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| County: [[Belmont_County,_Ohio|Belmont]] | | County: [[Belmont_County,_Ohio|Belmont]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[York Township,_Belmont_County,_Ohio|York Township]] |
|- | |- | ||
| Operator Name: [[RICE DRILLING D LLC]] | | Operator Name: [[RICE DRILLING D LLC]] |
Well ID: 34-013-20975 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: York Township | |
Operator Name: RICE DRILLING D LLC | |
Well Pad ID: US-OH-001271 | |
Farm/Lease Name: BIG DAWG | |
License Status: Producing | |
License Date: 2015-11-06 | |
Spud Date: 2015-09-18 | |
Spud Drilling Contractor: PATTERSON DRILLING | |
Final Drill Date: 2016-01-26 | |
Well Total Depth: 19640 ft | |
Configuration: Horizontal | |
Latitude: 39.860671818 | |
Longitude: -80.88004712 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2015-09-23 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:9/23/2015, Expired Date:9/22/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2015-11-06 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:11/6/2015, Expired Date:11/5/2017 12:00:00 PM, Drilling unit acres:474.5341, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2016-01-26 | |
Correction to Well | 2017-01-06 | UPDATE TAKEPOINT/ACREAGE PER AS-DRILLED PLAT-ALE |
Completion Report Received | 2017-01-25 | |
Construction Permit Expires | 2017-11-05 | |
Record Last Modified | 2018-02-08 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2016-12-28 | 10630 | 18954 | 0 |
For data sources see[3]
Job Number | Job Start Date | Job End Date | True Vertical Depth (ft) | Total Water Volume (gal) | Total Non-Water Volume (gal) |
---|---|---|---|---|---|
1 | 09/10/2016 | 10/03/2016 | 10300 | 22,015,100.0 | 0 |
Job Number | Trade Name | Supplier | Purpose | Ingredient Name | CAS Number | Additive Percentage by Mass | Job Percentage by Mass | Mass Used (lb) |
---|---|---|---|---|---|---|---|---|
1 | FE-100L | FTSI | Iron Control | Sodium Hydroxide | 1310-73-2 | 2 | 0.00000774 | 18.386 |
Sodium glycolate | 2836-32-0 | 1.5 | 0.00000581 | 13.789 | ||||
Trisodium Nitrilotriacetic acid | 5064-31-3 | 2 | 0.00000774 | 18.386 | ||||
Iminodiacetate disodium salt | 17593-73-6 | 0.2 | 0.00000077 | 1.839 | ||||
Tetrasodium EDTA | 64-02-8 | 41 | 0.000158741 | 376.907 | ||||
Ethylenediaminetriaceticacid, trisodium salt | 19019-43-3 | 0.8 | 0.00000310 | 7.354 | ||||
Sodium formate | 141-53-7 | 0.6 | 0.00000232 | 5.516 | ||||
Water | 7732-18-5 | 65 | 0.000251663 | 597.535 | ||||
K-BAC 1020 DBNPA | WST | Bacteriacide | Polyethylene glycol | 25322-68-3 | 50 | 0.0020765 | 4930.33 | |
Water | 7732-18-5 | 30 | 0.0012459 | 2958.2 | ||||
2,2-Dibromo-3-nitrilopropionamide | 10222-01-2 | 21 | 0.000872128 | 2070.74 | ||||
Bellasol S50 | BWA | Antiscalant | Phosphinocarboxylic Acid | 110224-99-2 | 60 | 0.00229873 | 5458 | |
Water | Rice Energy | Carrier/Base Fluid | Water | 7732-18-5 | 100 | 77.3754 | 183,716,000.0 | |
Hydrochloric Acid (HCl) | FTSI | Acid | Hydrogen Chloride | 7647-01-0 | 15 | 0.0298973 | 70986.7 | |
Insitu Additive | Silver Creek Services | Bacteriacide | Sodium Hypochlorite | 7681-52-9 | 14 | 0.00275873 | 6550.2 | |
30/50 MgLight | Fores | Proppant | Silicon Dioxide | 7631-86-9 | 40 | 0.956102 | 2,270,120.0 | |
Magnesium silicate | 1343-88-0 | 60 | 1.43415 | 3,405,180.0 | ||||
Magnesium iron silicate | 1317-71-1 | 10 | 0.239025 | 567531 | ||||
