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Difference between revisions of "34-129-20043"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-129-20043
 
| Well ID: 34-129-20043
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.5481499551, -82.9278588498 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.54814996, -82.92785885 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Pickaway County, Ohio|Pickaway]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[REDMAN E C /REDMAN OIL CO]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1994-01-31
 
| Spud Date: 1994-01-31
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.5481499551
+
| Latitude: 39.54814996
 
|-
 
|-
| Longitude: -82.9278588498
+
| Longitude: -82.92785885
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 559.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 801.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 792.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 636.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 317.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 24.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 38.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 139:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1248i241
 
| 1248i241
 
| 2002-02-21
 
| 2002-02-21
|
+
|  
| WEATHER CONDITIONS: Cloudy and 40 degrees. Meet with Joe Melville and Dave Athea on location. Service rig was to pull 4 1/2" casing to start plugging operations but during swabbing the well was producing oil. They are going to continue swabbing the well and might put it back in to production. Joe to call me if they decide not to plug the well.
+
| WEATHER CONDITIONS: Cloudy and 40 degrees. Meet with Joe Melville and Dave Athea on location. Service rig was to pull 4 1/2 casing to start plugging operations but during swabbing the well was producing oil. They are going to continue swabbing the well and might put it back in to production. Joe to call me if they decide not to plug the well.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1248i245
 
| 1248i245
 
| 2002-02-25
 
| 2002-02-25
|
+
|  
| WEATHER CONDITIONS: Partly cloudy 45 degrees.  Meet with Joe Melville on location and was advised that the rig had ripped the 4 1/2" casing at 2660'. Calculated the size, depth, and sacks of cement needed to plug the well. Plugging operations to start at 8:00 A.M. tomorrow.
+
| WEATHER CONDITIONS: Partly cloudy 45 degrees.  Meet with Joe Melville on location and was advised that the rig had ripped the 4 1/2 casing at 2660'. Calculated the size, depth, and sacks of cement needed to plug the well. Plugging operations to start at 8:00 A.M. tomorrow.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 18425
 
| 18425
|
+
|  
|
+
|  
| PASSED Y WITNESSED 12/20/94 INSPECTOR BOB MARTIN DATE 12/2019/94 DATA FROM OLD VAX INFO
+
| PASSED Y WITNESSED 12/20/94 INSPECTOR BOB MARTIN DATE 12/2019/94 DATA FROM OLD VAX INFO
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 47974061
 
| 47974061
 
| 2002-09-03
 
| 2002-09-03
|
+
|  
 
| Inspection revealed storage tank left on location. I called Joe Millville in regards to a 210 Bbl. Storage tank located on the next property and was advised that the tank is to heavy to move. He is going to open the tank and remove the materials so the tank can be removed. He will call me when this is done. WEATHERCONDITIONS: Sunny and 75 degrees.
 
| Inspection revealed storage tank left on location. I called Joe Millville in regards to a 210 Bbl. Storage tank located on the next property and was advised that the tank is to heavy to move. He is going to open the tank and remove the materials so the tank can be removed. He will call me when this is done. WEATHERCONDITIONS: Sunny and 75 degrees.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 02:50, 15 July 2015

Well Details

Well ID: 34-129-20043
Loading map...
County: Pickaway
Municipality:
Operator Name: REDMAN E C /REDMAN OIL CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1994-01-31
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.54814996
Longitude: -82.92785885

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1994-0 0.0 559.0
1995-0 0.0 801.0
1996-0 0.0 792.0
1997-0 0.0 636.0
1998-0 0.0 317.0
1999-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 24.0
2002-0 0.0 38.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1248i241 2002-02-21 WEATHER CONDITIONS: Cloudy and 40 degrees. Meet with Joe Melville and Dave Athea on location. Service rig was to pull 4 1/2 casing to start plugging operations but during swabbing the well was producing oil. They are going to continue swabbing the well and might put it back in to production. Joe to call me if they decide not to plug the well.
1248i245 2002-02-25 WEATHER CONDITIONS: Partly cloudy 45 degrees. Meet with Joe Melville on location and was advised that the rig had ripped the 4 1/2 casing at 2660'. Calculated the size, depth, and sacks of cement needed to plug the well. Plugging operations to start at 8:00 A.M. tomorrow.
18425 PASSED Y WITNESSED 12/20/94 INSPECTOR BOB MARTIN DATE 12/2019/94 DATA FROM OLD VAX INFO
47974061 2002-09-03 Inspection revealed storage tank left on location. I called Joe Millville in regards to a 210 Bbl. Storage tank located on the next property and was advised that the tank is to heavy to move. He is going to open the tank and remove the materials so the tank can be removed. He will call me when this is done. WEATHERCONDITIONS: Sunny and 75 degrees.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.