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Difference between revisions of "34-019-20660"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-019-20660
 
| Well ID: 34-019-20660
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.5996375038, -81.2606322443 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.59, -81.26 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| Country: United States
 
|-
 
|-
| Municipality:
+
| State: Ohio
 
|-
 
|-
| Operator Name:
+
| County: [[Carroll_County,_Ohio|Carroll]]
 
|-
 
|-
| Well Pad ID:
+
| Municipality: [[Rose_Township,_Carroll_County,_Ohio|Rose Township]]
 
|-
 
|-
| Farm/Lease Name:
+
| Operator Name: [[WADDY & SON OILFIELD SERVICES]]
 
|-
 
|-
| First Permit Date:
+
| Well Pad ID:  
 
|-
 
|-
| Last Permit Date:
+
| Farm/Lease Name: KING W M & N M
 
|-
 
|-
| Spud Date:
+
| License Status: Producing
 
|-
 
|-
| Unconventional:
+
| License Date: 1972-11-01
 
|-
 
|-
| Horizontal:
+
| Spud Date:  
 
|-
 
|-
| Producing: No
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Violations: 2
+
| Final Drill Date: 1972-11-19
 
|-
 
|-
| Latitude: 40.5996375038
+
| Well Total Depth: 5386.00 ft
 
|-
 
|-
| Longitude: -81.2606322443
+
| Configuration: Vertical
 +
|-
 +
| Latitude: 40.590000
 +
|-
 +
| Longitude: -81.260000
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Oil and Gas
 +
| 1802-01-01
 +
| Issued Date 10/27/72 Expired Date  Acres  Tool Type  Proposed Formation  Proposed Depth  Proposed Drill Depth
 +
|-
 +
| Completed
 +
| 1972-11-19
 +
| GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
 +
|-
 +
| Reached Total Depth
 +
| 1972-11-19
 +
| GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
 +
|-
 +
| Construction Permit Expires
 +
| 1973-10-27
 +
| GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
 +
|-
 +
| CO
 +
| 1990-04-17
 +
| 1976    WADDY & SON OILFLD SER IN
 +
|-
 +
| Record Last Modified
 +
| 2013-10-03
 +
| GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
+
|-
!scope="col" | OIL PRODUCTION DAYS
+
| 1982
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 668.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1983
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 588.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1984
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 537.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 442.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1986
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 226.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1987
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 184.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1988
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 83.00
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1989
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 49.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1990
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 1253.00
 +
| style="text-align: right;" | 573.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 2668.00
 +
| style="text-align: right;" | 345.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 2752.00
 +
| style="text-align: right;" | 313.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 2746.00
 +
| style="text-align: right;" | 329.00
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 4.00
 +
| style="text-align: right;" | 258.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2001
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 1250.00
 +
| style="text-align: right;" | 220.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2002
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 841.00
 +
| style="text-align: right;" | 229.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2003
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 412.00
 +
| style="text-align: right;" | 160.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2004
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 383.00
 +
| style="text-align: right;" | 140.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2005
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 425.00
 +
| style="text-align: right;" | 162.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2006
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 400.00
 +
| style="text-align: right;" | 94.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2007
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 314.00
 +
| style="text-align: right;" | 138.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2008
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 295.00
 +
| style="text-align: right;" | 109.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2009
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 275.00
 +
| style="text-align: right;" | 211.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2010
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 333.00
 +
| style="text-align: right;" | 80.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2011
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 329.00
 +
| style="text-align: right;" | 165.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2012
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 250.00
 +
| style="text-align: right;" | 80.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2013
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 248.00
 +
| style="text-align: right;" | 73.00
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2014
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 70.00
 +
| style="text-align: right;" | 113.00
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2015
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 121.00
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2016
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 20.00
 +
| style="text-align: right;" | 83.00
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2017
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 12.00
 +
| style="text-align: right;" | 120.00
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2018
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| style="text-align: right;" | 15.00
 +
| style="text-align: right;" | 93.00
 +
| style="text-align: right;" | 50
 +
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
{| class="wikitable sortable" width="95%"
+
{| class="wikitable sortable"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | TYPE
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | QUANTITY
+
!scope="col" style="text-align: center"| Waste Type
!scope="col" | UNITS
+
!scope="col" style="text-align: center"| Quantity (bbl)
!scope="col" | DISPOSAL METHOD
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | WASTE FACILITY PERMIT ID
+
|-
!scope="col" | WASTE FACILITY NAME
+
| 1982
!scope="col" | FACILITY CITY
+
| [[WADDY & SON OILFIELD SERVICES]]
!scope="col" | FACILITY STATE
+
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1983
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1984
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1986
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1987
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1988
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1989
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1990
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 200
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1991
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 89
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 93
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 59
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 240
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2001
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 185
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2002
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 120
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2003
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 170
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2004
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 64
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2005
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 54
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2006
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 51
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2007
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 56
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2008
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 25
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2009
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 20
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2010
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 18
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2011
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 17
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2012
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 25
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2013
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 21
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2014
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 50
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2015
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 35
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2016
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 65
 +
| style="text-align: right;" | 48
 +
|-
 +
| 2017
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 44
 +
| style="text-align: right;" | 50
 +
|-
 +
| 2018
 +
| [[WADDY & SON OILFIELD SERVICES]]
 +
| Brine
 +
| style="text-align: right;" | 49
 +
| style="text-align: right;" | 50
 +
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Production Table - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
 