StimLube NE | StimLube NE | Friction Reducer | Alcohols, ethoxylated | 68439-50-9 | 3.1 | 0.000284903 | 676.459 | |
Alcohols, ethoxylated | 68551-12-2 | 3.1 | 0.000284903 | 676.459 | ||||
Petroleum distillates, hydrotreated light | 64742-47-8 | 30 | 0.00275712 | 6546.38 | ||||
Alcohols, ethoxylated | 68002-97-1 | 3.1 | 0.000284903 | 676.459 | ||||
UFR-47 | Silver Creek Services | Friction Reducer | Alcohols, C-12-16, ethoxylated | 68551-12-2 | 5 | 0.00268193 | 6367.85 | |
Hydrotreated light distillate (petroleum) | 64742-47-8 | 30 | 0.0160916 | 38207.1 | ||||
Cationic Copolymer of acrylamide | 69418-26-4 | 30 | 0.0160916 | 38207.1 | ||||
40/70 MgLight | Fores | Proppant | Magnesium iron silicate | 1317-71-1 | 10 | 0.440477 | 1,045,850.0 | |
Silicon Dioxide | 7631-86-9 | 40 | 1.76191 | 4,183,390.0 | ||||
Magnesium silicate | 1343-88-0 | 60 | 2.64286 | 6,275,080.0 | ||||
30/50 ShaleProp | Imerys | Proppant | Ceramic material and wares, chemical | 66402-68-4 | 100 | 4.5939 | 10,907,500.0 | |
Sand (Proppant) | Silver Creek | Proppant | Silica Substrate | 14808-60-7 | 87 | 7.69162 | 18,262,600.0 | |
40/70 ProLite | Imerys | Proppant | Mullite | 1302-93-8 | 70 | 1.47237 | 3,495,930.0 | |
Amorphous Silica | 7631-86-9 | 15 | 0.315508 | 749128 | ||||
Cristobalite | 14464-46-1 | 30 | 0.631017 | 1,498,260.0 | ||||
CI-150 | FTSI | Acid Corrosion Inhibitor | Dimethylformamide | 68-12-2 | 10 | 0.00009665 | 229.488 | |
Aromatic aldehyde | Proprietary | 30 | 0.000289958 | 688.463 | ||||
Isopropanol | 67-63-0 | 30 | 0.000289958 | 688.463 | ||||
Organic amine resin salt | Proprietary | 30 | 0.000289958 | 688.463 | ||||
Quarternary ammonium compound | Proprietary | 10 | 0.00009665 | 229.488 | ||||
Ethylene Glycol | 107-21-1 | 30 | 0.000289958 | 688.463 | ||||
Polyalkylene glycol | Proprietary | 10 | 0.00009665 | 229.488 | ||||
NE-100 | FTSI | Non-emulsifier | 2-Propanol | 67-63-0 | 10 | 0.00001894 | 44.98 | |
2-Butoxyethanol | 111-76-2 | 10 | 0.00001894 | 44.98 | ||||
Water | 7732-18-5 | 90 | 0.000170495 | 404.816 | ||||
Dodecylbenzenesulfonic acid | 27176-87-0 | 5 | 0.00000947 | 22.49 |
For data sources see[4]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2016-09-10 | H2O | 15 | 10578 Bbl | 490687 | Frac Tech Services | STAGE 1/49
30 SHOTS STAGES 2-48 SEE IMAGES |
2016-10-03 | H2O | 15 | 9707 Bbl | 500200 | Frac Tech Services | STAGE 49/49
42 SHOTS |
For data sources see[5]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2016 | RICE DRILLING D LLC | 0 | 0 | 0 |
2017 | RICE DRILLING D LLC | 4303015 | 0 | 349 |
2018 | RICE DRILLING D LLC | 2084440 | 0 | 364 |
2019 | RICE DRILLING D LLC | 302365 | 0 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2016 | RICE DRILLING D LLC | Brine | 4246 | 0 |
2017 | RICE DRILLING D LLC | Brine | 163816 | 349 |
2018 | RICE DRILLING D LLC | Brine | 64080 | 364 |
2019 | RICE DRILLING D LLC | Brine | 8913 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0342236602 | 2016-01-05 | Drill / Deepen / Reopen | No Violations | On my inspection this day, accompanying ODNR Inspector Eric Conrad, Patterson Rig 288 was drilling 12.25 bore hole at a current depth of 6,173 feet. A walk-around inspection of the well pad indicated some deficiencies in secondary containment curbing, specifically flattened curbing at the edge if the rig matts in heavy traffic areas, which were brought to the attention of the Drill Site Manager. |
