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Difference between revisions of "37-127-20021"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-127-20021
 
| Well ID: 37-127-20021
| style="height=100%; align=center" rowspan="14" | {{#display_map: 41.936969, -75.467963 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.936969, -75.467963 | width=100% | height=100% }}  
 
|-
 
|-
 
| County: [[Wayne County, Pennsylvania|Wayne]]
 
| County: [[Wayne County, Pennsylvania|Wayne]]
Line 9: Line 9:
 
| Municipality: [[Scott Township, Wayne County, Pennsylvania|Scott Township]]
 
| Municipality: [[Scott Township, Wayne County, Pennsylvania|Scott Township]]
 
|-
 
|-
| Operator Name: [[HESS CORP|HESS CORP]]
+
| Operator Name: [[HESS CORP]]
 
|-
 
|-
| Well Pad ID: [[147385]]
+
| Well Pad ID: [[147385|147385]]
 
|-
 
|-
 
| Farm/Lease Name: MILLER 1V
 
| Farm/Lease Name: MILLER 1V
Line 25: Line 25:
 
| Horizontal: No
 
| Horizontal: No
 
|-
 
|-
| Producing: No
+
| Well Status: ACTIVE
 
|-
 
|-
| Violations: None
+
| Violations: 0
 
|-
 
|-
 
| Latitude: 41.936969
 
| Latitude: 41.936969
 
|-
 
|-
 
| Longitude: -75.467963
 
| Longitude: -75.467963
|-
 
|}
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | INSPECTION ID
 
!scope="col" | DATE
 
!scope="col" | DESCRIPTION
 
!scope="col" | COMMENT
 
!scope="col" | VIOLATION ID
 
|-
 
| 1912374
 
| 2010-09-08
 
| No Violations Noted
 
| H&P 272.  Drill on air to 6000 and then coring.  Have 13 3/8" set to 750 and cemented.  Have open tops for fluid and cuttings and discussed with CO. Man that 2' freeboard must be maintained in open tops.  Secondary containment = plastic under entire substructure and cuttings handling area.
 
|
 
|-
 
|-
 
| 1917633
 
| 2010-10-04
 
| No Violations Noted
 
| H&P 272. Depth of drilling 6988'.  TD is 7075'.  Coring is complete.  BOP's tested and charts look ok.  Cemented 13 3/8" and 9 5/9" with returns reported on both strings.  Will set 5 1/2" at TD.
 
|
 
|-
 
|-
 
| 1939207
 
| 2010-12-12
 
| No Violations Noted
 
|
 
|
 
|-
 
|-
 
| 2009762
 
| 2011-10-11
 
| No Violations Noted
 
| DEP on site at 15:30.  Operator is filing for Inactive Status.  Site secured with gated entrance.  Well is temporarily plugged.  Protective steel barricades are in place around well head.  No evidence of gas leaking in cellar.  Gauges on annuli both read 0 psi.  E&S controls appear to be in place and working sufficiently.  No one on site at time of inspection.  Site ID sign has been torn down and is laying on ground at entrance to site.
 
|
 
|-
 
|-
 
| 2113241
 
| 2012-10-25
 
| No Violations Noted
 
| Key Ind. Service Rig on site.  Duncan Hatch - Co. Man on site.  Have cut 5 1/2" casing at 1900' and at 1895'.  TOC estimated to be at 1950'.  Tried pulling casing - were unsuccessful.  Plan is to make another cut at 1500' and try to pull casing.  Will then set a 100' plug of cement and CIBP at 1500', come up hole and set top plug at @835' (100' below surface casing shoe).  Will top off with gravel to surface and cap well.  No violations at this time.
 
