X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-151-25720"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-151-25720
 
| Well ID: 34-151-25720
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.798260541, -81.0998040895 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.79818212, -81.09991993 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Stark County, Ohio|Stark]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[D & L ENERGY INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2011-03-11
 
| Spud Date: 2011-03-11
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.798260541
+
| Latitude: 40.79818212
 
|-
 
|-
| Longitude: -81.0998040895
+
| Longitude: -81.09991993
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 1163.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1392.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 3220.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 2118.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 376.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1389.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 85:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1010529108
 
| -1010529108
 
| 2012-01-09
 
| 2012-01-09
|
+
|  
 
| On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time.
 
| On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1302121253
 
| 1302121253
 
| 2011-03-31
 
| 2011-03-31
|
+
|  
 
| Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8'' dia. wellhead from the annular space between the 4-1/2'' dia. casing and the inside of the 8-5/8'' dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2'' dia casing at 433'. This was determined by pumping a colored paint down the 4-1/2'' dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue.
 
| Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8'' dia. wellhead from the annular space between the 4-1/2'' dia. casing and the inside of the 8-5/8'' dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2'' dia casing at 433'. This was determined by pumping a colored paint down the 4-1/2'' dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 463071781
 
| 463071781
 
| 2011-08-19
 
| 2011-08-19
|
+
|  
 
| The well is in production and the location is rough graded.
 
| The well is in production and the location is rough graded.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 12:21, 16 July 2015

Well Details

Well ID: 34-151-25720
Loading map...
County: Stark
Municipality:
Operator Name: D & L ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2011-03-11
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.79818212
Longitude: -81.09991993

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2011-0 1163.0 1392.0
2012-0 3220.0 2118.0
2013-0 376.0 1389.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1010529108 2012-01-09 On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time.
1302121253 2011-03-31 Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8 dia. wellhead from the annular space between the 4-1/2 dia. casing and the inside of the 8-5/8 dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2 dia casing at 433'. This was determined by pumping a colored paint down the 4-1/2 dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue.
463071781 2011-08-19 The well is in production and the location is rough graded.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.