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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-099-21010 | | Well ID: 34-099-21010 | ||
+ | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.07595195, -80.79443683 | width=100% | height=100% }} | ||
|- | |- | ||
− | | County: | + | | County: [[Mahoning County, Ohio|Mahoning]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[D & L ENERGY INC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: 1978-04-27 |
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: | + | | Latitude: 41.07595195 |
|- | |- | ||
− | | Longitude: | + | | Longitude: -80.79443683 |
|- | |- | ||
|} | |} | ||
Line 42: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1984-0 | ||
+ | | style="text-align:right;" | 2819.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1985-0 | ||
+ | | style="text-align:right;" | 2966.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1986-0 | ||
+ | | style="text-align:right;" | 2977.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1987-0 | ||
+ | | style="text-align:right;" | 2841.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1988-0 | ||
+ | | style="text-align:right;" | 2992.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 63.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1989-0 | ||
+ | | style="text-align:right;" | 2146.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1990-0 | ||
+ | | style="text-align:right;" | 863.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1991-0 | ||
+ | | style="text-align:right;" | 925.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1992-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1993-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1998-0 | ||
+ | | style="text-align:right;" | 2351.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1999-0 | ||
+ | | style="text-align:right;" | 2553.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 49.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2000-0 | ||
+ | | style="text-align:right;" | 3755.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2001-0 | ||
+ | | style="text-align:right;" | 2813.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 27.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2002-0 | ||
+ | | style="text-align:right;" | 2486.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2003-0 | ||
+ | | style="text-align:right;" | 2567.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2004-0 | ||
+ | | style="text-align:right;" | 1381.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 40.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 1252.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2006-0 | ||
+ | | style="text-align:right;" | 1880.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 1755.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 1993.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 36.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 1859.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 1913.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 1143.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 2041.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 12.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 1001.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 63: | Line 292: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | 1409664166 | ||
+ | | 2014-05-28 | ||
+ | | | ||
+ | | I was on location with Wade Balser from the Ohio EPA to follow up on the clean up operation from the brine and oil release that was reported on 5/27/2014. KDA is on location with equipment to start the clean up . Water trucks are vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. Wade and I walked from the tank battery to the pond and found that the vegetation and soil along the ditch has to be removed. All fluids were contained inside the pond. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1409667711 | ||
+ | | 2014-05-29 | ||
+ | | | ||
+ | | I was on location with Wade Balser from the Ohio EPA to follow up on the clean up operation from the brine and oil release that was reported on 5/27/2014. KDA is on location with equipment to start the clean up . Water trucks are vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. The clean up is progressing slowly. The backhoe is pulling the vegetation away from the edge of the pond that has oil residue on it and putting it into containers. After they remove this they will finish vacuuming the pond. Wade Balser from the Ohio EPA has finished his inspection. The tank battery consist of one 35 barrel tank and one vertical separator. The well is equipped with 1.5 tubing. Well is shut in at this time. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1409747123 | ||
+ | | 2014-06-13 | ||
+ | | | ||
+ | | I was on location to perform a follow up inspection. KDA is on location with equipment performing the clean up. The clean up is progressing slowly. The tank battery consist of one 35 barrel tank and one vertical separator. The well is equipped with 1.5 tubing. Well is shut in at this time. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1426943527 | ||
+ | | 2015-03-16 | ||
+ | | | ||
+ | | I performed a follow up inspection on this location. Compliance Notice dated 5/27/2014 #1401722020 can be closed. Vegetation has been established in all of the disturbed areas. Landscape has been replaced. Dike has been rebuild. The tank battery is equipped with one (1) 35 barrel poly tank and one (1) horizontal separator. The well is an 1.5 plunger lift. ID signs are posted. No noted violations at this time. This Compliance Notice is closed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -1665132347 | ||
+ | | 2014-06-03 | ||
+ | | | ||
+ | | I was on location to perform a follow up inspection. KDA is on location with equipment performing the clean up . Water trucks are finishing vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. The clean up is progressing slowly. The tank battery consist of one 35 barrel tank and one vertical separator. The well is equipped with 1.5 tubing. Well is shut in at this time. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
|- | |- | ||
| -1895400299 | | -1895400299 | ||
| 2012-02-09 | | 2012-02-09 | ||
− | | | + | | |
| On 02/06/2012, DNR Inspector Richard Skidmore completed a production well inspection status check for DNR Inspector Chris Grimm. The lease road, tank battery, and well head locations are in compliance with 1501:9-9-05. Inspection passed. | | On 02/06/2012, DNR Inspector Richard Skidmore completed a production well inspection status check for DNR Inspector Chris Grimm. The lease road, tank battery, and well head locations are in compliance with 1501:9-9-05. Inspection passed. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -19173415 | ||
+ | | 2014-06-05 | ||
+ | | | ||
+ | | I was on location to perform a follow up inspection. KDA is on location with equipment performing the clean up . Water trucks are finishing vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. The clean up is progressing slowly. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 856949538 | | 856949538 | ||
| 2009-09-18 | | 2009-09-18 | ||
− | | | + | | |
| I GPS'd both the wellhead and the tank battery for the first time. I continued my walk around the tank battery and the wellhead and found that there were no violations at this time. | | I GPS'd both the wellhead and the tank battery for the first time. I continued my walk around the tank battery and the wellhead and found that there were no violations at this time. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-099-21010 | Loading map...