0996977583 | 2016-01-12 | Drill / Deepen / Reopen | No Violations | On my inspection today, Patterson Drilling Rig 288 was drilling the vertical section at a current depth of 9,781 feet and anticipate starting their Kick-0ff Point for the horizontal section at approximately 9,875 feet. Their anticipated Total Measured Depth is 19,640 feet. A walk-around inspection of the well pad shows that the secondary containment has been improved on the back yard side of the rig by extending liner, rig mats and curbing to include the dry chemical area all the way to the pad earthen berm, with drive-over ramps protecting the high traffic areas. Small slip on far right corner of pad slope has had additional silt fence added below the slip until better weather permits more repair. Current conditions are heavy blowing snow with 3- |
1384230144 | 2018-03-29 | Production Wells | No Violations | The well is equipped with 5.5-inch diameter production casing. The well appears to be free flowing with no artificial lift technology present. The well is piped to a gas processing unit. From there, it is routed to a production area that contains six 400-barrel production fluid holding tanks. Annular pressures read on the gauges provided appeared to be 1500 pounds on the outside of the 5.5-inch diameter casing and the inside of the 9.625-inch diameter casing. A gauge for the inside of the 13.375-inch diameter casing and the outside of the 9.625- |
1445261668 | 2015-10-05 | Casing String Witnessed | No Violations | On this day Falcon Drilling Rig # 23 had reached a total depth of 1120. The 18.625 casing was ran into a 22 open hole to a depth of 1114. Halliburton cement company was on site to cement the casing with 570 sacks of Class H cement. Cement to surface established. See cement ticket for details. |
1453402405 | 2016-01-21 | Drill / Deepen / Reopen | No Violations | On my inspection today, Patterson Drilling Rig 288 has reached Total Measured Depth of 19,640 feet and is nearly finished setting in place their 5.5 inch production casing. Baker Hughes is on site and is partially rigged-up waiting to cement the casing. A walk-around inspection of the well pad shows that the secondary containment is still well maintained around the rig, all auxiliary equipment, and chemicals. |
1964496530 | 2016-02-01 | Preliminary Restoration | No Violations | On this day this site appeared to be in satisfactory condition. Erosion and sediment controls are in place and functioning properly. Preliminary Restoration for this site has passed. |
2029093151 | 2016-01-05 | Drill / Deepen / Reopen | No Violations | I am accompanied by inspector Nicholson. Our inspection finds the drilling contractor, Patterson Drilling is drilling a 12.25 borehole at a depth of 6177. The anticipated total depth of this section is 9700. Deficiencies in the containment system were pointed out to the company representative as well as, an erosion channel that is forming at the south end of the pad. |
2066981251 | 2017-06-14 | Completion Testing | No Violations | During this inspection, the well was currently in the flow back phase of completion. There was piping from the well that lead to a sand separating unit and then to the 500 barrel fluid storage tanks. There was a total of ten 500 barrel fluid storage tanks on site. The tank battery on site contained four 400 barrel production fluid holding tanks and there were also gas processing units on site. |
For data sources see[10]