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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-117-24241 | | Well ID: 34-117-24241 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 40.562101702, -82.66143406 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | Operator Name: [[SCION ENERGY | + | | County: [[Morrow_County,_Ohio|Morrow]] |
+ | |- | ||
+ | | Municipality: [[Perry,_Morrow_County,_Ohio|Perry]] | ||
+ | |- | ||
+ | | Operator Name: [[SCION ENERGY INC]] | ||
|- | |- | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: SEI-M & A KRABILL-JORDON UNIT |
|- | |- | ||
− | | | + | | License Status: Final Restoration |
|- | |- | ||
− | | | + | | License Date: 2012-12-11 |
|- | |- | ||
| Spud Date: 2012-06-25 | | Spud Date: 2012-06-25 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: [[KILBARGER DRLG]] |
+ | |- | ||
+ | | Final Drill Date: 2012-07-07 | ||
+ | |- | ||
+ | | Well Total Depth: 3950 ft | ||
|- | |- | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | | + | | Latitude: 40.562101702 |
|- | |- | ||
− | | | + | | Longitude: -82.66143406 |
+ | |} | ||
+ | For data sources see<ref name=RBDMS>{{cite web | ||
+ | | title = RBDMS | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" style="width: 50%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
|- | |- | ||
− | | | + | |}--> |
+ | |||
+ | <!--== Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
|- | |- | ||
− | | | + | |}--> |
+ | |||
+ | <!--== Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
|- | |- | ||
− | |} | + | |}--> |
+ | |||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | 0089887781 | |
+ | | 2012-07-05 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Kilbarger #1 went to fluid after holiday shut down, unable to unload hole possible bad cement job on the 7 intermediate casing (unable to shut off Newburg water). Drilling 3392 Trenton top 3363 (stratagraph mudlogger pick). | ||
+ | |- | ||
+ | | 0799974661 | ||
+ | | 2012-08-10 | ||
+ | | Final Restoration | ||
+ | | No Violations | ||
+ | | Miller roustabout has planted wheat on the 2.5 acre site. The gravel access road and plastic culvert have been removed. | ||
|- | |- | ||
| 1340125984 | | 1340125984 | ||
| 2012-06-19 | | 2012-06-19 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Preliminary site inspection. Miller roustabout has removed 2-3 feet of top soil off of the location (down to clay) and piled it surrounding the location which prevents run-off. A large air pit has been dug and they are waiting on the location to dry before digging the fluid pit. The entrance off state route 314 is rocked and a 12 | + | | No Violations |
− | + | | Preliminary site inspection. Miller roustabout has removed 2-3 feet of top soil off of the location (down to clay) and piled it surrounding the location which prevents run-off. A large air pit has been dug and they are waiting on the location to dry before digging the fluid pit. The entrance off state route 314 is rocked and a 12 plastic ditch culvert installed. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1340720369 | | 1340720369 | ||
| 2012-06-26 | | 2012-06-26 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Kilbarger #1 move in and spud 2:30 p.m. 6/25/2012. Set 90 | + | | No Violations |
− | + | | Kilbarger #1 move in and spud 2:30 p.m. 6/25/2012. Set 90 of 13.375 36# new conductor, not cemented. 6/26/2012 10:00 a.m. go to fluid at 460. Reached total depth on surface hole at 669, 3:25 p.m. on fluid. 5:00 p.m. Os power tongs running 9.625 surface casing. Hit bridge at 110. 6:00 p.m. lay down surface casing. Kilbarger #1 going in hole to ream. 8:15 p.m. going back in hole with surface casing. 9:00 p.m. hit bridge again at 110. Pull out of hole and go in without casing shoe. Hit bridge at 110, unable to get through. 10:30 p.m. decision made by Tom Roberts to pull conductor and drill deeper to set conductor deeper. Permit shows 121 of drift. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1340827784 | | 1340827784 | ||
| 2012-06-27 | | 2012-06-27 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Kilbarger #1 pulled conductor, went back in hole and reamed. Ran 150 | + | | No Violations |
− | + | | Kilbarger #1 pulled conductor, went back in hole and reamed. Ran 150 conductor, not cemented. 10:00 a.m. run back in hole with 12.25 bit to clean out hole to 659 and circulate clean.. 3:00 p.m. Os power tongs rig up and start running 9.625 with guide shoe on bottom, ran 591 set at 601. 4:15 Formation cementing hooking up. Formation gained circulation by pumping 59 barrels gel and lost circulation material (cottonseed hulls) ahead of 210 sacks class A displaced by 45.3 barrels. Plug down 5:15 p.m. Good cement circulation at surface which held. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1341240170 | | 1341240170 | ||
