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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-151-25720 | | Well ID: 34-151-25720 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.79818212, -81.09991993 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Stark County, Ohio|Stark]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[D & L ENERGY INC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 2011-03-11 | | Spud Date: 2011-03-11 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 40. | + | | Latitude: 40.79818212 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.09991993 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 1163.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1392.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 3220.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 2118.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 376.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 1389.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 85: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
| -1010529108 | | -1010529108 | ||
| 2012-01-09 | | 2012-01-09 | ||
− | | | + | | |
| On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time. | | On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1302121253 | | 1302121253 | ||
| 2011-03-31 | | 2011-03-31 | ||
− | | | + | | |
| Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8'' dia. wellhead from the annular space between the 4-1/2'' dia. casing and the inside of the 8-5/8'' dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2'' dia casing at 433'. This was determined by pumping a colored paint down the 4-1/2'' dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue. | | Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8'' dia. wellhead from the annular space between the 4-1/2'' dia. casing and the inside of the 8-5/8'' dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2'' dia casing at 433'. This was determined by pumping a colored paint down the 4-1/2'' dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 463071781 | | 463071781 | ||
| 2011-08-19 | | 2011-08-19 | ||
− | | | + | | |
| The well is in production and the location is rough graded. | | The well is in production and the location is rough graded. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-151-25720 | Loading map...
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County: Stark | |
Municipality: | |
Operator Name: D & L ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2011-03-11 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 40.79818212 | |
Longitude: -81.09991993 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2011-0 | 1163.0 | 1392.0 | ||||
2012-0 | 3220.0 | 2118.0 | ||||
2013-0 | 376.0 | 1389.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1010529108 | 2012-01-09 | On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time. | ||||
1302121253 | 2011-03-31 | Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8 dia. wellhead from the annular space between the 4-1/2 dia. casing and the inside of the 8-5/8 dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2 dia casing at 433'. This was determined by pumping a colored paint down the 4-1/2 dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue. | ||||
463071781 | 2011-08-19 | The well is in production and the location is rough graded. |
For data sources see[2]