
-764307877 2007-2-26 0:00: PB No Violations
-779582953 2007-8-28 0:00: PB No Violations
0001754705 2007-03-27 Plug / Plug Back Violations Noted On 3/27/2007, a site visit revealed no activity at the well. Attempts have been made to contact Paul Grims shop. No calls have been returned. Paul Grims Company appears to have broken an old production line. A significant amount of C&P was observed, in a low lying area, below the well location. It has been noted that oil gradually rises to the surface. This company has been instructed on several occassions to pump contaminated water into the pit and remove oily soil. Also, noted was that the pit liner needs replaced and fluid pumped from the pit. No change was observed with well plugging status. Company is still having problems running tubing back into the well.
0003080695 2008-06-10 Final Restoration No Violations FR meets requirements.
0010063694 2007-12-12 Final Restoration No Violations An inspection revealed that more work will be needed on the final restoration. A cement slab, (2) cement blocks and railroad tie will need to be removed. The landowner states that he is working out a deal with Paul Grim and will sign a waiver for the vegetation requirement.
0012150849 2007-12-27 Final Restoration No Violations An inspection revealed non-compliance.
0040325971 2004-02-24 Production Wells Violations Noted FOLLOW UP TO NOV # 1077829349 An inspection of the well revealed the well is idle and incapable of production, according to production records well has not produced for several years. All valves shut in, brush and weeds growing up in pump jack and around equipment.
0040975803 2007-02-15 Plug / Plug Back No Violations An inspection conducted on 2/15/2007 revealed that company has made no progress pulling the pipe out of the well. No activity was observed at the time of the inspection. Mr. Paul Grim was again informed by telephone to obtain plugging contractor if work can not be performed by his crew.
0091391731 2007-08-16 Plug / Plug Back No Violations An inspection revealed activity at the well site. Mr. John Ogle, Paul Grims employee, states that they gained 31 feet. The company believes that current depth is between 240 feet and 250 feet. Mr. Paul Thompson states that they are working on a talley sheet for the casing retrieved from the well. Paul Grims employess were instructed to have the fluid removed from the pit that has reached maximum capacity. Also, the pit will need to be replaced.
0147749570 2007-11-29 Final Restoration No Violations An inspection revealed that the company is working on the final restoration. It was noted that a railroad tie, (2) cement slabs, and 2 joints of casing will need to be removed. A landowner waiver will be received for the vegetative cover.
0199452399 2007-09-12 Plug / Plug Back No Violations An inspection revealed activity at the well. A talley sheet for the 5.5 inch casing was obtained from Mr. Paul Grims employees. The pipe talley sheet will need to be calculated.
0206254081 2007-09-17 Plug / Plug Back No Violations An inspection revealed that the company has placed 5 bags of Quickrete around the 7 inch casing to aid with the circulation. Paul Grims employees state that the current depth is 15 joints at 440 feet.
0249657727 2006-04-19 Production Wells No Violations Follow-up on NOV and Chiefs Order, Non-Compliance, well still idle and incapable of producing, took photos of well.
0337212012 2007-01-03 Plug / Plug Back No Violations The company is making an attempt to rip 5.5 pipe.
0445102940 2004-10-19 Production Wells No Violations Follow-up on NOV, Non-Complaince, well still idle, no action taken to date to plug or produce. NEW LAT & LONG
0483174573 2007-11-08 Final Restoration No Violations An inspection revealed that company is working on final restoration. The pit has been closed. More dirt work will be needed.
0543169590 2007-04-09 Plug / Plug Back No Violations An inspection revealed no activity at the well site. Paul Grim still needs to run tubing back into the well to set final plug.
0562228820 2008-01-04 Final Restoration No Violations A follow-up inspection revealed non-compliance.
0563377575 2007-10-19 Plug / Plug Back No Violations An inspection revealed that the well has been topped off. ID has been placed on well bore.
0571289577 2006-04-19 Production Wells No Violations Follow-up inspection was conducted with Dan Goins. No action was taken to remedy the violations.
0710406226 2007-02-08 Plug / Plug Back No Violations An inspection conducted on 2/8/2007 revealed no activity at the well site.