| 2012-07-02 | | 2012-07-02 | ||
− | | | + | | Drill / Deepen / Reopen |
− | | Kilbarger #1 drilling ahead on soap 3037 | + | | No Violations |
− | + | | Kilbarger #1 drilling ahead on soap 3037 2 hours per kelly. D.V. survey 2970 2.75 degree. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1341698763 | | 1341698763 | ||
| 2012-07-07 | | 2012-07-07 | ||
− | | | + | | Plug / Plug Back |
− | | Kilbarger #1 reached total depth at 3950 | + | | No Violations |
− | + | | Kilbarger #1 reached total depth at 3950 in the Trempealeau on 8.6 pound KCL fluid. Appalachian well surveys logged well. Decision made to plug well. Formation cementing on location 5:00 p.m. Kilbarger on bottom with drill pipe (open ended) 7:30 p.m. break circulation, start first plug. When pulling out of hole for the surface casing plug realized they lost 7 joints (210) of drill pipe, probably when hitting a bridge inside the 7 at 1930. See plug report for detailed description. Final adjusted plugs: 1) 3713-3363. 2) 1891-1691. 3) 1199-999. 4) 414-190. 5) 125-ground level. Broke circulation before all plugs. Finish plugging well at 1:15 a.m. circulated Class A cement to surface which held. Kilbarger #1 well bore deviation surveys: 1) 650-1 degree 2) 754-3.5 3) 849-1.5 4) 1230-1.25 5) 2150-.5 6) 2470-.75 7) 2849-3.5 8) 2913-3 9) 2970- 2.75 10) 3040-1 11) 3225-1.75 12) 3250-1.75 13) 3360-.75. | |
− | |||
− | |||
− | |||
|- | |- | ||
| 1342550145 | | 1342550145 | ||
| 2012-07-17 | | 2012-07-17 | ||
− | | | + | | Preliminary Restoration |
+ | | No Violations | ||
| The preliminary restoration has begun on the Krabil-Jordon Unit #1 by Miller roustabout. Both the air and fluid pits have been filled and compacted. All drilling debris and trash has been removed. Miller is currently working on replacing the topsoil. | | The preliminary restoration has begun on the Krabil-Jordon Unit #1 by Miller roustabout. Both the air and fluid pits have been filled and compacted. All drilling debris and trash has been removed. Miller is currently working on replacing the topsoil. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1681221138 | ||
+ | | 2012-07-06 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Kilbarger #1 drilling ahead on fluid 3630 (Black River) 1.5 hours per kelly. | ||
+ | |- | ||
+ | | 1787140308 | ||
+ | | 2012-06-28 | ||
+ | | Drill / Deepen / Reopen | ||
+ | | No Violations | ||
+ | | Kilbarger #1 drilling ahead at 960 on air. D.V. survey 754 3.5 degree, 849 1.5 degree. | ||
+ | |- | ||
+ | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | For data sources see<ref name=RBDMS/> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
|- | |- | ||
− | | - | + | |}--> |
− | | | + | <!--==== Fluid Composition Data ==== |
− | | | + | {| class="wikitable sortable" style="width: 100%" |
− | | | + | !scope="col" style="text-align: center"| Job Number |
− | | | + | !scope="col" style="text-align: center"| Trade Name |
− | | | + | !scope="col" style="text-align: center"| Supplier |
− | | | + | !scope="col" style="text-align: center"| Purpose |
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
|- | |- | ||
+ | |}--> | ||
+ | |||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
|- | |- | ||
− | | - | + | |}--> |
− | + | ||
− | + | == Well History == | |
− | | | + | {| class="wikitable sortable" width="95%" |
− | | | + | !scope="col" style="text-align: center"| Well Status |
− | | | + | !scope="col" style="width: 15%;text-align: center"| Well Status Date |
− | | | + | !scope="col" style="text-align: center"| Comment |
|- | |- | ||
+ | | APP | ||
+ | | 2012-04-20 | ||
+ | | Proposed Formations:UTICA THRU TREMPEALEAU (MAY NOT PRODUCE BLACK RIVER), Issued Date:4/20/2012, Expired Date:4/20/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL | ||
|- | |- | ||
− | | | + | | Reached Total Depth |
− | | 2012- | + | | 2012-07-07 |
| | | | ||
− | | | + | |- |
+ | | Plugged/Abandoned | ||
+ | | 2012-07-08 | ||
| | | | ||
+ | |- | ||
+ | | Completion Report Received | ||
+ | | 2012-11-14 | ||
| | | | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2014-04-20 | ||
| | | | ||
|- | |- | ||
− | | | + | | Record Last Modified |
− | + | | 2017-10-24 | |
− | | | ||
− | |||
− | |||
− | |||
− | |||
| | | | ||
|- | |- | ||
|} | |} | ||
− | For data sources see<ref | + | For data sources see<ref name=RBDMS/> |
− | + | ==References== | |
− | + | <references/> | |
− | |||
− | |||
− | |||
− | == References == | ||
− | |||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-117-24241 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morrow | |
Municipality: Perry | |
Operator Name: SCION ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: SEI-M & A KRABILL-JORDON UNIT | |