| -395668451
 
| -395668451
 +
| 2010-6-22 0:00:
 +
| PW
 +
| No Violations
 +
| 2.50
 +
|-
 +
| 0395668451
 
| 2010-06-22
 
| 2010-06-22
|
+
| Production Wells
 +
| No Violations
 
| Follow-up inspection revealed that the operator has started on the brine spill clean-up. The operator has started pushing the brine contaminated topsoil into a pile below the tank battery. The operator has also started removing the brine saturated soil from inside the tank battery SPCC dike. He has placed a pile of dirt  downslope from the tank battery to prevent any other brine from escaping past that point if it rains and any brine might possibly be flushed out of the ground. Mike Noble advised me that they should be completely finished with the remedial work within the couple of weeks.
 
| Follow-up inspection revealed that the operator has started on the brine spill clean-up. The operator has started pushing the brine contaminated topsoil into a pile below the tank battery. The operator has also started removing the brine saturated soil from inside the tank battery SPCC dike. He has placed a pile of dirt  downslope from the tank battery to prevent any other brine from escaping past that point if it rains and any brine might possibly be flushed out of the ground. Mike Noble advised me that they should be completely finished with the remedial work within the couple of weeks.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1006055948
 
| 1006055948
 
| 2010-06-14
 
| 2010-06-14
|
+
| Production Wells
| I was contacted by Mike Noble with Waddy & Son that they had a brine spill at the King tank battery (common tank battery for 4 King wells). He advised that it traveled thru the dike and downslope and then into the road ditch. I arrived on site and found that the plastic line running into the top of the brine tank had come off the back of the oil storage tank. The line was hanging down in the plastic brine storage tank and when it came off the oil storage tank and  it allowed the brine to be siphoned out of the plastic brine storage tank and into the dike area. There was no oil spilled siphoned out of the brine storage tank. The brine traveled thru the SPCC dike and downslope approximately 90' to 100' and then into the road ditch. The vegetation is dead outside the dike and on the downslope below the tank battery. There is a very minimal amount of dead vegetation in the road ditch therefore it appears that a very small amount of brine ever actually made it to the road ditch. I spoke with Mike Noble and he advised that they are going to start clean-up and dike repair later this week. I advised that I would check back on the clean-up progress later next week. I advised him that they needed to have all the remedial work completed by July 16th, 2010.
+
| Violations Noted
|
+
| I was contacted by Mike Noble with Waddy & Son that they had a brine spill at the King tank battery (common tank battery for 4 King wells). He advised that it traveled thru the dike and downslope and then into the road ditch. I arrived on site and found that the plastic line running into the top of the brine tank had come off the back of the oil storage tank. The line was hanging down in the plastic brine storage tank and when it came off the oil storage tank and  it allowed the brine to be siphoned out of the plastic brine storage tank and into the dike area. There was no oil spilled siphoned out of the brine storage tank. The brine traveled thru the SPCC dike and downslope approximately 90 to 100 and then into the road ditch. The vegetation is dead outside the dike and on the downslope below the tank battery. There is a very minimal amount of dead vegetation in the road ditch therefore it appears that a very small amount of brine ever actually made it to the road ditch. I spoke with Mike Noble and he advised that they are going to start clean-up and dike repair later this week. I advised that I would check back on the clean-up progress later next week. I advised him that they needed to have all the remedial work completed by July 16th, 2010.
| 9-1-07
 
|
 
|-
 
 
|-
 
|-
 
| 1389659996
 
| 1389659996
 
| 2014-01-13
 
| 2014-01-13
|
+
| Production Wells
 +
| Violations Noted
 
| I was on site to conduct a follow-up inspection on a verbal violation issued on 06/14/2010 with a compliance date of 07/16/2010. The follow-up inspection revealed that the operator has removed  the contaminated soils from the site. The violation has been corrected and there are no violations at this time. --------------------------------  RESOLVED ----------------------
 