0717364399 2007-08-21 Plug / Plug Back No Violations Paul Grims crew state that the current depth is 340 feet. They were again informed to have the pit pumped and liner replaced. Fluid level high and the liner has been compromised. Company states again that their pump truck is still broke down. A talley sheet was not provided. Paul Grims crew was informed that we would need to set a plug 50 feet below the Berea at 1085 feet.
0752013080 2006-12-11 Plug / Plug Back No Violations On 12/11/2006, it was noted that the company was having trouble pulling pipe out of the well.
0764307877 2007-02-26 Plug / Plug Back No Violations Company is still pulling 5.5 casing. No activity was observed at time of inspection.
0770999571 2007-08-13 Plug / Plug Back No Violations An inspection revealed that Paul Grims employees are tripping out of the well. They believe that their rock bit might be plugged. In addition, they state that they have gained approximately 50 feet.
0779582953 2007-08-28 Plug / Plug Back No Violations Activity observed at the well site. Mr. Paul Grims employee, Mr. Paul Thompson, states that they lost circulation at 414 feet on 8/26/2007. Also stating that on 8/27/2007, they hauled truck loads of water to regain circulation. At the time of the inspection, the drill string was stuck in the hole. The company was instructed not to plug this well over the holiday weekend.
0794460748 2006-12-11 Plug / Plug Back No Violations On 12/11/2006, it was noted that the company is having problems pulling pipe.
0869256826 2007-01-04 Plug / Plug Back No Violations The company is making an attempt to set brush and stone plug for the lime plug. The brush and stone plug got stuck inside well at a depth of 900 The company was informed that they would need to reach the required depth of 2385
0963932219 2006-12-28 Plug / Plug Back No Violations An inspection conducted on 12/29/2006 revealed that the company is having problems getting their tools out of the well. The company was also instructed to dig a pit.
0991359368 2007-08-06 Plug / Plug Back No Violations An inspection revealed that Paul Grims crew is utilizing a power swivel (installed on 8/4/2007) to mill down to the required depth. No activity observed at the time of the inspection. Made attempt to visit with Paul Grim at his shop. A mechanic for Mr. Grim stated that he left a short while ago. He states that the crew made 15 feet. Spoke with Mr. Kenny Wright whom assisted Paul Grims crew over the weekend and also loaned Mr. Grim the power swivel states that the crew made only 5 feet.
1000056686 2008-05-01 Final Restoration No Violations A follow-up inspection revealed non-compliance.
1012066323 2007-03-13 Plug / Plug Back No Violations Company is still having problems running tubing into the hole to set final plug.
1039158129 2007-06-26 Administrative Inspection No Violations An attempt was made to meet with Mr. Paul Grim. Mr. Grim was not available at the time of the visit. Mr. Grims worker, Mr. Paul Thompson, was informed that the Division of Mineral Resources Management Supervisor, Mr. Joe Hoerst, agreed that Paul Grim will not move the service rig onto another well and will need to make effort to drill deeper and set the final plug. Mr. Thompson was instructed to tell Mr. Grim to give me a call if there are any questions.
1053014419 2007-08-29 Plug / Plug Back No Violations An inspection revealed that company is having problems with circulation. Mr. Paul Grims employees state that they pull 3 joints at the conclusion of the day to prevent drill string from getting stuck.
1077829349 2004-02-24 Production Wells Violations Noted An inspection of the well revealed the well is idle and incapable of production, according to production records well has not produced for several years. All valves shut in, brush and weeds growing up in pump jack and around equipment.
1085143051 2008-03-21 Final Restoration No Violations Checked on status of final restoration. No activity observed.
1107992341 2007-08-14 Plug / Plug Back No Violations An inspection revealed that the pressure hose for the swivel will need repaired. Paul Grims employees were instructed to pump the pit and replace the liner. The company states that their pump truck is broke down and is being repaired. They were informed to contact a local contractor to have fluid hauled away.
1128619364 2008-05-19 Final Restoration No Violations A follow-up inspection revealed FR not complete.
1166132811 2006-12-05 Plug / Plug Back No Violations On 12/5/2006, the bottom hole plug was witnessed. 500 feet of clay washed into the well.
1173838615 2007-08-09 Plug / Plug Back No Violations An inspection revealed that the company is making another mill bit to aid in drilling down to required depth. Paul Grims crew states that they believe the total depth is 190 feet. They were instructed to keep a pipe talley sheet.
