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Well ID: 34-151-25720 | Loading map...
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Country: United States | |
State: Ohio | |
County: Stark | |
Municipality: Paris Township | |
Operator Name: BOBCAT WELL & PIPELINE LLC | |
Well Pad ID: | |
Farm/Lease Name: EYER | |
License Status: Producing | |
License Date: 2011-02-22 | |
Spud Date: 2011-03-11 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2011-03-21 | |
Well Total Depth: 5705.00 ft | |
Configuration: Vertical | |
Latitude: 40.790000 | |
Longitude: -81.090000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2011-02-22 | Proposed Formations:CLINTON, Issued Date:2/22/2011, Expired Date:2/21/2013 12:00:00 PM, Drilling unit acres:41.55, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2011-03-21 | |
Completion Report Received | 2011-08-23 | |
Construction Permit Expires | 2013-02-21 | |
Change of Owner | 2015-01-27 | Operator changed from 2651, D & L ENERGY INC to 9426, BOBCATE WELL AND PIPELINE LLC |
Record Last Modified | 2015-05-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-12-01 | 5468 | 5474 | 5 |
2011-12-01 | 5478 | 5482 | 4 |
5468 | 5474 | 5 | |
5478 | 5482 | 4 | |
5490 | 5530 | 0 | |
5468 | 5474 | 5 | |
2011-12-16 | 5490 | 5530 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2011-03-22 | H2O | 0 | 500 Gal | 80000 | Superior Well Services |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | D & L ENERGY INC | 1163.00 | 1392.00 | 0 |
2012 | D & L ENERGY INC | 3220.00 | 2118.00 | 365 |
2013 | D & L ENERGY INC | 376.00 | 1389.00 | 365 |
2014 | D & L ENERGY INC | 234.00 | 992.00 | 365 |
2015 | BOBCAT WELL & PIPELINE LLC | 140.00 | 887.00 | 365 |
2016 | BOBCAT WELL & PIPELINE LLC | 627.00 | 738.00 | 358 |
2017 | BOBCAT WELL & PIPELINE LLC | 1456.00 | 769.00 | 358 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2011 | D & L ENERGY INC | Brine | 1097 | |
2012 | D & L ENERGY INC | Brine | 980 | 365 |
2013 | D & L ENERGY INC | Brine | 306 | 365 |
2014 | D & L ENERGY INC | Brine | 293 | 365 |
2015 | BOBCAT WELL & PIPELINE LLC | Brine | 324 | 365 |
2016 | BOBCAT WELL & PIPELINE LLC | Brine | 255 | 358 |
2017 | BOBCAT WELL & PIPELINE LLC | Brine | 110 | 358 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1010529108 | 2012-1-9 0:00:0 | PL | No Violations | 1.00 |
0463071781 | 2011-08-19 | Preliminary Restoration | No Violations | The well is in production and the location is rough graded. |
1010529108 | 2012-01-09 | Preliminary Restoration | No Violations | On 1/9/2012, I performed a status check on the above well site. Well is in production, location needs reclaimed and identification sings are posted, Preliminary Restoration can not be passed at this time. |
1302121253 | 2011-03-31 | Completion Testing | No Violations | Superior Well Services fraced the well today. During the frac job, flow started coming out of the open valve on the 8-5/8 dia. wellhead from the annular space between the 4-1/2 dia. casing and the inside of the 8-5/8 dia. casing. The job was shut down and the flow was directed into the drilling pits. It is believed that there is a split in the 4-1/2 dia casing at 433. This was determined by pumping a colored paint down the 4-1/2 dia casing and out of the annulus. Casing failure depth was calculated from displacement volume. Remediation of the situation will continue. |
463071781 | 2011-8-19 0:00: | PL | No Violations |
For data sources see[9]