| I was on site to conduct a follow-up inspection on a verbal violation issued on 06/14/2010 with a compliance date of 07/16/2010. The follow-up inspection revealed that the operator has removed  the contaminated soils from the site. The violation has been corrected and there are no violations at this time. --------------------------------  RESOLVED ----------------------
|
+
|-
| 9-1-07
+
| 1395323460
|
+
| 2017-12-28
 +
| Production Wells
 +
| No Violations
 +
| The well is equipped with an electrically-driven pumping unit.  The tank battery is shared with PN# (20295, 20742,  & 21038), and identification for all four wells was posted.  The tank battery consists of one 210 bbl production tank, two vertical separators, one 50 bbl poly brine tank.  The load line to the tanks production valve was secured with a plug. The access road was stable and drivable.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
| 1006055948
 +
| US-OH-100052
 +
| 2010-07-27
 +
|
 +
| Well operation causing pollution and contamination
 +
|-
 +
| 1389659996
 +
| US-OH-111519
 +
| 2014-02-05
 +
|
 +
| Well operation causing pollution and contamination
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2020-11-16
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-11-16 }}</ref>
 +
==References==
 +
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Latest revision as of 21:40, 12 January 2021

Well Details

Well ID: 34-019-20660
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: WADDY & SON OILFIELD SERVICES
Well Pad ID:
Farm/Lease Name: KING W M & N M
License Status: Producing
License Date: 1972-11-01
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1972-11-19
Well Total Depth: 5386.00 ft
Configuration: Vertical
Latitude: 40.590000
Longitude: -81.260000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1802-01-01 Issued Date 10/27/72 Expired Date Acres Tool Type Proposed Formation Proposed Depth Proposed Drill Depth
Completed 1972-11-19 GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
Reached Total Depth 1972-11-19 GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
Construction Permit Expires 1973-10-27 GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.
CO 1990-04-17 1976 WADDY & SON OILFLD SER IN
Record Last Modified 2013-10-03 GL=1061.3, KB=1-69.3 IP. AMOUNTS FOUND IN SR.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1982 WADDY & SON OILFIELD SERVICES 0.00 668.00 0
1983 WADDY & SON OILFIELD SERVICES 0.00 588.00 0
1984 WADDY & SON OILFIELD SERVICES 0.00 537.00 0
1985 WADDY & SON OILFIELD SERVICES 0.00 442.00 0
1986 WADDY & SON OILFIELD SERVICES 0.00 226.00 0
1987 WADDY & SON OILFIELD SERVICES 0.00 184.00 0
1988 WADDY & SON OILFIELD SERVICES 0.00 83.00 0
1989 WADDY & SON OILFIELD SERVICES 0.00 49.00 365
1990 WADDY & SON OILFIELD SERVICES 1253.00 573.00 365
1991 WADDY & SON OILFIELD SERVICES 2668.00 345.00 365
1992 WADDY & SON OILFIELD SERVICES 2752.00 313.00 365
1993 WADDY & SON OILFIELD SERVICES 2746.00 329.00 365
2000 WADDY & SON OILFIELD SERVICES 4.00 258.00 50
2001 WADDY & SON OILFIELD SERVICES 1250.00 220.00 50
2002 WADDY & SON OILFIELD SERVICES 841.00 229.00 50
2003 WADDY & SON OILFIELD SERVICES 412.00 160.00 50
2004 WADDY & SON OILFIELD SERVICES 383.00 140.00 50
2005 WADDY & SON OILFIELD SERVICES 425.00 162.00 50
2006 WADDY & SON OILFIELD SERVICES 400.00 94.00 50
2007 WADDY & SON OILFIELD SERVICES 314.00 138.00 50
2008 WADDY & SON OILFIELD SERVICES 295.00 109.00 50
2009 WADDY & SON OILFIELD SERVICES 275.00 211.00 50
2010 WADDY & SON OILFIELD SERVICES 333.00 80.00 50
2011 WADDY & SON OILFIELD SERVICES 329.00 165.00 50
2012 WADDY & SON OILFIELD SERVICES 250.00 80.00 50
2013 WADDY & SON OILFIELD SERVICES 248.00 73.00 48
2014 WADDY & SON OILFIELD SERVICES 70.00 113.00 48
2015 WADDY & SON OILFIELD SERVICES 0.00 121.00 48
2016 WADDY & SON OILFIELD SERVICES 20.00 83.00 48
2017 WADDY & SON OILFIELD SERVICES 12.00 120.00 50
2018 WADDY & SON OILFIELD SERVICES 15.00 93.00 50