1183040392 2007-06-25 Administrative Inspection No Violations An administrative inspection revealed that the company has not reached the required depth. Mr. Paul Grim stated that his crew has been working on the well. Mr. Grim was informed that previous inspections have revealed no activity. Mr. Grim was asked for a pipe talley sheet. Initially, the shot/rip depth was 600 feet and would later change to 784 feet per Mr. Paul Thompson on March 8, 2007. Mr. Grim stated that he did not have a talley sheet on the recovered casing, but would provide one if needed. Furthermore, he stated that if I am a man of my word, I will stand by the initial depth of 600 feet. Mr. Grim stated that he would like to move his service rig onto another Bozett well and begin plugging. Mr. Grim was informed that the current well will need to be plugged before the rig is moved. Mr. Grim was again informed that a power swivel should be utilized on this well. Mr. Grim stated that he spoke with Mr. Kenny Wright about borrowing this tool, but didnt want to damage someone elses equipment. The contamination and pollution below the well site was again brought to Mr. Grims attention. Mr. Grim was informed that more effort will need to be placed on this well. The landowner, Mr. Jeremy Adams, would like for the wells to be plugged and company removed from the property.
1183136837 2007-05-18 Plug / Plug Back No Violations A follow-up inspection revealed that the contaminiation and pollution has been cleaned up. The source of this contaminant appears to the fluid contained inside the well which continuously migrates to this location due to the depth. The impacted area is approximately 20 feet below the well location. No activity observed at the well site. The pit liner has not been replaced and contaminant removed.
1183528383 2007-10-17 Plug / Plug Back No Violations An inspection revealed that the cement has settled approximately 12 feet. A grout mix will be placed in the well.
1183991359 2007-07-03 Plug / Plug Back No Violations An inspection revealed activity at the well site. Mr. Paul Grims crew, Mr. Paul Thompson and Mr. Pat Dougharty were having trouble drilling deeper. No progress has been made to reach required depth.
1185451624 2007-07-06 Administrative Inspection No Violations An administrative inspection revealed that Paul Grims crew is repairing the service rig.
1186587047 2007-07-23 Plug / Plug Back No Violations An inspection revealed that the company is repairing the service rig.
1190917567 2007-09-26 Plug / Plug Back No Violations Mr. Paul Grims employees state that the Varel Rock Bit continues to get plugged. They state that the current depth is approximately 500 feet with 17 joints.
1192455667 2007-10-09 Plug / Plug Back No Violations An inspection revealed that Paul Grim no longer has a power swivel. The current depth at the time of the inspection was 583 feet. The company states that they can not get down the well any further. A second talley sheet was received. It was noted that this sheet showed only 28 joints instead of 30 observed on the first talley sheet.
1213177505 2007-01-16 Plug / Plug Back No Violations An inspection conducted on 1/16/2007 revealed that the company is still trying to rip 5.5 pipe.
1265084082 2007-09-04 Plug / Plug Back No Violations Paul Grims crew state that the pump will need to be repaired. According to the crew, the current depth is 426 feet. They have also switched back to a mill bit. A talley sheet for the retrieved casing was again requested. The company states that they have not had a chance to talley the pipe.
1357237036 2007-01-29 Plug / Plug Back No Violations Checked on status of plugging. No change was observed. Company is still having trouble pulling 7 pipe.
1372109746 2007-06-15 Plug / Plug Back No Violations No activity observed at the well. Contamination and pollution still exists below the well that is being plugged.
1414488377 2007-03-08 Plug / Plug Back No Violations Company is having problems running tubing into the hole.
1418520551 2007-07-17 Plug / Plug Back No Violations An inspection revealed that Paul Grims crew is repairing drawl works on the service rig.
1422898295 2005-01-25 Production Wells No Violations Follow-up on NOV, Non-Compliance, well still incapable of production. According to landowner company has no lease and is not able to produce well. Landowner will not sign a lease and wants the well plugged. A delay of plugging has been granted to the comp
1426938645 2007-08-24 Plug / Plug Back No Violations No activity was observed at the time of the inspection. The pit needs to be pumped and liner replaced. Oil sheen observed around location below the well.
1461772656 2007-08-10 Plug / Plug Back No Violations An inspection revealed activity at the well. Mr. Paul Grims employees are making an attempt to mill down deeper. They began working at 9am this morning and have made approximately 3 feet.