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County: Mahoning | |
Municipality: | |
Operator Name: D & L ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1978-04-27 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.07595195 | |
Longitude: -80.79443683 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 2819.0 | 0.0 | ||||
1985-0 | 2966.0 | 0.0 | ||||
1986-0 | 2977.0 | 0.0 | ||||
1987-0 | 2841.0 | 0.0 | ||||
1988-0 | 2992.0 | 63.0 | ||||
1989-0 | 2146.0 | 0.0 | ||||
1990-0 | 863.0 | 0.0 | ||||
1991-0 | 925.0 | 0.0 | ||||
1992-0 | 0.0 | 0.0 | ||||
1993-0 | 0.0 | 0.0 | ||||
1998-0 | 2351.0 | 0.0 | ||||
1999-0 | 2553.0 | 49.0 | ||||
2000-0 | 3755.0 | 0.0 | ||||
2001-0 | 2813.0 | 27.0 | ||||
2002-0 | 2486.0 | 0.0 | ||||
2003-0 | 2567.0 | 0.0 | ||||
2004-0 | 1381.0 | 40.0 | ||||
2005-0 | 1252.0 | 0.0 | ||||
2006-0 | 1880.0 | 0.0 | ||||
2007-0 | 1755.0 | 0.0 | ||||
2008-0 | 1993.0 | 36.0 | ||||
2009-0 | 1859.0 | 0.0 | ||||
2010-0 | 1913.0 | 0.0 | ||||
2011-0 | 1143.0 | 0.0 | ||||
2012-0 | 2041.0 | 12.0 | ||||
2013-0 | 1001.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1409664166 | 2014-05-28 | I was on location with Wade Balser from the Ohio EPA to follow up on the clean up operation from the brine and oil release that was reported on 5/27/2014. KDA is on location with equipment to start the clean up . Water trucks are vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. Wade and I walked from the tank battery to the pond and found that the vegetation and soil along the ditch has to be removed. All fluids were contained inside the pond. | ||||
1409667711 | 2014-05-29 | I was on location with Wade Balser from the Ohio EPA to follow up on the clean up operation from the brine and oil release that was reported on 5/27/2014. KDA is on location with equipment to start the clean up . Water trucks are vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. The clean up is progressing slowly. The backhoe is pulling the vegetation away from the edge of the pond that has oil residue on it and putting it into containers. After they remove this they will finish vacuuming the pond. Wade Balser from the Ohio EPA has finished his inspection. The tank battery consist of one 35 barrel tank and one vertical separator. The well is equipped with 1.5 tubing. Well is shut in at this time. | ||||
1409747123 | 2014-06-13 | I was on location to perform a follow up inspection. KDA is on location with equipment performing the clean up. The clean up is progressing slowly. The tank battery consist of one 35 barrel tank and one vertical separator. The well is equipped with 1.5 tubing. Well is shut in at this time. | ||||
1426943527 | 2015-03-16 | I performed a follow up inspection on this location. Compliance Notice dated 5/27/2014 #1401722020 can be closed. Vegetation has been established in all of the disturbed areas. Landscape has been replaced. Dike has been rebuild. The tank battery is equipped with one (1) 35 barrel poly tank and one (1) horizontal separator. The well is an 1.5 plunger lift. ID signs are posted. No noted violations at this time. This Compliance Notice is closed. | ||||
-1665132347 | 2014-06-03 | I was on location to perform a follow up inspection. KDA is on location with equipment performing the clean up . Water trucks are finishing vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. The clean up is progressing slowly. The tank battery consist of one 35 barrel tank and one vertical separator. The well is equipped with 1.5 tubing. Well is shut in at this time. | ||||
-1895400299 | 2012-02-09 | On 02/06/2012, DNR Inspector Richard Skidmore completed a production well inspection status check for DNR Inspector Chris Grimm. The lease road, tank battery, and well head locations are in compliance with 1501:9-9-05. Inspection passed. | ||||
-19173415 | 2014-06-05 | I was on location to perform a follow up inspection. KDA is on location with equipment performing the clean up . Water trucks are finishing vacuuming oil from the pond, booms are located at the spillway. Roll offs are on location, a backhoe is removing contaminated soil. The clean up is progressing slowly. | ||||
856949538 | 2009-09-18 | I GPS'd both the wellhead and the tank battery for the first time. I continued my walk around the tank battery and the wellhead and found that there were no violations at this time. |
For data sources see[2]