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1982 WADDY & SON OILFIELD SERVICES Brine 0 0
1983 WADDY & SON OILFIELD SERVICES Brine 0 0
1984 WADDY & SON OILFIELD SERVICES Brine 0 0
1985 WADDY & SON OILFIELD SERVICES Brine 0 0
1986 WADDY & SON OILFIELD SERVICES Brine 0 0
1987 WADDY & SON OILFIELD SERVICES Brine 0 0
1988 WADDY & SON OILFIELD SERVICES Brine 0 0
1989 WADDY & SON OILFIELD SERVICES Brine 0 365
1990 WADDY & SON OILFIELD SERVICES Brine 200 365
1991 WADDY & SON OILFIELD SERVICES Brine 89 365
1992 WADDY & SON OILFIELD SERVICES Brine 93 365
1993 WADDY & SON OILFIELD SERVICES Brine 59 365
2000 WADDY & SON OILFIELD SERVICES Brine 240 50
2001 WADDY & SON OILFIELD SERVICES Brine 185 50
2002 WADDY & SON OILFIELD SERVICES Brine 120 50
2003 WADDY & SON OILFIELD SERVICES Brine 170 50
2004 WADDY & SON OILFIELD SERVICES Brine 64 50
2005 WADDY & SON OILFIELD SERVICES Brine 54 50
2006 WADDY & SON OILFIELD SERVICES Brine 51 50
2007 WADDY & SON OILFIELD SERVICES Brine 56 50
2008 WADDY & SON OILFIELD SERVICES Brine 25 50
2009 WADDY & SON OILFIELD SERVICES Brine 20 50
2010 WADDY & SON OILFIELD SERVICES Brine 18 50
2011 WADDY & SON OILFIELD SERVICES Brine 17 50
2012 WADDY & SON OILFIELD SERVICES Brine 25 50
2013 WADDY & SON OILFIELD SERVICES Brine 21 48
2014 WADDY & SON OILFIELD SERVICES Brine 50 48
2015 WADDY & SON OILFIELD SERVICES Brine 35 48
2016 WADDY & SON OILFIELD SERVICES Brine 65 48
2017 WADDY & SON OILFIELD SERVICES Brine 44 50
2018 WADDY & SON OILFIELD SERVICES Brine 49 50

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-395668451 2010-6-22 0:00: PW No Violations 2.50
0395668451 2010-06-22 Production Wells No Violations Follow-up inspection revealed that the operator has started on the brine spill clean-up. The operator has started pushing the brine contaminated topsoil into a pile below the tank battery. The operator has also started removing the brine saturated soil from inside the tank battery SPCC dike. He has placed a pile of dirt downslope from the tank battery to prevent any other brine from escaping past that point if it rains and any brine might possibly be flushed out of the ground. Mike Noble advised me that they should be completely finished with the remedial work within the couple of weeks.
1006055948 2010-06-14 Production Wells Violations Noted I was contacted by Mike Noble with Waddy & Son that they had a brine spill at the King tank battery (common tank battery for 4 King wells). He advised that it traveled thru the dike and downslope and then into the road ditch. I arrived on site and found that the plastic line running into the top of the brine tank had come off the back of the oil storage tank. The line was hanging down in the plastic brine storage tank and when it came off the oil storage tank and it allowed the brine to be siphoned out of the plastic brine storage tank and into the dike area. There was no oil spilled siphoned out of the brine storage tank. The brine traveled thru the SPCC dike and downslope approximately 90 to 100 and then into the road ditch. The vegetation is dead outside the dike and on the downslope below the tank battery. There is a very minimal amount of dead vegetation in the road ditch therefore it appears that a very small amount of brine ever actually made it to the road ditch. I spoke with Mike Noble and he advised that they are going to start clean-up and dike repair later this week. I advised that I would check back on the clean-up progress later next week. I advised him that they needed to have all the remedial work completed by July 16th, 2010.
1389659996 2014-01-13 Production Wells Violations Noted I was on site to conduct a follow-up inspection on a verbal violation issued on 06/14/2010 with a compliance date of 07/16/2010. The follow-up inspection revealed that the operator has removed the contaminated soils from the site. The violation has been corrected and there are no violations at this time. -------------------------------- RESOLVED ----------------------
1395323460 2017-12-28 Production Wells No Violations The well is equipped with an electrically-driven pumping unit. The tank battery is shared with PN# (20295, 20742, & 21038), and identification for all four wells was posted. The tank battery consists of one 210 bbl production tank, two vertical separators, one 50 bbl poly brine tank. The load line to the tanks production valve was secured with a plug. The access road was stable and drivable.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1006055948 US-OH-100052 2010-07-27 Well operation causing pollution and contamination
1389659996 US-OH-111519 2014-02-05 Well operation causing pollution and contamination

For data sources see[7]

References