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Well ID: 34-129-20043 | Loading map...
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Country: United States | |
State: Ohio | |
County: Pickaway | |
Municipality: Pickaway Township | |
Operator Name: REDMAN E C /REDMAN OIL CO | |
Well Pad ID: | |
Farm/Lease Name: KERNS UNIT | |
License Status: Final Restoration | |
License Date: 2001-10-02 | |
Spud Date: 1994-01-31 | |
Spud Drilling Contractor: R WOLFE DRLG | |
Final Drill Date: 1994-02-08 | |
Well Total Depth: 2716.00 ft | |
Configuration: Vertical | |
Latitude: 39.540000 | |
Longitude: -82.920000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1994-01-14 | Issued Date 1/14/94 Expired Date 1/14/95 Acres 0020000 Tool Type RTAF Proposed Formation KNOX/ROSE RUN Proposed Depth 02716 Proposed Drill Depth 02716 |
Original Spud | 1994-02-02 | |
Completed | 1994-02-08 | |
Reached Total Depth | 1994-02-08 | |
CO | 1994-06-17 | 1901 REDMAN E C /REDMAN OIL CO GeoDate 1/14/94 |
Completion Report Received | 1994-07-26 | |
APP | 2001-10-02 | Proposed Formations:ROSE RUN, Issued Date:10/2/2001, Expired Date:10/2/2002 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2002-02-26 | |
Construction Permit Expires | 2002-10-02 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 2702 | 0 | |
2702 | 0 | ||
2702 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 500 Gal | 0 | ACIDIZED W/500 GAL |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1994 | REDMAN E C /REDMAN OIL CO | 0.00 | 559.00 | 200 |
1995 | REDMAN E C /REDMAN OIL CO | 0.00 | 801.00 | 100 |
1996 | REDMAN OIL CO INC | 0.00 | 792.00 | 124 |
1997 | REDMAN E C /REDMAN OIL CO | 0.00 | 636.00 | 305 |
1998 | REDMAN E C /REDMAN OIL CO | 0.00 | 317.00 | 120 |
1999 | REDMAN E C /REDMAN OIL CO | 0.00 | 0.00 | 0 |
2000 | REDMAN E C /REDMAN OIL CO | 0.00 | 0.00 | 0 |
2001 | REDMAN E C /REDMAN OIL CO | 0.00 | 24.00 | 31 |
2002 | OHIO ENERGY ASSETS, INC. | 0.00 | 38.00 | 30 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1994 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 200 |
1995 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 100 |
1996 | REDMAN OIL CO INC | Brine | 0 | 124 |
1997 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 305 |
1998 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 120 |
1999 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 0 |
2000 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 0 |
2001 | REDMAN E C /REDMAN OIL CO | Brine | 0 | 31 |
2002 | OHIO ENERGY ASSETS, INC. | Brine | 0 | 30 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000018425 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 12/20/94 INSPECTOR BOB MARTIN DATE 12/2019/94 DATA FROM OLD VAX INFO | |
001248i241 | 2002-02-21 | Production Wells | No Violations | WEATHER CONDITIONS: Cloudy and 40 degrees. Meet with Joe Melville and Dave Athea on location. Service rig was to pull 4 1/2 casing to start plugging operations but during swabbing the well was producing oil. They are going to continue swabbing the well and might put it back in to production. Joe to call me if they decide not to plug the well. |
001248i245 | 2002-02-25 | Production Wells | No Violations | WEATHER CONDITIONS: Partly cloudy 45 degrees. Meet with Joe Melville on location and was advised that the rig had ripped the 4 1/2 casing at 2660. Calculated the size, depth, and sacks of cement needed to plug the well. Plugging operations to start at 8:00 A.M. tomorrow. |
0047974061 | 2002-09-03 | Final Restoration | No Violations | Inspection revealed storage tank left on location. I called Joe Millville in regards to a 210 Bbl. Storage tank located on the next property and was advised that the tank is to heavy to move. He is going to open the tank and remove the materials so the tank can be removed. He will call me when this is done. WEATHERCONDITIONS: Sunny and 75 degrees. |
1248i241 | 2002-2-21 0:00: | PW | No Violations | |
1248i245 | 2002-2-25 0:00: | PW | No Violations | |
18425 | PL | No Violations | ||
47974061 | 2002-9-3 0:00:0 | FR | No Violations |
For data sources see[9]