|
 
 
|-
 
|-
 
|}
 
|}
Line 87: Line 44:
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 
|-
 
|-
| 2012-2
+
| 2010-3
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2010-2
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 96: Line 62:
 
|-
 
|-
 
|-
 
|-
| 2012-1
+
| 2010-2
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 114: Line 80:
 
|-
 
|-
 
|-
 
|-
| 2010-2
+
| 2012-1
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 123: Line 89:
 
|-
 
|-
 
|-
 
|-
| 2010-3
+
| 2012-2
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 132: Line 98:
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Oil and Gas Historical Production Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Production
 +
| accessdate = 2015-05-27 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 143: Line 115:
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
!scope="col" | FACILITY STATE
 +
|-
 +
| 2010-2
 +
| DRILL CUTTINGS
 +
| style="text-align:right;" | 456.0
 +
| Tons
 +
| LANDFILL
 +
| 301626
 +
| WHITE PINES LANDFILL
 +
| MILLVILLE
 +
| PA
 +
|-
 
|-
 
|-
 
| 2010-2
 
| 2010-2
 
| DRILLING FLUID WASTE
 
| DRILLING FLUID WASTE
| style="text-align:right;" | 5143.0
+
| style="text-align:right;" | 5.0
 
| Bbl
 
| Bbl
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| CENTRALIZED TREATMENT PLANT FOR RECYCLE
 
| WMGR119
 
| WMGR119
| EUREKA RESOURCES (WILLIAMSPORT WATER TREATMENT)
+
| EUREKA RESOURCES LLC WILLIAMSPORT WATER TREATMENT
 
| WILLIAMSPORT
 
| WILLIAMSPORT
 
| PA
 
| PA
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Oil and Gas Historical Waste Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Waste
 +
| accessdate = 2015-05-26 }}</ref>
 +
== Inspection Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | INSPECTION ID
 +
!scope="col" | DATE
 +
!scope="col" | DESCRIPTION
 +
!scope="col" | COMMENT
 +
!scope="col" | VIOLATION ID
 +
!scope="col" | VIOLATION CODE
 +
!scope="col" | VIOLATION_COMMENT
 +
|-
 +
| 1912374
 +
| 2010-09-08
 +
| No Violations Noted
 +
| H&P 272.  Drill on air to 6000 and then coring.  Have 13 3/8" set to 750 and cemented.  Have open tops for fluid and cuttings and discussed with CO. Man that 2' freeboard must be maintained in open tops.  Secondary containment = plastic under entire substructure and cuttings handling area.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1917633
 +
| 2010-10-04
 +
| No Violations Noted
 +
| H&P 272. Depth of drilling 6988'.  TD is 7075'.  Coring is complete.  BOP's tested and charts look ok.  Cemented 13 3/8" and 9 5/9" with returns reported on both strings.  Will set 5 1/2" at TD.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1939207
 +
| 2010-12-12
 +
| No Violations Noted
 +
|
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2009762
 +
| 2011-10-11
 +
| No Violations Noted
 +
| DEP on site at 15:30.  Operator is filing for Inactive Status.  Site secured with gated entrance.  Well is temporarily plugged.  Protective steel barricades are in place around well head.  No evidence of gas leaking in cellar.  Gauges on annuli both read 0 psi.  E&S controls appear to be in place and working sufficiently.  No one on site at time of inspection.  Site ID sign has been torn down and is laying on ground at entrance to site.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2113241
 +
| 2012-10-25
 +
| No Violations Noted
 +
| Key Ind. Service Rig on site.  Duncan Hatch - Co. Man on site.  Have cut 5 1/2" casing at 1900' and at 1895'.  TOC estimated to be at 1950'.  Tried pulling casing - were unsuccessful.  Plan is to make another cut at 1500' and try to pull casing.  Will then set a 100' plug of cement and CIBP at 1500', come up hole and set top plug at @835' (100' below surface casing shoe).  Will top off with gravel to surface and cap well.  No violations at this time.
 +
|
 +
|
 +
|
 
