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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-031-22971 | | Well ID: 34-031-22971 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.4178741, -82.11259824 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Coshocton County, Ohio|Coshocton]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[PATTEN W H DRLG CO]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1977-04-06 | | Spud Date: 1977-04-06 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Plugged and Abandoned |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 40. | + | | Latitude: 40.4178741 |
|- | |- | ||
− | | Longitude: -82. | + | | Longitude: -82.11259824 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1984-0 | ||
+ | | style="text-align:right;" | 323.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 382.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1985-0 | ||
+ | | style="text-align:right;" | 125.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 430.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1986-0 | ||
+ | | style="text-align:right;" | 583.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 213.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1987-0 | ||
+ | | style="text-align:right;" | 430.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 222.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1988-0 | ||
+ | | style="text-align:right;" | 223.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 290.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1989-0 | ||
+ | | style="text-align:right;" | 77.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 74.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1990-0 | ||
+ | | style="text-align:right;" | 459.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 70.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1991-0 | ||
+ | | style="text-align:right;" | 247.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 61.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1992-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 77.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1994-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 72.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1995-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 72.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1996-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 151.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1997-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 77.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1998-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 69.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1999-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2000-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 70.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2001-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2002-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2003-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2004-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2006-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 319: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1295886457 | | 1295886457 | ||
| 2011-01-24 | | 2011-01-24 | ||
− | | | + | | |
| Last production reported was in 2001. Talked to Bill Patten by phone, said the company was planning on plugging well this summer and would apply for a plugging permit. | | Last production reported was in 2001. Talked to Bill Patten by phone, said the company was planning on plugging well this summer and would apply for a plugging permit. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1408976206 | | 1408976206 | ||
| 2014-08-25 | | 2014-08-25 | ||
− | | | + | | |
− | | On the day of my inspection I found that Gene Matheny had pulled the 4.5 | + | | On the day of my inspection I found that Gene Matheny had pulled the 4.5 casing from the well. They set a brush and stone bridge at 1092' and then made an attempt at pulling the 7 casing. The casing parted as soon as they stared to pull. They got 117' of 7 casing out of the well. The casing was rotted and full of holes at the point where it parted. Matheny washed 5 tons of clay down the well. The well did not fill up. It will be allowed to settle overnight before adding more clay. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 2130851168 | | 2130851168 | ||
| 2014-08-21 | | 2014-08-21 | ||
− | | | + | | |
− | | On the day of my inspection Gene Matheny washed 2.5 tons of clay down the 4.5 | + | | On the day of my inspection Gene Matheny washed 2.5 tons of clay down the 4.5 casing. They ripped the casing at approximately 2000' and pulled two joints. Then they washed another 2.5 tons of clay down the casing for a total of 5 tons of clay for the bottom plug. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 303177169 | | 303177169 | ||
| 2014-08-28 | | 2014-08-28 | ||
− | | | + | | |
− | | On the day of my inspection Gene Matheny washed 9 tons of clay down the well filling it to surface. I requested | + | | On the day of my inspection Gene Matheny washed 9 tons of clay down the well filling it to surface. I requested that they leave the well open to allow the clay to settle overnight. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -35934982 | ||
+ | | 2004-09-14 | ||
+ | | | ||
+ | | Motor removed from pumping unit . | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 611509520 | | 611509520 | ||
| 2014-08-29 | | 2014-08-29 | ||
− | | | + | | |
− | | On the day of my inspection I found that the clay was sitting firm | + | | On the day of my inspection I found that the clay was sitting firm at the surface of the well. I authorized Patten Drilling to cut the casing and cap the well. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-031-22971 | Loading map...
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County: Coshocton | |
Municipality: | |
Operator Name: PATTEN W H DRLG CO | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1977-04-06 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Plugged and Abandoned | |
Violations: 0 | |
Latitude: 40.4178741 | |
Longitude: -82.11259824 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 323.0 | 382.0 | ||||
1985-0 | 125.0 | 430.0 | ||||
1986-0 | 583.0 | 213.0 | ||||
1987-0 | 430.0 | 222.0 | ||||
1988-0 | 223.0 | 290.0 | ||||
1989-0 | 77.0 | 74.0 | ||||
1990-0 | 459.0 | 70.0 | ||||
1991-0 | 247.0 | 61.0 | ||||
1992-0 | 0.0 | 77.0 | ||||
1994-0 | 0.0 | 72.0 | ||||
1995-0 | 0.0 | 72.0 | ||||
1996-0 | 0.0 | 151.0 | ||||
1997-0 | 0.0 | 77.0 | ||||
1998-0 | 0.0 | 69.0 | ||||
1999-0 | 0.0 | 0.0 | ||||
2000-0 | 0.0 | 70.0 | ||||
2001-0 | 0.0 | 0.0 | ||||
2002-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1295886457 | 2011-01-24 | Last production reported was in 2001. Talked to Bill Patten by phone, said the company was planning on plugging well this summer and would apply for a plugging permit. | ||||
1408976206 | 2014-08-25 | On the day of my inspection I found that Gene Matheny had pulled the 4.5 casing from the well. They set a brush and stone bridge at 1092' and then made an attempt at pulling the 7 casing. The casing parted as soon as they stared to pull. They got 117' of 7 casing out of the well. The casing was rotted and full of holes at the point where it parted. Matheny washed 5 tons of clay down the well. The well did not fill up. It will be allowed to settle overnight before adding more clay. | ||||
2130851168 | 2014-08-21 | On the day of my inspection Gene Matheny washed 2.5 tons of clay down the 4.5 casing. They ripped the casing at approximately 2000' and pulled two joints. Then they washed another 2.5 tons of clay down the casing for a total of 5 tons of clay for the bottom plug. | ||||
303177169 | 2014-08-28 | On the day of my inspection Gene Matheny washed 9 tons of clay down the well filling it to surface. I requested that they leave the well open to allow the clay to settle overnight. | ||||
-35934982 | 2004-09-14 | Motor removed from pumping unit . | ||||
611509520 | 2014-08-29 | On the day of my inspection I found that the clay was sitting firm at the surface of the well. I authorized Patten Drilling to cut the casing and cap the well. |
For data sources see[2]