License Status: Final Restoration | |
License Date: 2012-12-11 | |
Spud Date: 2012-06-25 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2012-07-07 | |
Well Total Depth: 3950 ft | |
Configuration: Vertical | |
Latitude: 40.562101702 | |
Longitude: -82.66143406 |
For data sources see[1]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0089887781 | 2012-07-05 | Drill / Deepen / Reopen | No Violations | Kilbarger #1 went to fluid after holiday shut down, unable to unload hole possible bad cement job on the 7 intermediate casing (unable to shut off Newburg water). Drilling 3392 Trenton top 3363 (stratagraph mudlogger pick). |
0799974661 | 2012-08-10 | Final Restoration | No Violations | Miller roustabout has planted wheat on the 2.5 acre site. The gravel access road and plastic culvert have been removed. |
1340125984 | 2012-06-19 | Drill / Deepen / Reopen | No Violations | Preliminary site inspection. Miller roustabout has removed 2-3 feet of top soil off of the location (down to clay) and piled it surrounding the location which prevents run-off. A large air pit has been dug and they are waiting on the location to dry before digging the fluid pit. The entrance off state route 314 is rocked and a 12 plastic ditch culvert installed. |
1340720369 | 2012-06-26 | Drill / Deepen / Reopen | No Violations | Kilbarger #1 move in and spud 2:30 p.m. 6/25/2012. Set 90 of 13.375 36# new conductor, not cemented. 6/26/2012 10:00 a.m. go to fluid at 460. Reached total depth on surface hole at 669, 3:25 p.m. on fluid. 5:00 p.m. Os power tongs running 9.625 surface casing. Hit bridge at 110. 6:00 p.m. lay down surface casing. Kilbarger #1 going in hole to ream. 8:15 p.m. going back in hole with surface casing. 9:00 p.m. hit bridge again at 110. Pull out of hole and go in without casing shoe. Hit bridge at 110, unable to get through. 10:30 p.m. decision made by Tom Roberts to pull conductor and drill deeper to set conductor deeper. Permit shows 121 of drift. |
1340827784 | 2012-06-27 | Drill / Deepen / Reopen | No Violations | Kilbarger #1 pulled conductor, went back in hole and reamed. Ran 150 conductor, not cemented. 10:00 a.m. run back in hole with 12.25 bit to clean out hole to 659 and circulate clean.. 3:00 p.m. Os power tongs rig up and start running 9.625 with guide shoe on bottom, ran 591 set at 601. 4:15 Formation cementing hooking up. Formation gained circulation by pumping 59 barrels gel and lost circulation material (cottonseed hulls) ahead of 210 sacks class A displaced by 45.3 barrels. Plug down 5:15 p.m. Good cement circulation at surface which held. |
1341240170 | 2012-07-02 | Drill / Deepen / Reopen | No Violations | Kilbarger #1 drilling ahead on soap 3037 2 hours per kelly. D.V. survey 2970 2.75 degree. |
1341698763 | 2012-07-07 | Plug / Plug Back | No Violations | Kilbarger #1 reached total depth at 3950 in the Trempealeau on 8.6 pound KCL fluid. Appalachian well surveys logged well. Decision made to plug well. Formation cementing on location 5:00 p.m. Kilbarger on bottom with drill pipe (open ended) 7:30 p.m. break circulation, start first plug. When pulling out of hole for the surface casing plug realized they lost 7 joints (210) of drill pipe, probably when hitting a bridge inside the 7 at 1930. See plug report for detailed description. Final adjusted plugs: 1) 3713-3363. 2) 1891-1691. 3) 1199-999. 4) 414-190. 5) 125-ground level. Broke circulation before all plugs. Finish plugging well at 1:15 a.m. circulated Class A cement to surface which held. Kilbarger #1 well bore deviation surveys: 1) 650-1 degree 2) 754-3.5 3) 849-1.5 4) 1230-1.25 5) 2150-.5 6) 2470-.75 7) 2849-3.5 8) 2913-3 9) 2970- 2.75 10) 3040-1 11) 3225-1.75 12) 3250-1.75 13) 3360-.75. |
1342550145 | 2012-07-17 | Preliminary Restoration | No Violations | The preliminary restoration has begun on the Krabil-Jordon Unit #1 by Miller roustabout. Both the air and fluid pits have been filled and compacted. All drilling debris and trash has been removed. Miller is currently working on replacing the topsoil. |
1681221138 | 2012-07-06 | Drill / Deepen / Reopen | No Violations | Kilbarger #1 drilling ahead on fluid 3630 (Black River) 1.5 hours per kelly. |
1787140308 | 2012-06-28 | Drill / Deepen / Reopen | No Violations | Kilbarger #1 drilling ahead at 960 on air. D.V. survey 754 3.5 degree, 849 1.5 degree. |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2012-04-20 | Proposed Formations:UTICA THRU TREMPEALEAU (MAY NOT PRODUCE BLACK RIVER), Issued Date:4/20/2012, Expired Date:4/20/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2012-07-07 | |
Plugged/Abandoned | 2012-07-08 | |
Completion Report Received | 2012-11-14 | |
Construction Permit Expires | 2014-04-20 | |
Record Last Modified | 2017-10-24 |
For data sources see[1]