|-
 
|-
 
|-
 
|-
| 2010-2
+
| 2173552
| DRILL CUTTINGS
+
| 2013-06-07
| style="text-align:right;" | 456.0
+
| No Violations Noted
| Tons
+
| Inspection conducted on 6/7/13 with Bob Wrazen, URS and Dean Jameson, Hess of the Miller Pad.  Inspection based on site visit to discuss pad reclamation requirements.  Hess is expecting to pick a contractor to reclaim the pad within the next week.  The Department will allow the access road to stay if the land owner so desires.  An inspection of the existing silt sock revealed that new silt sock will need to be installed up gradient of the existing silt sock.  Well has been plugged.  Site is temporarily stabilized at this time.
| LANDFILL
+
|  
| 301626
+
|  
| WHITE PINES LANDFILL
+
|  
| MILLVILLE
 
| PA
 
 
|-
 
|-
 
|}
 
|}
==References==
+
For data sources see<ref>{{cite web
{{Reflist}}
+
| title = Oil and Gas Historical Inspection Report
 
+
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Inspections
 +
| accessdate = 2015-05-27 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 05:22, 25 June 2015

Well Details

Well ID: 37-127-20021
Loading map...
County: Wayne
Municipality: Scott Township
Operator Name: HESS CORP
Well Pad ID: 147385
Farm/Lease Name: MILLER 1V
First Permit Date: 2010-07-28
Last Permit Date: 2010-07-28
Spud Date: 2010-08-03
Unconventional: Yes
Horizontal: No
Well Status: ACTIVE
Violations: 0
Latitude: 41.936969
Longitude: -75.467963

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-3 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2010-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 0.0 0.0 0.0 0.0 0.0 0.0
2012-2 0.0 0.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2010-2 DRILL CUTTINGS 456.0 Tons LANDFILL 301626 WHITE PINES LANDFILL MILLVILLE PA
2010-2 DRILLING FLUID WASTE 5.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119 EUREKA RESOURCES LLC WILLIAMSPORT WATER TREATMENT WILLIAMSPORT PA

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1912374 2010-09-08 No Violations Noted H&P 272. Drill on air to 6000 and then coring. Have 13 3/8" set to 750 and cemented. Have open tops for fluid and cuttings and discussed with CO. Man that 2' freeboard must be maintained in open tops. Secondary containment = plastic under entire substructure and cuttings handling area.
1917633 2010-10-04 No Violations Noted H&P 272. Depth of drilling 6988'. TD is 7075'. Coring is complete. BOP's tested and charts look ok. Cemented 13 3/8" and 9 5/9" with returns reported on both strings. Will set 5 1/2" at TD.
1939207 2010-12-12 No Violations Noted
2009762 2011-10-11 No Violations Noted DEP on site at 15:30. Operator is filing for Inactive Status. Site secured with gated entrance. Well is temporarily plugged. Protective steel barricades are in place around well head. No evidence of gas leaking in cellar. Gauges on annuli both read 0 psi. E&S controls appear to be in place and working sufficiently. No one on site at time of inspection. Site ID sign has been torn down and is laying on ground at entrance to site.
2113241 2012-10-25 No Violations Noted Key Ind. Service Rig on site. Duncan Hatch - Co. Man on site. Have cut 5 1/2" casing at 1900' and at 1895'. TOC estimated to be at 1950'. Tried pulling casing - were unsuccessful. Plan is to make another cut at 1500' and try to pull casing. Will then set a 100' plug of cement and CIBP at 1500', come up hole and set top plug at @835' (100' below surface casing shoe). Will top off with gravel to surface and cap well. No violations at this time.
2173552 2013-06-07 No Violations Noted Inspection conducted on 6/7/13 with Bob Wrazen, URS and Dean Jameson, Hess of the Miller Pad. Inspection based on site visit to discuss pad reclamation requirements. Hess is expecting to pick a contractor to reclaim the pad within the next week. The Department will allow the access road to stay if the land owner so desires. An inspection of the existing silt sock revealed that new silt sock will need to be installed up gradient of the existing silt sock. Well has been plugged. Site is temporarily stabilized at this time.

For data sources see[3]

References