1469815706 2007-05-01 Plug / Plug Back No Violations An inspection revealed no activity. C&P has not been removed from area below the well.
1474514639 2007-03-12 Plug / Plug Back No Violations Company is still having problems running tubing into the hole. No activity was observed at time of the inspection.
1505078640 2007-08-20 Plug / Plug Back No Violations Paul Grims crew state that they will be at 310 feet once the current joint is drilled down into the hole. They were informed to have the pit pumped and liner replaced. Fluid level high and the liner has been compromised. Company states again that their pump truck is broke down. In addition, they state that talley sheet will be provided tomorrow.
1629731035 2007-05-03 Plug / Plug Back No Violations No activity observed.
1648580094 2007-08-27 Plug / Plug Back No Violations No activity was observed at the time of the inspection. The pit has been pumped and liner replaced.
1650824828 2007-02-22 Plug / Plug Back No Violations Checked on plugging. No activity observed. Spoke with Paul Grims helper whom stated that they have pulled on pipe and 8 is also coming with the 7 and 5. He was given the required plugs since they ripped pipe above the Berea formation. Paul Grims helper was also instructed to run tubing immediately after pulling the casing to avoid cave-in. If requirement is delayed and tubing can not reach required depth, they will be required to drill down to this pipe tally depth.
1682168106 2008-04-02 Final Restoration No Violations Met with Paul Grims employees at well site to discuss final restoration requirements. Mr. Grims employee was also informed that a landowner waiver has not been received for vegetative cover around well site and the lease road. Mr. Grims employee was informed that if a waiver is not received, they will need to seed and straw areas.
1687359198 2007-06-05 Plug / Plug Back No Violations No activity observed at the well site.
1737683732 2007-07-02 Plug / Plug Back No Violations An inpsection revealed no activity observed at the well site.
1780776760 2007-01-17 Plug / Plug Back No Violations An inspection revealed that service rig still needs repaired. No activity was observed.
1798488863 2007-07-06 Administrative Inspection No Violations An administrative inspection revealed that the company is repairing the service rig. Mr. Paul Thompson states that the back of the drawl works (attached to the mast) is bent and will need repaired.
1953962125 2007-01-05 Plug / Plug Back No Violations The company placed brush and stone plug for the lime plug at the required depth of 2385 250 of clay was washed into the hole.
1993194513 2007-09-07 Plug / Plug Back No Violations An inspection revealed no activity at the well site. The company is still broke down.
2022898350 2007-11-19 Final Restoration No Violations An inspection revealed that Paul Grim is working on final restoration.
206254081 2007-9-17 0:00: PB No Violations
2086023468 2007-05-30 Plug / Plug Back No Violations An inspection revealed non-compliance. Contamination and pollution exists in the same location that had been cleaned up. No activity observed at the well site.
2091978877 2007-10-16 Plug / Plug Back No Violations Witnessed cement placed from 586 feet to the surface. This well has now been plugged.
2125054986 2006-12-13 Plug / Plug Back No Violations Checked on status of plugging. No change was observed. Company is still having trouble pulling pipe.
2131205571 2007-05-18 Plug / Plug Back No Violations No activity at the well site.
3080695 2008-6-10 0:00: FR No Violations
337212012 2007-1-3 0:00:0 PB No Violations
40325971 2004-2-24 0:00: PW No Violations
40975803 2007-2-15 0:00: PB No Violations
483174573 2007-11-8 0:00: FR No Violations
571289577 2006-4-19 0:00: PW No Violations
752013080 2006-12-11 0:00 PB No Violations
770999571 2007-8-13 0:00: PB No Violations
794460748 2006-12-11 0:00 PB No Violations
869256826 2007-1-4 0:00:0 PB No Violations
91391731 2007-8-16 0:00: PB No Violations
963932219 2006-12-28 0:00 PB No Violations
991359368 2007-8-6 0:00:0 PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0001754705 US-OH-117458 2007-04-10 Pollution and contamination
0001754705 US-OH-117459 2007-04-10 Pit incapable of preventing escape of brine or other wastes
0040325971 US-OH-124292 2004-02-26 Well shall be plugged
1077829349 US-OH-101683 2004-02-26 Well shall be plugged

For data sources see[7]

References