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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-031-23941 | | Well ID: 34-031-23941 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.32287737, -82.15748397 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Coshocton County, Ohio|Coshocton]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[PRIME TIME ENERGY INVEST]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1980-09-26 | | Spud Date: 1980-09-26 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: 40. | + | | Latitude: 40.32287737 |
|- | |- | ||
− | | Longitude: -82. | + | | Longitude: -82.15748397 |
|- | |- | ||
|} | |} | ||
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!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 2001-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 359.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 234.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 156.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 155.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 196.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 79.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 155.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 613.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 604.0 | ||
+ | | style="text-align:right;" | 365.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 139: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
| -1512658150 | | -1512658150 | ||
| 2013-05-02 | | 2013-05-02 | ||
− | | | + | | |
| FOLLOW UP TO CA #818395417: On the day of my inspection I found that the leak had been stopped and all of the contaminated soil and gravel had been removed from inside of the dike. This violation is resolved. | | FOLLOW UP TO CA #818395417: On the day of my inspection I found that the leak had been stopped and all of the contaminated soil and gravel had been removed from inside of the dike. This violation is resolved. | ||
− | | | + | | |
− | | | + | | |
− | + | | | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | | | ||
|- | |- | ||
|- | |- | ||
| 818395417 | | 818395417 | ||
| 2013-04-18 | | 2013-04-18 | ||
− | | | + | | |
| On the day of my inspection I found that the tank battery consisted of four 100 barrel stock tanks, two separators and an earthen dike. The equipment was heavily rusted and the bull plug in the load line was leaking. I found an area of oil-soaked soil approximately 2 to 3 feet in diameter at the plug. The center of the contaminated area was pooled with water. I conducted a field titration test on the water with a low range Quantab. The water tested at 239 ppm for chlorides. Fix the leak and remove all contaminated soil from inside the dike. | | On the day of my inspection I found that the tank battery consisted of four 100 barrel stock tanks, two separators and an earthen dike. The equipment was heavily rusted and the bull plug in the load line was leaking. I found an area of oil-soaked soil approximately 2 to 3 feet in diameter at the plug. The center of the contaminated area was pooled with water. I conducted a field titration test on the water with a low range Quantab. The water tested at 239 ppm for chlorides. Fix the leak and remove all contaminated soil from inside the dike. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-031-23941 | Loading map...
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County: Coshocton | |
Municipality: | |
Operator Name: PRIME TIME ENERGY INVEST | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1980-09-26 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 40.32287737 | |
Longitude: -82.15748397 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2001-0 | 0.0 | 359.0 | ||||
2007-0 | 0.0 | 234.0 | ||||
2008-0 | 0.0 | 156.0 | ||||
2009-0 | 0.0 | 155.0 | ||||
2010-0 | 0.0 | 196.0 | ||||
2011-0 | 0.0 | 79.0 | ||||
2012-0 | 0.0 | 155.0 | ||||
2013-0 | 0.0 | 613.0 | ||||
2014-0 | 0.0 | 365.0 | 604.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1512658150 | 2013-05-02 | FOLLOW UP TO CA #818395417: On the day of my inspection I found that the leak had been stopped and all of the contaminated soil and gravel had been removed from inside of the dike. This violation is resolved. | ||||
818395417 | 2013-04-18 | On the day of my inspection I found that the tank battery consisted of four 100 barrel stock tanks, two separators and an earthen dike. The equipment was heavily rusted and the bull plug in the load line was leaking. I found an area of oil-soaked soil approximately 2 to 3 feet in diameter at the plug. The center of the contaminated area was pooled with water. I conducted a field titration test on the water with a low range Quantab. The water tested at 239 ppm for chlorides. Fix the leak and remove all contaminated soil from inside the dike. |
For data sources see[2]